ENS 43012
ENS Event | |
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18:33 Sep 29, 2006 | |
Title | Invalid Specific System Actuation |
Event Description | On September 29, 2006, at 1:33 pm CDT, a safety-related 120VAC distribution panel was inadvertently de-energized during a planned shift of its power supply. The plant was operating at 100 percent power at the time. The loss of power resulted in the automatic closure of primary containment isolation valves in the reactor water cleanup and the suppression pool cooling/cleanup systems. This event is being reported in accordance with 10CFR50.73(a)(1) as an invalid actuation of the containment isolation valves affecting more than one system.
This event occurred during a planned shift of the inverters that supply the distribution panel. This shift was being performed to support post-maintenance testing of one of the inverters. The operators performing the shift were utilizing the appropriate procedure. At a certain point in the procedure, the off-going inverter was deenergized, and the operators discussed the expected equipment response. Following that discussion, a step was erroneously performed out of sequence, resulting in the loss of power to the 120VAC distribution panel. The primary containment isolation signal was actuated as designed, and the appropriate valves responded correctly. Reactor power was not affected by the containment isolation signal. The pertinent response procedures were implemented, and actions were taken to restore the distribution panel to service. This was completed at 5:31 pm CDT that day. The licensee will notify the NRC Resident Inspector. |
Where | |
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River Bend Louisiana (NRC Region 4) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1407.03 h58.626 days <br />8.375 weeks <br />1.927 months <br />) | |
Opened: | Danny Williamson 10:35 Nov 27, 2006 |
NRC Officer: | Bill Gott |
Last Updated: | Nov 27, 2006 |
43012 - NRC Website | |
Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 541212019-04-30T11:50:00030 April 2019 11:50:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification Due to Invalid Actuation of a General Containment Isolation Signal ENS 517842016-01-10T08:43:00010 January 2016 08:43:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of the Primary Containment Isolation Logic ENS 510032015-02-24T22:02:00024 February 2015 22:02:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephone Notification of Invalid System Actuation Due to Motor Generator Output Breaker Trip ENS 507742014-12-06T16:12:0006 December 2014 16:12:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Optional Report - Half Scram and a Division 2 Primary Containment Isolation Signal ENS 468442011-03-20T12:24:00020 March 2011 12:24:00 10 CFR 50.73(a)(1), Submit an LER "a" Train Reactor Protection System Unexpectedly De-Energized Resulting in a Half Scram Signal ENS 445172008-08-01T00:30:0001 August 2008 00:30:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves Due to a Power Failure ENS 443472008-06-02T11:24:0002 June 2008 11:24:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation of Division 1 Containment Isolation Valves ENS 442782008-04-23T20:56:00023 April 2008 20:56:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Notification of Invalid Specified System Actuation ENS 430122006-09-29T18:33:00029 September 2006 18:33:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specific System Actuation ENS 408472004-05-22T09:29:00022 May 2004 09:29:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Division 1 Primary Containment Isolation Due to Loss of a Rps Bus 2019-04-30T11:50:00 | |