Pages that link to "05000395/LER-1982-044, Forwards LER 82-044/01T-0.Detailed Event Analysis Encl"
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The following pages link to 05000395/LER-1982-044, Forwards LER 82-044/01T-0.Detailed Event Analysis Encl:
Displayed 21 items.
- ML20070G952 (redirect page) (← links)
- 05000395/LER-1982-044 (redirect page) (← links)
- 05000395/LER-1982-046, Forwards LER 82-046/03L-0.Detailed Event Analysis Encl (← links)
- 05000395/LER-1982-037, Forwards LER 82-037/03L-0.Detailed Event Analysis Encl (← links)
- 05000395/LER-1982-036, Forwards LER 82-036/03L-0.Detailed Event Analysis Encl (← links)
- 05000395/LER-1982-064, Forwards LER 82-064/03L-0.Detailed Event Analysis Encl (← links)
- 05000395/LER-1982-066, Forwards LER 82-066/03L-0.Detailed Event Analysis Encl (← links)
- 05000395/LER-1982-063, Forwards LER 82-063/03L-0.Detailed Event Analysis Encl (← links)
- 05000395/LER-1982-062, Forwards LER 82-062/03L-0.Detailed Event Analysis Encl (← links)
- 05000395/LER-1982-003, Forwards LER 82-003/03L-0 (← links)
- 05000395/LER-1982-044-01, /01T-0:on 821202,surveillance Test Performed on 821005 for RHR Pump a Signed Off Approved When Acceptance Criteria Not Met.Caused by Personnel Error Due to Lack of Experience (← links)
- 05000395/LER-1982-048-03, /03L-0:on 821117,condensate Polisher Backwash Water Released to Site Settling Ponds W/O Sampling.Caused by Inadequate Procedures for Release Process.Station Order Generated to Address Group Interface Prior to Release (← links)
- 05000395/LER-1982-047-03, /03L-0:on 821118,operations Personnel Failed to Document Tavg on 30-minute Basis Greater than 551 Degrees w/Tavg-Tref Deviation Alarm Not Reset.Caused by Failure of Operator to Recognize Surveillance Requirements (← links)
- 05000395/LER-1982-049-03, /03L-0:on 821118,Surveillance Requirement 4.7.9.1.1(e) Not Performed on Fire Suppression Water Sys. Caused by Fire Protection Group Being Unaware of Mode 6 Restriction.Personnel Counseled & Tracking Program Updated (← links)
- 05000395/LER-1982-043-03, /03L-0:on 821113,nuclear Instrumentation Power Range Channel (N42) low-range Trip Setpoint Found Set at 50% Instead of 25% of Rated Thermal Power.Caused by Personnel error.Low-range Trip Setpoint Reset (← links)
- 05000395/LER-1982-039-03, /03L-0:on 821108,steam Generator Steam Flow Transmitter (FT-476) Power Supply Found Defective.Caused by Failure on Transmitter Power Supply (FQY-476).Channel Placed in Tripped Condition.Circuit Board Replaced & Tested (← links)
- 05000395/LER-1982-034-03, /03L-0:on 821103,during Mode 4,radiation Monitor RM-G19C (Main Steam Line C Monitor) Failed to High Radiation Alarm Setpoint.Caused by Moisture Penetration of Cable Connectors Between Detector & Preamp.Detector Replaced (← links)
- 05000395/LER-1982-036-03, /03L-0:on 821103,plant Entered Mode 3 W/Control Room Evacuation Panel Pressurizer Relief Tank Level Indicator LI-470A Inoperable.Caused by Level Transmitter Being Out of Calibr.Transmitter Calibr (← links)
- 05000395/LER-1982-026-03, /03L-0:on 821019,operator Noticed Frequent Auto Reactor Coolant Makeup to Vol Control Tank of Chemical Vol & Control Sys.Caused by Cracked Safety Injection Filter B Vent Valve.Leak Test Performed W/Results of 12 Gpm (← links)
- 05000395/LER-1982-025-03, /03L-0:on 821020,during Performance of Surveillance Test Procedure,Porv PCV-445A Found Leaking. Caused by Degraded Seat/Disk Interface Due to Steam Impingement.Valves Will Be Repaired (← links)
- 05000395/LER-1982-021-03, /03L-0:on 821011,steam Line Pressure Dropped Below Tech Spec Min.Caused by Safety Valve 2806P Inadvertently Lifting After Being Freed from stuck-closed Position.Valve & Power Range Neutron Flux High Setpoint Reset (← links)