ENS 42847
ENS Event | |
---|---|
08:05 Sep 19, 2006 | |
Title | Pressurizer Heater Capacity Less Than Tech Spec Limit |
Event Description | The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73.
On September 19, 2006, at approximately 01:05 hours Mountain Standard Time (MST), Palo Verde Nuclear Generating Station (PVNGS) Unit 1 commenced a reactor shutdown required by Technical Specification 3.0.3. Limiting Condition for Operability (LCO) 3.0.3 requires the unit shall be placed in a Mode or other specified condition in which the LCO is not applicable when an LCO is not met and the associated ACTIONS are not met, an associated ACTION is not provided, or if directed by the associated ACTIONS. LCO 3.4.9 Pressurizer, requires two groups of pressurizer heaters OPERABLE with the capacity of each group > [greater than] 125 Kw and capable of being powered from an emergency power supply. TS LCO 3.0.3 and 3.4.9.B were entered at 22:35 hours an 09/18/06 when the Pressurizer Class Heaters were declared INOPERABLE. Engineering personnel with input from the heater manufacturer informed the Unit 1 SM [Shift Manager] and STA that reasonable assurance of OPERABILITY no longer exists. Prompt Operability Determination research to date concludes that the Heaters will not perform their design function for the specified mission time. The heaters were meggered and showed low resistance. There is no affect on Units 2 and 3. LCO 3.4.9.B is in affect for modes 1-3. The licensee intends to go to mode 3 and will evaluate continuing to mode 5. The licensee notified the NRC Resident Inspector. |
Where | |
---|---|
Palo Verde ![]() Arizona (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition | |
Time - Person (Reporting Time:+-3.95 h-0.165 days <br />-0.0235 weeks <br />-0.00541 months <br />) | |
Opened: | Brad Eklund 04:08 Sep 19, 2006 |
NRC Officer: | Mark Abramovitz |
Last Updated: | Sep 19, 2006 |
42847 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 42847\u003C/a\u003E - \u003Ca href=\"/Palo_Verde\" title=\"Palo Verde\"\u003EPalo Verde\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EPressurizer Heater Capacity Less than Tech Spec Limit\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 42847 - Palo Verde\n","link":"","lat":33.386894444444444,"lon":-112.86263333333333,"icon":"/w/images/9/93/Arizona_Public_Service_icon.png"}],"imageoverlays":null} | |
Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
Palo Verde ![]() | |
WEEKMONTHYEARENS 539682019-04-01T03:06:0001 April 2019 03:06:00
[Table view]10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Unanalyzed Condition Due to Eccs Leakage ENS 520832016-07-12T20:00:00012 July 2016 20:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Degraded Fire Barrier ENS 506002014-11-06T18:16:0006 November 2014 18:16:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Dropped Control Element Assembly ENS 496012013-12-03T06:24:0003 December 2013 06:24:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Shutdown Due to Dropped Control Element Assembly ENS 494112013-10-04T16:46:0004 October 2013 16:46:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Postulated Fire Event Could Result in a Hot Short That Could Adversely Impact Safe Shutdown Equipment ENS 488142013-03-09T02:21:0009 March 2013 02:21:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Spent Fuel Pool Criticality Analysis of Record Not Revised Following Power Uprate ENS 474592011-11-19T15:28:00019 November 2011 15:28:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition the Low Pressure Safety Injection System Was Subjected to High Pressure Resulting in Both Trains Being Declared Inoperable ENS 448462009-02-11T20:18:00011 February 2009 20:18:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Possibly Inadequate Backup Nitrogen Supply for Atmospheric Dump Operation ENS 442742008-06-06T06:56:0006 June 2008 06:56:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Shutdown Due to Leak in Safety Injection Tank Vent Line ENS 438042007-11-24T05:26:00024 November 2007 05:26:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Plant Shutdown Due to Inoperable Load Sequencer ENS 437362007-10-22T10:11:00022 October 2007 10:11:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Shutdown Due to Inoperable Steam Driven Auxiliary Feedwater Pump ENS 431732007-02-19T21:57:00019 February 2007 21:57:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit 2 Performed a Ts Required Shutdown ENS 431402007-02-03T19:32:0003 February 2007 19:32:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Technical Specification 3.0.3 Entered During Routine Surveillance Testing of Control Element Assemblies (Cea'S) ENS 428472006-09-19T08:05:00019 September 2006 08:05:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Pressurizer Heater Capacity Less than Tech Spec Limit ENS 427322006-07-27T02:00:00027 July 2006 02:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Limiting Condition for Operation 3.7.4 Deemed to Be Nonconservative ENS 424872006-04-10T19:33:00010 April 2006 19:33:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit 2 Entered a Ts Required Shutdown Due to Inoperable Auxiliary Feedwater Pumps ENS 420502005-10-11T23:02:00011 October 2005 23:02:00 10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Shutdown of Both Unit 2 and 3 ENS 419392005-08-22T23:05:00022 August 2005 23:05:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown Due to Core Protection Calculator System (Cpcs) Software Not Consistent with System Design Requirements. ENS 419132005-08-12T07:19:00012 August 2005 07:19:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Entered Lco Action Statement 3.8.1 to Be in Mode 5 Due to Unit 1 "B" Diesel Gen. Being Declared Inoperable ENS 417892005-06-23T15:23:00023 June 2005 15:23:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unit 2 Aux Feedwater Train Separation Not Maintained During Operation ENS 415022005-03-18T22:00:00018 March 2005 22:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Inoperable Diesel Generator ENS 413892005-02-09T08:04:0009 February 2005 08:04:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specifications Required Shutdown Due to Loss of Normal and Alternate Power to Safety Bus ENS 405032004-02-03T22:35:0003 February 2004 22:35:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Technical Specification Required Shutdown Due to Rcs Pressure Boundary Leakage 2019-04-01T03:06:00 | |