ENS 47812
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ENS Event | |
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21:57 Apr 6, 2012 | |
Title | Local Leak Rate Test Results Exceed Pathway Technical Specification Limits |
Event Description | Appendix J local leak rate testing has determined that secondary containment bypass leakage (SCBL) has been exceeded for Unit 1. During performance of leak rate test SE-159-026 for X-9A penetration it was determined the combined SCBL limit of 15 scfh [standard cubic feet per hour] for as-found minimum pathway was exceeded as specified in Tech Spec SR 3.6.1.3.11.
Acceptance criteria test results were within acceptance criteria for the 10CFR50 Appendix J limits of 0.6 La. This event is being reported as a degraded or unanalyzed condition pursuant to 10CFR50.72(b)(3)(ii). Licensee corrective actions are to repair the identified valve seats. The licensee has notified the NRC Resident Inspector. |
Where | |
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Susquehanna Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded | |
LER: | 05000348/LER-2012-004 05000387/LER-2012-003 |
Time - Person (Reporting Time:+-1.4 h-0.0583 days <br />-0.00833 weeks <br />-0.00192 months <br />) | |
Opened: | Ron Fry 20:33 Apr 6, 2012 |
NRC Officer: | Vince Klco |
Last Updated: | Apr 6, 2012 |
47812 - NRC Website
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WEEKMONTHYEARENS 564342023-03-26T20:03:00026 March 2023 20:03:00
[Table view]10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Degraded Condition - Leak Rate Limits Exceeded ENS 519872016-06-08T06:26:0008 June 2016 06:26:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Discovery of Unisolable Reactor Pressure Boundary Leakage ENS 519832016-06-06T09:56:0006 June 2016 09:56:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Isolable Leakage Identified from Seal Water Line Weld Inside Rcs Pressure Boundary ENS 515382015-11-13T22:45:00013 November 2015 22:45:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Degraded Condition of Leakage from Pump Lower Seal Weld ENS 509762015-04-11T13:58:00011 April 2015 13:58:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Drywell Leakage Point Identified ENS 506862014-12-13T22:00:00013 December 2014 22:00:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Degraded Reactor Coolant Pressure Boundary ENS 500612014-04-27T03:22:00027 April 2014 03:22:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Minimum Pathway Limit of Msiv Combined Leakage Exceeded During Surveillance Testing ENS 493512013-09-16T18:55:00016 September 2013 18:55:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Degraded Condition Caused by Rhr Relief Valve Leakage ENS 480362012-06-19T21:20:00019 June 2012 21:20:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Mode Change Required by Technical Specifications ENS 478122012-04-06T21:57:0006 April 2012 21:57:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Local Leak Rate Test Results Exceed Pathway Technical Specification Limits ENS 457672010-03-15T13:46:00015 March 2010 13:46:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Secondary Containment Bypass Leakage Exceeded Technical Specification Limit ENS 432252007-03-09T18:45:0009 March 2007 18:45:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Secondary Containment Bypass Leakage Rate Exceeded ENS 424072006-03-12T07:17:00012 March 2006 07:17:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Llrt Test Identified Piping Penetration with Excessive Leakage ENS 415062005-03-21T03:30:00021 March 2005 03:30:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Pressure Boundary Leakage Discovered During Hydro Test ENS 406052004-03-23T12:46:00023 March 2004 12:46:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Indication of Crack Failure on Rcs Pressure Boundary Penetration ENS 405662004-03-04T10:20:0004 March 2004 10:20:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Rcic Steam Supply Failed Llrt 2023-03-26T20:03:00 | |
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