05000267/LER-1980-030-03, /03L-0:on 800604,while Performing Leakage Test, Discovered That Loop 2 Steam Generator Penetration Leakage Exceeded Allowable Limit.Cause Unknown.Temporary Relief from Allowable Limit Received from NRC

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/03L-0:on 800604,while Performing Leakage Test, Discovered That Loop 2 Steam Generator Penetration Leakage Exceeded Allowable Limit.Cause Unknown.Temporary Relief from Allowable Limit Received from NRC
ML19320B323
Person / Time
Site:  
Issue date: 07/02/1980
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19320B321 List:
References
LER-80-030-03L, LER-80-30-3L, NUDOCS 8007100176
Download: ML19320B323 (1)


LER-1980-030, /03L-0:on 800604,while Performing Leakage Test, Discovered That Loop 2 Steam Generator Penetration Leakage Exceeded Allowable Limit.Cause Unknown.Temporary Relief from Allowable Limit Received from NRC
Event date:
Report date:
2671980030R03 - NRC Website

text

NRC FORM 366 U. S. NUCLE AR REGULATORY COMMISSION ml7 77)

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LICENSEE EVENT REPORT i

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8 60 61 DOCK ET NUV8 ER 63 69 EVENT DATE 74 75 RE* ORT CATE 80 l

EVENT DESCRIPTION AND PROB ABLE CONSEOUENCES I o 12 ( l On June 4, 1980, during normal power operation while nerforming SR 5. 2.16a-m, Loop 2 l

[ steam generator penetration leakage apoeared to be greater than the 400 pounds oer davl I o 13 l I o i 4 I l limit o f LCO 4.2.9.

Further testing revealed the leakage was less then 400 counds cer!

I o 15 l t day and appeared to be internal to the steam eenerator not through the seals. No l

1o is l I similar reportable occurrences. There was no affect on public health or safetv.

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,i j o l l Cause of the interspace leakaze is not known at this time.

Temocrarv relief from the l lijijiLCO limit of 400 pounds per day was recuested and received from the NRC.

The eroblem I i,,7, l will be investigated and repairs made as recuired durinz the next refueline shutdown. l l Results will be submitted in a future supplemental recert7 l

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