05000313/LER-1980-027-04, /04L-0:on 800725,average Gas Release Rate for Third Quarter 1980 Is 4.47% of Release Rate Per Tech Specs. Caused by Reactor Bldg Purge Following Shutdown to Correct Steam Generator Tube Leak.Failed Fuel Will Be Rotated

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/04L-0:on 800725,average Gas Release Rate for Third Quarter 1980 Is 4.47% of Release Rate Per Tech Specs. Caused by Reactor Bldg Purge Following Shutdown to Correct Steam Generator Tube Leak.Failed Fuel Will Be Rotated
ML19344E366
Person / Time
Site: Arkansas Nuclear 
Issue date: 08/22/1980
From: Bramlett L
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19344E365 List:
References
LER-80-027-04L, LER-80-27-4L, NUDOCS 8008280454
Download: ML19344E366 (1)


LER-1980-027, /04L-0:on 800725,average Gas Release Rate for Third Quarter 1980 Is 4.47% of Release Rate Per Tech Specs. Caused by Reactor Bldg Purge Following Shutdown to Correct Steam Generator Tube Leak.Failed Fuel Will Be Rotated
Event date:
Report date:
3131980027R04 - NRC Website

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8 60 61 DOCK Ei hum 8 g n Mt 69 EvtNT oats se 75 REPORT DATE A0 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h io p; ' The averaae aross cas release rate for the 3rd Quarter 1980 is 4.47% of i FCTT1 I the release rate per T.S. 2.4.2.3.a.

Reportable pcr ETS 5.6.2.b.

LER i 50 313/80-006 was a simi.lar occurrence.

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