LER-1976-006, /01T-0:on 760624,during Normal Operation,Routine Safety Injection Tank Makeup Was Performed Per Plant Procedure.Acceptance Criteria Not Met.Caused by Change 117, Suppl 3,requiring Limits on Boron Concentration |
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EEVT DESCRIPTION Duri g normal operation a routine safety injection tank makeup was performed according to approved plant procedures.
The supervisor completing the procedure contacted higher supervision indicating he could not meet the acceptance criteria of the procedure and questioned the reason for the upper limit on Boron concentration.
The supervisor was informed that the acceptance criteria upper limit was based on the new accident analysis limit for boron precipitation.
Even through the safety injection tank boron concentration was' exactly at the safety analysis limit and greater than the conservative acceptance criteria of the procedure the concentration could not be decreased.
due to time limitations on the length of time the safety injection tank recirculation valve may be open during the month imposed by Technical Specification Change No. 126.
A subsequent review of procedures completed since start up of Core XII revealed that on ten (10) occasions the acceptance criteria had been exceeded during makeup without any corrective action and three (3) of these exceeded the safety analysis limit of 2400 ppm.
This incident is reported as Reportable Occurrence 50-29/76-06.
CAUSE DESCRIFFION Change 117, Supplement 3, Enclosure A required specific r.pper limits,
on boron concentration in the safety injection tank, safety injection accumulator and Main Coolant system to preclude boron precipitation in the unlikely event of a loss of coolant accident.
The potential consequences from this incident have been found to be minimal since a calculation of total ppm of boron based on volume weighed average conc.entration was less than that assumed in the accident analysis.
Previous cores had not required an upper limit on boron concentration.
Though the makeup procedure had been revised consistant with the safety analysis, the procedure had been performed with apparent disregard for the acceptance criteria.
Consequently, the boron concentration linits were exceeded in an attempt to leave a conservative margin to the low limit.
Chemistry calculations for makeup did not consider a high limit for similar reasons.
The personnel involved were reminded of their responsibilities to l
strictly adhere the plant procedure requirements.
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U.S. NUCLEAR REGULA'ORY COM ION DOCKET NUMLE R
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FROM:
DATE oF DOCUMENT Yankee Atomig -Electric Company 7/8/76
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Mr. J. P. O'Re'lly Rowe, Mass.
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i DATE RECEIVED
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Mr. Herbert A. Autio 7/10/76 ILETTER ONoToRIZE D PROP INPUT FORM NUMBER oF COPIES RECEIVED DoAIGINAL
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's ENCLOSURE Ltr. trans the following:
Licensee Eve t Report (R0 S0-29/76-06/01T) on 6/24/76 concerning a routine safety injection tank makeup being performed and not meeting the acceptance criteria of the procedure.
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| 05000029/LER-1976-001, Forwards LER 76-001/03L-0 | Forwards LER 76-001/03L-0 | | | 05000029/LER-1976-001-03, /03L-0:on 760204,slight Leakage from Charging Pump 3 Found in Two Areas,Relief Valve Discharge Flange & Pump Suction Tee to Valve Line Welds.Caused by Vibration Induced Fatigue Failure.Flange & Tee Replaced | /03L-0:on 760204,slight Leakage from Charging Pump 3 Found in Two Areas,Relief Valve Discharge Flange & Pump Suction Tee to Valve Line Welds.Caused by Vibration Induced Fatigue Failure.Flange & Tee Replaced | | | 05000029/LER-1976-002, Forwards LER 76-002/03L-0 | Forwards LER 76-002/03L-0 | | | 05000029/LER-1976-002-03, /03L-0:on 760210,auxiliary Operator Noted Leak in Weld on Reducer Discharge Header of Charging Pump 3.Caused by Vibration Induced Fatigue Failure,Due to Continuous Operation of Displacement Charging Pump | /03L-0:on 760210,auxiliary Operator Noted Leak in Weld on Reducer Discharge Header of Charging Pump 3.Caused by Vibration Induced Fatigue Failure,Due to Continuous Operation of Displacement Charging Pump | | | 05000029/LER-1976-003, Forwards LER 76-003/01T-0 | Forwards LER 76-003/01T-0 | | | 05000029/LER-1976-003-01, /01T-0:on 760513,review of ECCS Analysis Found Error in Accident Analysis.Caused by Error in Assumption of Accident Analysis.Reanalysis Performed.Proposed Change to Tech Specs Submitted | /01T-0:on 760513,review of ECCS Analysis Found Error in Accident Analysis.Caused by Error in Assumption of Accident Analysis.Reanalysis Performed.Proposed Change to Tech Specs Submitted | | | 05000029/LER-1976-004, Forwards LER 76-004/03L-0 | Forwards LER 76-004/03L-0 | | | 05000029/LER-1976-004-03, /03L-0:on 761216,during Monthly Test,Hpsi Pump 1 Shaft Housing Seal Was Found to Leak Lightly.Caused by Cut in Gasket.Defective Gasket Replaced | /03L-0:on 761216,during Monthly Test,Hpsi Pump 1 Shaft Housing Seal Was Found to Leak Lightly.Caused by Cut in Gasket.Defective Gasket Replaced | | | 05000029/LER-1976-005-03, /03L-0:on 760520,auxiliary Operator Noted Slight Leakage from Weld on Inlet Charging Pump 3 Relief Valve. Caused by Pullback Gap Not Allowed During Installation of Pipe & Vibration Induced Fatigue Failure | /03L-0:on 760520,auxiliary Operator Noted Slight Leakage from Weld on Inlet Charging Pump 3 Relief Valve. Caused by Pullback Gap Not Allowed During Installation of Pipe & Vibration Induced Fatigue Failure | | | 05000029/LER-1976-005-30, /030-1:on 760520,weld on Inlet to Charging Pump 3 Relief Valve Found Leaking.Caused by Error in Installation of Pipe in Which Full 1/16 Inch Pullback Not Allowed | /030-1:on 760520,weld on Inlet to Charging Pump 3 Relief Valve Found Leaking.Caused by Error in Installation of Pipe in Which Full 1/16 Inch Pullback Not Allowed | | | 05000029/LER-1976-005, Forwards LER 76-005/03L-0 | Forwards LER 76-005/03L-0 | | | 05000029/LER-1976-006, Forwards LER 76-006/01T-0 | Forwards LER 76-006/01T-0 | | | 05000029/LER-1976-006-01, /01T-0:on 760624,during Normal Operation,Routine Safety Injection Tank Makeup Was Performed Per Plant Procedure.Acceptance Criteria Not Met.Caused by Change 117, Suppl 3,requiring Limits on Boron Concentration | /01T-0:on 760624,during Normal Operation,Routine Safety Injection Tank Makeup Was Performed Per Plant Procedure.Acceptance Criteria Not Met.Caused by Change 117, Suppl 3,requiring Limits on Boron Concentration | | | 05000029/LER-1976-007-01, /01T-0:on 760624,investigation of RO 76-06 Revealed That Assumed Boron Concentration of LOCA Analysis Was Exceeded During Hydrostatic Leak Test of Reactor Vessel. Caused by Personnel Error.Personnel Reinstructed | /01T-0:on 760624,investigation of RO 76-06 Revealed That Assumed Boron Concentration of LOCA Analysis Was Exceeded During Hydrostatic Leak Test of Reactor Vessel. Caused by Personnel Error.Personnel Reinstructed | | | 05000029/LER-1976-007, Forwards LER 76-007/01T-0 | Forwards LER 76-007/01T-0 | | | 05000029/LER-1976-008, Updated LER 76-008/010-0:on 760730,review of Rod Ejection Accident Analysis Revealed Error in Method Used for Core 11 Analysis.Caused by Error in Methods & Application of Analysis Codes.Sys of Documentation Control Initiated | Updated LER 76-008/010-0:on 760730,review of Rod Ejection Accident Analysis Revealed Error in Method Used for Core 11 Analysis.Caused by Error in Methods & Application of Analysis Codes.Sys of Documentation Control Initiated | | | 05000029/LER-1976-010, Forwards LER 76-010/01T-0 | Forwards LER 76-010/01T-0 | | | 05000029/LER-1976-010-01, /01T-0:on 760830,during Review of Core 12 Analysis,Error Found in Figure 8-1 of Tech Specs.Caused by Gamma Heating Correction Omitted by Error in Application of Computer Codes | /01T-0:on 760830,during Review of Core 12 Analysis,Error Found in Figure 8-1 of Tech Specs.Caused by Gamma Heating Correction Omitted by Error in Application of Computer Codes | | | 05000029/LER-1976-011, Forwards LER 76-011/03L-0 | Forwards LER 76-011/03L-0 | | | 05000029/LER-1976-011-03, /03L-0:on 760907,slight Leakage Noted from Welded Nipple on Charging Pump 3 Discharge Heater Line.Caused by Failure to Allow 1/16-inch Pull Back Gap During Installation of Weld.Pump Isolated & Nipple Replaced | /03L-0:on 760907,slight Leakage Noted from Welded Nipple on Charging Pump 3 Discharge Heater Line.Caused by Failure to Allow 1/16-inch Pull Back Gap During Installation of Weld.Pump Isolated & Nipple Replaced | | | 05000029/LER-1976-012-01, /01T-0:on 761119,safety Injection Accumulator for Boron Was 30 Ppm Over Tech Specs & 80 Ppm Over Administrative Limits.Investigation Revealed That Std Sodium Hydroxide Titrant Had Concentrations Lower than Predicted | /01T-0:on 761119,safety Injection Accumulator for Boron Was 30 Ppm Over Tech Specs & 80 Ppm Over Administrative Limits.Investigation Revealed That Std Sodium Hydroxide Titrant Had Concentrations Lower than Predicted | | | 05000029/LER-1976-012, Forwards LER 76-012/01T-0 | Forwards LER 76-012/01T-0 | | | 05000029/LER-1976-013-01, /01T-0:on 761128,following Plant Trip from Power, Main Collant Pump 3 Inadvertently Restarted During Scram Recovery.Caused by Jammed Trip Mechanism on Air Circuit Breaker.New Trip Coil Installed | /01T-0:on 761128,following Plant Trip from Power, Main Collant Pump 3 Inadvertently Restarted During Scram Recovery.Caused by Jammed Trip Mechanism on Air Circuit Breaker.New Trip Coil Installed | | | 05000029/LER-1976-013, Forwards LER 76-013/01T-0 | Forwards LER 76-013/01T-0 | | | 05000029/LER-1976-014-03, /03L-0:on 761216,during Performance of OP-4204, Monthly Test of Safety Injection Pumps,High Pressure Safety Injection Pump Shaft Housing Seal Found Leaking.Caused by Cut in Gasket.Defective Gasket Replaced | /03L-0:on 761216,during Performance of OP-4204, Monthly Test of Safety Injection Pumps,High Pressure Safety Injection Pump Shaft Housing Seal Found Leaking.Caused by Cut in Gasket.Defective Gasket Replaced | |
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