LER-1981-009, Combined Leakage in Excess of Allowable Limits Noted from 14 Electrical Penetrations & 23 Valves.Valve Leakage Caused by Valve Seat Deterioration or Limit Switch Drift |
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| 3381981009R03 - NRC Website |
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s UPDATE REPORT - PREVIOUS REPORT DATE JANUARY 28, 1981 hq U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK / / / / / / / (1)
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
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LICENSEE CODE LICENSE NUMBER LICENSE TYPE CAT 0/1/
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E DOCKET NUMBER EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES (10)
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While performing Type B and C containment penetration leak testing, 14 electr- /
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cal penetrations and 23 valves had combined leakage in excess of allowable li- /
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mits. The electrical penetration leakage resulted from leaking mechanical fit-/
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tings outside containment in the nitrogen system. The leaking valves had addi- /
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itional boundary isolation valves or were in closed systems that prevented di- /
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rect contact with the environment. Therefore the health and safety of the pub- /
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lic were not affected. This event is reportable pursuant to T.S. 6.9.1.9.b.
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SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE
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/S/D/ (11) /E/ (12) [X/ (13) /P/E/N/E/T/R/ (14) LX/ (15)
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SEQUENTIAL OCCURRENCE REPORT REVISION LER/R0 EVENT YEAR REPORT NO.
CODE TYPE NO.
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ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FORM SUB. SUPPLIER MANUFACTURER LD/ (18) LZ/ (19) g/ (20) LZ/ (21) /0/0/0/0/ (22) g/ (23) /N/ (24) LA/ (25) /X/9/9/9/ (26)
CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (27)
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Valve leakage was due to deterioration of the valve seats or to limit switch
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drift. Leakage from electrical penetrations was due to leaking piping
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connections.
In all cases, leaking components were reworked or readjusted
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until the leakage was acceptable.
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FACILITY METHOD OF STATUS
% POWER OTHER STATUS DISCOERY DESCRMM (32)
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TYPE B & C TESTING
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ACTIVITY CONTENT I
RELEASED OF RELEASE AMOUNT OF ACTIVITY (35)
LOCATION OF RELEASE (36) l
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PERSONNEL EXPOSURES NDiBER TYPE DESCRIPTION (39) j
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PERSONNEL INJURIES j
NUMBER DESCRIPTION (41) i
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LOSS OF OR DAMAGE TO FACILITY G3) l TYPE
DESCRIPTION
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LZ[ (42) /
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ISSUED DESCRIPTION (45)
NRC USE ONLY l
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NAME OF PREPARER W. R. CARTWRIGHT PHONE (703) 894-5151 l
8.1052,10 25 j
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UPDATED REPORT - PREVIOUS REPC'1T DATE JANUARY 28, 1981 Virginia Electric and Power Company North Anna Power Station, Unit #1
Attachment:
Page 1 of 3 Docket No. 50-338 Report No. LER 81-009/03X-1
Description of Event
While performing Type B and C penetratiou testing, 14 electrical penetrations and 23 valves had combined leakage that exceeded the maximum (0.6La) limit. These valves and electrical penetrations are noted on the attached list.
Probable Consequences of Occurrence The penetrations containing the leaking valves either had additional isolation valves or were in completely closed systems which prevented any direct contact with the environment. There was no throuFh-leakage detected for the electrical penetrations; the problen instead was caused by leaking mechanical fitting located external to the containment.
Therefore, the health and safety of the public were not affected.
Cause of Event
Valve leakage was due to normal deterioration of the valve seats or because of limit switch drift. Electrical penetration leakage was due to leaking connections on the nitrogen system. There was no leakage experienced from the penetration caps.
Immediate Corrective Action
All Type B and C penetrations that exhibited leakage in excess of allowable were repaired or readjusted.
In addition the leakage from all of the Type B or C penetrations (after repair) that were not e sposed to the overall Type A Containment Leakage test were summarized and used as a penalty for the total containment leak rate test. As such, the overall leak rate was less than the 10 CFR 50 Appendix J limit.
Scheduled Corrective Action No further action is required.
Actions Taken to Prevent Recurrence The surveillance program for containment penetrations has been instituted at North Anna in accordance with NRC guidelines. This program is designed to identify potential leakage paths and repair these valves and penetrations on a regularly scheduled basis. Therefore, no further actions are required.
Generic Implications There are no generic implications associated with this event.
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UPDATED REPORT - PREVIOUS REPORT DATE JANUARY 28, 1981 Attachment: Page 2 of 3 Valves Comp. Subcode Valve Code Component Manufacturer 1-CC-559 C
D M-360 1-CC-572 C
D M-360 1-CH-322 C
D E-090 TV-BD-100A F
D F-130 TV-BD-100B F
D F-130 TV-BD-100C F
D F-130 T5-BD-100D F
D F-130 TV-BD-100E F
D F-130 TV-BD-100F F
D F-130 TV-BD-100D F
D F-130 TV-SI-101 F
D F-130 TV-SV-102-1 F
D F-130 MOV-HV-100D B
D F-130 MOV-RS-101A B
D F-130 MOV-SW-103B B
D A-180 MOV-SW-103C B
D A-180 MOV-SW-103D B
D A-180 MOV-SW-104B B
D A-180 MOV-RS-104C B
D A-180 TV-DA-100A F
D F-130 TV-DA-100B F
D F-130 1-SI-79 C
A V-085 1-FP-272 A
D C-620
.. -- o UPDATED REPORT-PREVIOUS REPORT DATE JANUARY 28, 1981 Attachment: Page 3 of 3 Penetration
- Penetration Number Type 1A I-VA-4160V 6B I-III-2(5TW) s000V 10A I-III-3(5TW)-3000V ISA I-III-6(5TW)-3000V 16D I-IA-20(ATW)-480V 18A I-III-8(5TW)-3000V 18B I-III-9(STW)-3000V 19A I-IC-8-480V 20A I-IIB-5-480V 21A I-IIA-3-480V 21C I-IIC-4-480V 21D I-IIC-5-480V 22A I-IIE-6-480V 22B I-IIE-7-480V
- Component Manufacturer - C515
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| 05000339/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000339/LER-1981-001-03, /03L-0:on 810101,average RCS Temp Outside Tech Specs on Two Occasions.First Caused by Vol Control Tank Being Overborated;Second by Overcooling Primary.Steam Generator Blowdown Secured,Rods Withdrawn & RCS Diluted | /03L-0:on 810101,average RCS Temp Outside Tech Specs on Two Occasions.First Caused by Vol Control Tank Being Overborated;Second by Overcooling Primary.Steam Generator Blowdown Secured,Rods Withdrawn & RCS Diluted | | | 05000338/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000338/LER-1981-001-03, /03L:on 810318 & 19,nitrogen Supply Tank Pressure for Associated Pressure Operated Relief Valves Dropped Below Min Required to Operate Valves for Low Temp RCS Overpressurization Protection.Caused by Leaks in Tanks | /03L:on 810318 & 19,nitrogen Supply Tank Pressure for Associated Pressure Operated Relief Valves Dropped Below Min Required to Operate Valves for Low Temp RCS Overpressurization Protection.Caused by Leaks in Tanks | | | 05000338/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000338/LER-1981-002-03, /03L-0:on 801231,pressurizer Power Operated Relief Valve Declared Inoperable Because of Low Nitrogen Gas Supply Tank Pressure in 1-GN-TK-1A.Caused by Excessive Usage of Nitrogen to Cycle Relief Valves to Reduce RCS Pressure | /03L-0:on 801231,pressurizer Power Operated Relief Valve Declared Inoperable Because of Low Nitrogen Gas Supply Tank Pressure in 1-GN-TK-1A.Caused by Excessive Usage of Nitrogen to Cycle Relief Valves to Reduce RCS Pressure | | | 05000339/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000339/LER-1981-002-03, /03L-0:on 801230,w/unit in Mode 1,steam Flow Channel III Became Erratic W/O Any Annunciators or Computer Alarms.Cause Unknown.Channel Placed in Trip Condition, Calibr & Returned to Svc | /03L-0:on 801230,w/unit in Mode 1,steam Flow Channel III Became Erratic W/O Any Annunciators or Computer Alarms.Cause Unknown.Channel Placed in Trip Condition, Calibr & Returned to Svc | | | 05000338/LER-1981-003-03, /03L-0:on 810104,loop 3 Reactor Coolant Flow Protection Channel II,F-1435,found Out of Tolerance High. Caused by Voltage Drift in Flow Transmitter Serving Loop. Channel Recalibr | /03L-0:on 810104,loop 3 Reactor Coolant Flow Protection Channel II,F-1435,found Out of Tolerance High. Caused by Voltage Drift in Flow Transmitter Serving Loop. Channel Recalibr | | | 05000338/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000339/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000339/LER-1981-003-03, /03L-0:on 810104,casing Cool Tank Level Indication LI-RS-203B Failed High.Caused by Frozen Transmitter Due to Heat Tracing Failure.Transmitter Was Thawed Out & Redundant Heat Tracing Turned on | /03L-0:on 810104,casing Cool Tank Level Indication LI-RS-203B Failed High.Caused by Frozen Transmitter Due to Heat Tracing Failure.Transmitter Was Thawed Out & Redundant Heat Tracing Turned on | | | 05000338/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000338/LER-1981-004-03, /03L-0:on 801229,three Motor Operated Valves Failed to Actuate During Containment Depressurization Actuation Functional Test.Caused by Loose Lead on Breaker/ Controller & Water in Motor.Valves Repaired | /03L-0:on 801229,three Motor Operated Valves Failed to Actuate During Containment Depressurization Actuation Functional Test.Caused by Loose Lead on Breaker/ Controller & Water in Motor.Valves Repaired | | | 05000339/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000339/LER-1981-004-03, /03L-0:on 810104,during Mode 1 Operation,Flux Penalty Summing Amplifier Found Failed During Loop Calibr Check.Caused by Faulty NSA Card.Card Replaced & Calibr | /03L-0:on 810104,during Mode 1 Operation,Flux Penalty Summing Amplifier Found Failed During Loop Calibr Check.Caused by Faulty NSA Card.Card Replaced & Calibr | | | 05000338/LER-1981-005-03, /03L-0:on 810105,discovered That Control Room Floor Sleeve 1FC00108 Was Never Resealed After Being Previously Breached for Cable Installation.Caused by Failure of Personnel to Follow Procedures.Sleeve Resealed | /03L-0:on 810105,discovered That Control Room Floor Sleeve 1FC00108 Was Never Resealed After Being Previously Breached for Cable Installation.Caused by Failure of Personnel to Follow Procedures.Sleeve Resealed | | | 05000338/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000339/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000339/LER-1981-005-03, /03L-0:on 810106,greater than 12-step Disagreement Noted Between Individual Rod Position for Rod B08 in Control Bank D & Group Demand Position.Caused by Voltage Drift in Signal Conditioning Card.Indicator Channel Recalibr | /03L-0:on 810106,greater than 12-step Disagreement Noted Between Individual Rod Position for Rod B08 in Control Bank D & Group Demand Position.Caused by Voltage Drift in Signal Conditioning Card.Indicator Channel Recalibr | | | 05000338/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000338/LER-1981-006-03, /03L-0:on 810113,pressurizer Pressure Transmitter PT 1457 Found Out of Calibr.Caused by Instrument Drift. Channel Recalibr | /03L-0:on 810113,pressurizer Pressure Transmitter PT 1457 Found Out of Calibr.Caused by Instrument Drift. Channel Recalibr | | | 05000339/LER-1981-006-03, /03L-0:on 810107,w/unit at 1% Power,Average RCS Temp Less than 541 F on Two Occasions.Caused by Overfeeding Steam Generators Due to Feedwater Control Problems.Condenser Steam Dumps Closed & Reactor Temp Increased | /03L-0:on 810107,w/unit at 1% Power,Average RCS Temp Less than 541 F on Two Occasions.Caused by Overfeeding Steam Generators Due to Feedwater Control Problems.Condenser Steam Dumps Closed & Reactor Temp Increased | | | 05000338/LER-1981-007-99, Plug Found Missing from Tube at Row 1,column 12.On 810202,two More Plugs Found Missing.Caused by Bad Seals.One Tube Was Replugged on 810124.Other Two Tubes Replugged on 810303 | Plug Found Missing from Tube at Row 1,column 12.On 810202,two More Plugs Found Missing.Caused by Bad Seals.One Tube Was Replugged on 810124.Other Two Tubes Replugged on 810303 | | | 05000339/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000339/LER-1981-007-03, /03L-0:on 801230,boron Concentration in Boron Acid Storage Tank C & Boron Injection Tank Below Tech Spec. Probably Caused by Inleakage of Unknown Source.Boric Acid Transferred to Tank C.Investigation of Leak Underway | /03L-0:on 801230,boron Concentration in Boron Acid Storage Tank C & Boron Injection Tank Below Tech Spec. Probably Caused by Inleakage of Unknown Source.Boric Acid Transferred to Tank C.Investigation of Leak Underway | | | 05000338/LER-1981-007, Forwards Updated LER 81-007/99X-1 | Forwards Updated LER 81-007/99X-1 | | | 05000339/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000338/LER-1981-008-03, /03L-0:on 810117,steam Generator a Protection Channel 2 Narrow Range Level Transmitter LT-1475 Found Out of Calibr.Caused by Voltage Drift in Level Transmitter Serving Instrument Loop.Recalibr & Returned to Svc | /03L-0:on 810117,steam Generator a Protection Channel 2 Narrow Range Level Transmitter LT-1475 Found Out of Calibr.Caused by Voltage Drift in Level Transmitter Serving Instrument Loop.Recalibr & Returned to Svc | | | 05000338/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000339/LER-1981-008-03, /03L-0:on 810107,primary Coolant Iodine Isotopic Analysis Not Made within 2-6 Hour Per Tech Spec Re Power Changes Exceeding 15% Per Hour.Caused by Failure of Operations Personnel to Follow Procedures.Sample Analyzed | /03L-0:on 810107,primary Coolant Iodine Isotopic Analysis Not Made within 2-6 Hour Per Tech Spec Re Power Changes Exceeding 15% Per Hour.Caused by Failure of Operations Personnel to Follow Procedures.Sample Analyzed | | | 05000339/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000339/LER-1981-009-03, /03L-0:on 810107,during Leak Test Containment Personnel Hatch Outer Door Leaked Air Past Seals.Caused by Improper Fitup of Door Seals to Frame.Door Adjusted | /03L-0:on 810107,during Leak Test Containment Personnel Hatch Outer Door Leaked Air Past Seals.Caused by Improper Fitup of Door Seals to Frame.Door Adjusted | | | 05000338/LER-1981-009-03, Combined Leakage in Excess of Allowable Limits Noted from 14 Electrical Penetrations & 23 Valves.Valve Leakage Caused by Valve Seat Deterioration or Limit Switch Drift | Combined Leakage in Excess of Allowable Limits Noted from 14 Electrical Penetrations & 23 Valves.Valve Leakage Caused by Valve Seat Deterioration or Limit Switch Drift | | | 05000338/LER-1981-009, Forwards Updated LER 81-009/03X-1 | Forwards Updated LER 81-009/03X-1 | | | 05000338/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000338/LER-1981-010-03, /03L-0:on 810211,w/unit in Mode 6,containment Purge & Exhaust Isolation Sys Was Rendered Inoperable When Power to MOV-HV-100B,D Was Lost.Caused by Fault on High Resistance Connection.Defective Parts Replaced | /03L-0:on 810211,w/unit in Mode 6,containment Purge & Exhaust Isolation Sys Was Rendered Inoperable When Power to MOV-HV-100B,D Was Lost.Caused by Fault on High Resistance Connection.Defective Parts Replaced | | | 05000339/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000339/LER-1981-010-03, /03L-0:on 810113,w/unit at 100% Power,Overspeed Trip of Turbine Driven Auxiliary Feedwater Pump Occurred During Surveillance Testing.Caused by Failure of Turbine Governor to Control Speed.Governor Was Replaced | /03L-0:on 810113,w/unit at 100% Power,Overspeed Trip of Turbine Driven Auxiliary Feedwater Pump Occurred During Surveillance Testing.Caused by Failure of Turbine Governor to Control Speed.Governor Was Replaced | | | 05000338/LER-1981-011-03, /03L-0:on 810117,w/unit in Mode 6,loss of Power to Radiation Monitor Common Alarms Panel Was Experienced for Less than 5 Minutes.Caused by Failure of Electrician to Switch Power to Unit 2 During Unit 1 Trip | /03L-0:on 810117,w/unit in Mode 6,loss of Power to Radiation Monitor Common Alarms Panel Was Experienced for Less than 5 Minutes.Caused by Failure of Electrician to Switch Power to Unit 2 During Unit 1 Trip | | | 05000338/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000339/LER-1981-011-03, /03L-0:on 810114,w/unit at 100% Power,Breaker for 2-QS-P-1A Spray Pump Racked Out & Suction Valve MOV-QS-200A Closed & de-energized.Caused by Dirty Seat on Vent Valve. Valve Seat Cleaned & Disc Lapped | /03L-0:on 810114,w/unit at 100% Power,Breaker for 2-QS-P-1A Spray Pump Racked Out & Suction Valve MOV-QS-200A Closed & de-energized.Caused by Dirty Seat on Vent Valve. Valve Seat Cleaned & Disc Lapped | | | 05000339/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000338/LER-1981-012-03, /03L-0:on 810118,fuel Bldg Supply & Exhaust Fan Suction Dampers Switched to Failed Position,Bypassing Iodine Filter Bank When Control Bank Was Isolated.Caused by Low Outdoor Temp.Dampers Positioned to Exhaust Through Filter | /03L-0:on 810118,fuel Bldg Supply & Exhaust Fan Suction Dampers Switched to Failed Position,Bypassing Iodine Filter Bank When Control Bank Was Isolated.Caused by Low Outdoor Temp.Dampers Positioned to Exhaust Through Filter | | | 05000338/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000339/LER-1981-012-03, /03L-0:on 810121,containment Pressure Protection Channel 3 Failed Low.Caused by Blown Transistor on Loop Power Supply Card,Resulting in Power Loss to Each Comparator in Loop.Failed Card Replaced W/Calibr Card | /03L-0:on 810121,containment Pressure Protection Channel 3 Failed Low.Caused by Blown Transistor on Loop Power Supply Card,Resulting in Power Loss to Each Comparator in Loop.Failed Card Replaced W/Calibr Card | | | 05000339/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000339/LER-1981-013-03, /03L-0:on 810126,containment Hi & hi-hi Pressure Channel III Annunciator Energized.Caused by Instrument Drift in Nonisolated Power Supply Card S/N 5088,increasing Output Voltage.Card Replaced & Channel Calibr | /03L-0:on 810126,containment Hi & hi-hi Pressure Channel III Annunciator Energized.Caused by Instrument Drift in Nonisolated Power Supply Card S/N 5088,increasing Output Voltage.Card Replaced & Channel Calibr | | | 05000338/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000339/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | |
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