LER-1976-013, /01T-0:on 761128,following Plant Trip from Power, Main Collant Pump 3 Inadvertently Restarted During Scram Recovery.Caused by Jammed Trip Mechanism on Air Circuit Breaker.New Trip Coil Installed |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 0291976013R01 - NRC Website |
|
text
i LER 76-13/1T
{lCENSEE EVENT REPORT C
- O~
CON 1em eLOCx:i i
i i
i i
i
--m--->
j 1
6 f
NAME LCENSE NUMBER E
TYPE
@ lM l A lY l Kl Rl Il l0 l0 l-l 0 l 0l 0l 0l 0l-l 0 l 0 l l 4l 1l1l 1l 1l l0l1l 7 89 14 15 25 26 30 31 32 CATEGOAY TYP SO E
DOCKET NuvBER EVENT DATE ACPOAT DATE
@ CONT ]
l l
LTJ W l0 l5 10 l-l0l01 2l 91 l1 l1 l2 l 8 l 7l 6l l1 l2 l1 l 3 l 7 l 6l 7 8 57 58 59 60 61 68 69 74 75 80
EVENT DESCRIPTION
95 I (See Attached Sheet) l 7 89 80 8i I
7 89 80 EI l
7 89 80
@l I
7 89 80 o
I l
7 89 pnuE 80 CE CODE COMPONENT CODE fER M
AC A
VOLATON 8 I El cl LFJ l C I Kl Tl El Rl K l [Nj l WI ll 2l Ol lN l 7 89 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION
@l (See Attached Sheet) l
'7 d9 80 BE I l
7 89 80 1
I I
F ACluTY METHOD OF STATUS
% POWEA OTHEA STATUS OfSCOVERY DISCOVEAY DESCRiPTON y
l 0l 0l 0l l Scram Recovery l
l NA l
J 7 8 9
10 12 13 44 45 46 80 AE E SED OF EL ASE AMOUNT OF ACTMTY LOCATON OF AELEASE L.J LzJ l
n i
I n
I 7 8 9
10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TfPE DESCA:DTION 1
l0l Ol0l Ul NA l
7 89 11 12 13 80 PERSONNEL INJURIES NuveEA DE SC A'PTON 8 1 01 0101 l NA l
7 89 11 12 80 OFFSITE CONSEQUENCES 1
l NA l
7 89 80 LOSS OR DAMAGE TO FACILITY TYPE DEF' ASTION
- - l NA l
1 7 89 10 80 PUBLICITY lNA l
17 7 89 80 ADDITIONAL FACTORS el 1
7 89 80 8011190 33 2
,, l i
7 89 80 NAME: James L. Staub 413-625-6140 PHONE:
s
)
G EVENT DESCRIPTION-i Following a plant trip from power the number three (3) Main Coolant Pump (MCP) was inadvertently restarted during the scram recovery when the No.1, 2400 volt bus was re-energi::ed. The MCP breaker should have opened automatically on loss of power to its bus. The operator was unable to trip the MCP from the Control Board. This event is reported as Reportable Occurrence 50-29/76-13.
CAUSE DESCRIFTION The Westinghouse MCP De Ion Air circuit breaker, 50 DH 250-E, trip.
mechanism had apparently jambed, preventing the trip coil from tripping the breaker, which resulted in the trip coil burning out.
Attempts to manually trip the breaker were also unsuccessful. The breaker was removed from service and inspected. A new trip coil was installed and the breaker was tested. The breaker failed to trip once out of 30 trips. This was considered sufficient cause to replace it with a spare breaker, that tested satisfactorily. The Air Circuit Breaker was disassembled and refurbished, no apparent reason for the binding could be identified. The Breaker will be tested by multiple trips prior to return to service.
2 k
.,__.__.____.._,._..___m.
t,2 m.,
m. p g.#m p e-=
r C <.c n t.
F. le s G
(
MUUEE MGGEC ELEaTDES GGMPLulf
/
.R
-,, c
.Jo-I Rowe,Mawxhusetts 01367 CUMG
=
J Novecher 19, 1976 a-f y
United States Na:1 ear Regulatory Agency c
Office of Inspection and Enfcrccoent Region I-631 Park Avcnue King of Prussia, Pennsylvania 19406 Attenticrt:
Mr. J. P. O'Reilly g
Dear Mr. O'Reilly:
Pursuanc to the recuirmts of T~,..h: ical Specifications Accendix A, Sectica E.2.a (9) the following is reported as Reportsble Occurrence
~
i 50-29/76-12 "Perforun e of structures, systc=s, or ccc:p;nents that require re edial action or corrective ceasures to prevcat operatica in a less conservative canner".
i The safety injwtion acc=ulator boron concentration was found to be 2432 ppa.
Tne safety analysis linits are 2200-2400 p;c.
ik. ever, i
based en time after startup, 2432 paa does not violate barca precipi-tatica cor.centrations follcroing a LCG.
Cnange No.117 Sep. 3 Enclosure j !
A restricts the weighted barca concentratica of:
the reacsor coolant,
}
safety injection tank and the acctenlator to 2314 p;n. Inc weighted i
l concentration is now 203S p;n.
l 'j A more detailed report will be sulnitted 15110 days.
c l l i
i Very truly yours, ht-kch k kJ
~~
(
Herbert A. Autio g
I Plant Superintendent
~~
i e
am..
m.
gggpggy 105 U.S. NUCLE AR REGbL ATOHY coy' 03 TON DOCKET NUMDEH s
- 2 7Gl 59-29
(
FILE tJU'A BE R NRC DISTRIBUTION ron PAF'T 50 DOCKET MATERIAL INCIDENT REPORT 4
' O:
I FROM:
DATE oF DOCUMENT l
T Yankee Atomic Electric Company 12/13/76 u
inss.
DATE RECEIVED
' :r. J. P. O'Leilly
!!r. Herbert A. Au tio 12/16/76 [LE T T E R ONOTORIZED PROP INPUT FORM NUMBER oF COPIES RECEIVE D CoRIGINAL N,J NC L ASSIFIE D One si;ned copy N O*Y
DESCRIPTION
E N CLOSU R E 1
Ltr. trcn; the follo"in;:
Licensee Event Report (R0 50-29/76-13/01T) on 11/25/76 concerning ::o. 3 main Coolant Pump Breaker Failure.
(1-P)
(2-P)
OWLEDGED PLANT NA!G:
DO NOT REliOVE y mn ucc 7.0..,
NOTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J. COLLINS FOR ACTION /INFORMATION 12/16/76 IGL
' [ EP/NCH CHTEF:
Schrencer 3
il W/3 CYS FOR ACTICN g LIC. ASST. :
Sheo,ard i:/
_CYS
/
/
,s ACRSl76 CYS-.J L;.,/S NT : &.g.[_gp[f,-
)
~
INTERNAL DISTRIBUTION
... REG FTLD l
_ NRC FDR I l M I & E (2)
(
i
, ~d IC ?C i SCHROED::R/IPPOLITO i HOUSTON NOVAK/ CHECK I~ 6 G?,I!ES l
CASE EUTLER HANAUER
_ TEDESCO/".ACCARY EISENHUT BAER SHA0 TUOLL_::En /EU_SCH_.
_ KREGER/J. COLLINS
._)
l
~
CONT ROL NUMGER EXTERNAL DISTRIBU'lON
~ LPDR: J.r a :
- telu, a :s.
/
3EC':
[m b[
! SIC.
/A72$
yp::v. w x n o-
's wMi n a la n
/
b " b j j t:j N M 5 k [i #
-( I [i *N m N N.Y b N O
~~
E V
'u / w ka W 12 O ll Od d ld YJ _[" N D mm imC f OHM 195 f 2 7G)
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000029/LER-1976-001, Forwards LER 76-001/03L-0 | Forwards LER 76-001/03L-0 | | | 05000029/LER-1976-001-03, /03L-0:on 760204,slight Leakage from Charging Pump 3 Found in Two Areas,Relief Valve Discharge Flange & Pump Suction Tee to Valve Line Welds.Caused by Vibration Induced Fatigue Failure.Flange & Tee Replaced | /03L-0:on 760204,slight Leakage from Charging Pump 3 Found in Two Areas,Relief Valve Discharge Flange & Pump Suction Tee to Valve Line Welds.Caused by Vibration Induced Fatigue Failure.Flange & Tee Replaced | | | 05000029/LER-1976-002, Forwards LER 76-002/03L-0 | Forwards LER 76-002/03L-0 | | | 05000029/LER-1976-002-03, /03L-0:on 760210,auxiliary Operator Noted Leak in Weld on Reducer Discharge Header of Charging Pump 3.Caused by Vibration Induced Fatigue Failure,Due to Continuous Operation of Displacement Charging Pump | /03L-0:on 760210,auxiliary Operator Noted Leak in Weld on Reducer Discharge Header of Charging Pump 3.Caused by Vibration Induced Fatigue Failure,Due to Continuous Operation of Displacement Charging Pump | | | 05000029/LER-1976-003, Forwards LER 76-003/01T-0 | Forwards LER 76-003/01T-0 | | | 05000029/LER-1976-003-01, /01T-0:on 760513,review of ECCS Analysis Found Error in Accident Analysis.Caused by Error in Assumption of Accident Analysis.Reanalysis Performed.Proposed Change to Tech Specs Submitted | /01T-0:on 760513,review of ECCS Analysis Found Error in Accident Analysis.Caused by Error in Assumption of Accident Analysis.Reanalysis Performed.Proposed Change to Tech Specs Submitted | | | 05000029/LER-1976-004, Forwards LER 76-004/03L-0 | Forwards LER 76-004/03L-0 | | | 05000029/LER-1976-004-03, /03L-0:on 761216,during Monthly Test,Hpsi Pump 1 Shaft Housing Seal Was Found to Leak Lightly.Caused by Cut in Gasket.Defective Gasket Replaced | /03L-0:on 761216,during Monthly Test,Hpsi Pump 1 Shaft Housing Seal Was Found to Leak Lightly.Caused by Cut in Gasket.Defective Gasket Replaced | | | 05000029/LER-1976-005-03, /03L-0:on 760520,auxiliary Operator Noted Slight Leakage from Weld on Inlet Charging Pump 3 Relief Valve. Caused by Pullback Gap Not Allowed During Installation of Pipe & Vibration Induced Fatigue Failure | /03L-0:on 760520,auxiliary Operator Noted Slight Leakage from Weld on Inlet Charging Pump 3 Relief Valve. Caused by Pullback Gap Not Allowed During Installation of Pipe & Vibration Induced Fatigue Failure | | | 05000029/LER-1976-005-30, /030-1:on 760520,weld on Inlet to Charging Pump 3 Relief Valve Found Leaking.Caused by Error in Installation of Pipe in Which Full 1/16 Inch Pullback Not Allowed | /030-1:on 760520,weld on Inlet to Charging Pump 3 Relief Valve Found Leaking.Caused by Error in Installation of Pipe in Which Full 1/16 Inch Pullback Not Allowed | | | 05000029/LER-1976-005, Forwards LER 76-005/03L-0 | Forwards LER 76-005/03L-0 | | | 05000029/LER-1976-006, Forwards LER 76-006/01T-0 | Forwards LER 76-006/01T-0 | | | 05000029/LER-1976-006-01, /01T-0:on 760624,during Normal Operation,Routine Safety Injection Tank Makeup Was Performed Per Plant Procedure.Acceptance Criteria Not Met.Caused by Change 117, Suppl 3,requiring Limits on Boron Concentration | /01T-0:on 760624,during Normal Operation,Routine Safety Injection Tank Makeup Was Performed Per Plant Procedure.Acceptance Criteria Not Met.Caused by Change 117, Suppl 3,requiring Limits on Boron Concentration | | | 05000029/LER-1976-007-01, /01T-0:on 760624,investigation of RO 76-06 Revealed That Assumed Boron Concentration of LOCA Analysis Was Exceeded During Hydrostatic Leak Test of Reactor Vessel. Caused by Personnel Error.Personnel Reinstructed | /01T-0:on 760624,investigation of RO 76-06 Revealed That Assumed Boron Concentration of LOCA Analysis Was Exceeded During Hydrostatic Leak Test of Reactor Vessel. Caused by Personnel Error.Personnel Reinstructed | | | 05000029/LER-1976-007, Forwards LER 76-007/01T-0 | Forwards LER 76-007/01T-0 | | | 05000029/LER-1976-008, Updated LER 76-008/010-0:on 760730,review of Rod Ejection Accident Analysis Revealed Error in Method Used for Core 11 Analysis.Caused by Error in Methods & Application of Analysis Codes.Sys of Documentation Control Initiated | Updated LER 76-008/010-0:on 760730,review of Rod Ejection Accident Analysis Revealed Error in Method Used for Core 11 Analysis.Caused by Error in Methods & Application of Analysis Codes.Sys of Documentation Control Initiated | | | 05000029/LER-1976-010, Forwards LER 76-010/01T-0 | Forwards LER 76-010/01T-0 | | | 05000029/LER-1976-010-01, /01T-0:on 760830,during Review of Core 12 Analysis,Error Found in Figure 8-1 of Tech Specs.Caused by Gamma Heating Correction Omitted by Error in Application of Computer Codes | /01T-0:on 760830,during Review of Core 12 Analysis,Error Found in Figure 8-1 of Tech Specs.Caused by Gamma Heating Correction Omitted by Error in Application of Computer Codes | | | 05000029/LER-1976-011, Forwards LER 76-011/03L-0 | Forwards LER 76-011/03L-0 | | | 05000029/LER-1976-011-03, /03L-0:on 760907,slight Leakage Noted from Welded Nipple on Charging Pump 3 Discharge Heater Line.Caused by Failure to Allow 1/16-inch Pull Back Gap During Installation of Weld.Pump Isolated & Nipple Replaced | /03L-0:on 760907,slight Leakage Noted from Welded Nipple on Charging Pump 3 Discharge Heater Line.Caused by Failure to Allow 1/16-inch Pull Back Gap During Installation of Weld.Pump Isolated & Nipple Replaced | | | 05000029/LER-1976-012-01, /01T-0:on 761119,safety Injection Accumulator for Boron Was 30 Ppm Over Tech Specs & 80 Ppm Over Administrative Limits.Investigation Revealed That Std Sodium Hydroxide Titrant Had Concentrations Lower than Predicted | /01T-0:on 761119,safety Injection Accumulator for Boron Was 30 Ppm Over Tech Specs & 80 Ppm Over Administrative Limits.Investigation Revealed That Std Sodium Hydroxide Titrant Had Concentrations Lower than Predicted | | | 05000029/LER-1976-012, Forwards LER 76-012/01T-0 | Forwards LER 76-012/01T-0 | | | 05000029/LER-1976-013-01, /01T-0:on 761128,following Plant Trip from Power, Main Collant Pump 3 Inadvertently Restarted During Scram Recovery.Caused by Jammed Trip Mechanism on Air Circuit Breaker.New Trip Coil Installed | /01T-0:on 761128,following Plant Trip from Power, Main Collant Pump 3 Inadvertently Restarted During Scram Recovery.Caused by Jammed Trip Mechanism on Air Circuit Breaker.New Trip Coil Installed | | | 05000029/LER-1976-013, Forwards LER 76-013/01T-0 | Forwards LER 76-013/01T-0 | | | 05000029/LER-1976-014-03, /03L-0:on 761216,during Performance of OP-4204, Monthly Test of Safety Injection Pumps,High Pressure Safety Injection Pump Shaft Housing Seal Found Leaking.Caused by Cut in Gasket.Defective Gasket Replaced | /03L-0:on 761216,during Performance of OP-4204, Monthly Test of Safety Injection Pumps,High Pressure Safety Injection Pump Shaft Housing Seal Found Leaking.Caused by Cut in Gasket.Defective Gasket Replaced | |
|