05000306/LER-1981-004-03, /03L-0:on 810406,during testing,turbine-driven Auxiliary Feedwater Pump 22 Failed to Come Up to Rated Speed.Caused by Low Governor Setting.Governor Adjusted to Proper Speed

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/03L-0:on 810406,during testing,turbine-driven Auxiliary Feedwater Pump 22 Failed to Come Up to Rated Speed.Caused by Low Governor Setting.Governor Adjusted to Proper Speed
ML20003H983
Person / Time
Site: Prairie Island 
Issue date: 05/05/1981
From: Hunstad A
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20003H982 List:
References
LER-81-004-03L, LER-81-4-3L, NUDOCS 8105080287
Download: ML20003H983 (1)


LER-1981-004, /03L-0:on 810406,during testing,turbine-driven Auxiliary Feedwater Pump 22 Failed to Come Up to Rated Speed.Caused by Low Governor Setting.Governor Adjusted to Proper Speed
Event date:
Report date:
3061981004R03 - NRC Website

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8 60 61 DOCKET NUMBE R 68 69 EVENT DATE 74 7b RE PORT D ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h Io l2l lDuring testing of No. 22 Turbine-Driven Auxiliary Feedwater Pump after modifications, I Io Iai Ithe pump failed to come up to rated speed. Pump was inoperable during periods with l

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