B13533, Discusses Proposed Rev to Tech Specs Re Facility ESF Actuation Sys Instrumentation Trip Setpoint,Per

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Discusses Proposed Rev to Tech Specs Re Facility ESF Actuation Sys Instrumentation Trip Setpoint,Per
ML20043D045
Person / Time
Site: Millstone Dominion icon.png
Issue date: 05/30/1990
From: Mroczka E
NORTHEAST NUCLEAR ENERGY CO., NORTHEAST UTILITIES
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
B13533, NUDOCS 9006070048
Download: ML20043D045 (3)


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(203) 665 5000 May 30, 1990 Docket No. 50-423 B13533 Re:

100FR50.90 U.S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555

Reference:

E. J. Mroczka letter to the U.S. Nuclear Regulatory Commission, Proposed Revision to Technical Specifications--ESF Actuation System Instrumentation, dated March 30, 1990.

Gentlemen:

Millstone Nuclear Power Station, Unit No. 3 j

Proposed Revision to Technical Specifications ESF Actuation System Instrumentation Trio Set Point (TAC No. 76490)

By letter dated March 30,1990 (reference), Northeast Nuclear Energy Company (NNECO) submitted a proposed revision to the Technical Specifications for Millstone Unit No. 3.

The proposed changes to Technical Spectfication Table 3.3-4 would revise total allowance (TA), sensor error (s), trip set point, and allowable value for turbine trip and feedwater isolation on high-high steam generator water level.

These proposed changes are accomplished by adjusting instrument settings and do not involve any physical addition, deletion, or modification to plant components.

in a subsequent discussion with the Stiff, the NRC requested NNECO to review the current and the proposed set point for high-high steam generator water level to determine if the proposed changes are more or less conservative with regard to "significant hazards consideration" criteria of 10CFR50.92.

The purpose of this letter is to provide the Staff with the requested information.

As stated in the reference, the steam generator high-high level trip provides protection against overfilling the steam generator.

The steam generator high-high water level trip provides engineered safety features actuation i

system (ESFAs) Interlock P-14.

This interlock initiates a feedwater isolation which closes the feedwater isolation valves, stops the main feedwater pumps, and trips the turbine.

The turbine trip then generates a reactor trip although this is not credited in the analysis.

However, this feedwater isolation signal is credited for mitigating the steam generator overfill consequences of an increase in feedwater flow.

The details of the analysis are presented in the Millstone Unit No. 3 Final Safety Analysis Report (FSAR)

Section 15.1.2.

9006070048 900539 fDR ADOCK 05000423 PDC

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U.S. Nuclear Regulatory Commission B13533/Page 2 May 30, 1990 The revised steam generator water level high-high trip set point and other associated values such as total allowance, etc., are calculated by the method-ology described in WCAP-10991, " Westinghouse Setpoint Methodology for Protec-tion System, Millstone Unit No. 3 " which is also the method used in calculat-ing other set points in Table 3.3-4 of the Technical Specifications.

The new set point is based on recent data which indicates that there is more error associated (increased channel statistical allowance for abnormal environmental conditions) with level measurement than previously assumed.

The current set point is at 82 percent narrow-range level.

The proposed revised trip set point is 80.45 percent narrow range level.

Since the new set point better represents the error associated with the level measurement, the change will maintain the assumed performance of ESFAS.

As requested, the following is a revised significant hazards consideration discussion concerning the proposed changes to steam generator high-high water level trip set point.

Sianificant Hazards Consideration NNECO has reviewed the proposed changes in accordance with 10CFR50.92 and has concluded that the changes do not involve a significant hazards consideration.

The basis for this conclusion is that the three criteria of 10CFR50.92(c) are not compromised.

The proposed changes do not involve a significant hazards consideration because they would not:

1.

Involve a significant increase in the probability or consequences of an accident previously analyzed. As stated above, the proposed revised set point will lower the steam generator level (narrow-range) at which a feedwater isolation will result.

The feedwater isolation is credited for mitigating the consequences of an increase in feedwater flow (FSAR Section 15.1.2).

With the current trip set point and considering the effects of temperature compensation shift errors, it is possible that a turbine trip /feedwater isolation signal would not be generated at the same time as assumed in the design basis.

With the proposed revised set point, this signal will be generated as assumed.

Therefore, the ability of.the ESFAS to respond as assumed to mitigate an increase in feedwater flow event is improved.

Therefore, with the proposed changes, the consequences of an increase in feedwater flow event will be bounded by the existing design basis analysis.

Sinc.e there are no hardware changes or changes in surveillance practices, the proposed changes will have a negligible impact on the probability of any accident.

2.

Create the possibility of a new or different kind of accident from that previously analyzed.

There are no physical design changes in plant operating procedures associated with the proposed changes.

The proposed l

l changes revise the set points for high-high steam generator water level i

l including total allowance (TA), 2, sensor error (S), trip set point, and i

allowable value.

Furthermore, the proposed change makes the ESFAS more sensitive to steam generator water level.

No new failure modes are l

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U.S. Nuclear Regulatory Commission B13533/Page 3 May 30, 1990 t

introduced.

Therefore, there can be no impact on plant response to the point where a different accident is created.

3.

Involve a significant reduction in a margin of safety.

The changes have no 41 pact on the consequences of an accident or on any of the protective boundaries.

There is no negative impact on any of the safety systems.

Therefore, there is no reduction in the margin of safety.

We believe the above information, coupled with the information provided in the reference, provides a complete basis for approval of the requested amendment.

Of course, should the Staff have any additional questions, we are available to discuss the Staff's concerns at your earliest convenience.

Very truly yours, NORTHEAST NUCLEAR ENERGY COMPANY z/f M

E. #! Mroczka #

Senior Vice President cc:

T. T. Martin, Region I Administrator D. H. Jaffe, NRC Project Manager, Millstone Unit No. 3 W. J. Raymond, Senior Resident inspector, Millstone Unit Nos.1, 2, and 3 Mr. Kevin McCarthy, Director Radiation Control Unit Department of Environmental Protection Hartford, CT 06116 STATE OF CONNECTICUT)

) ss. Berlin COUNTY OF HARTFORD )

Then personally appeared before me, E. J. Mroczka, who being duly sworn, did state that he is Senior Vice President of Northeast Nuclear Energy Company, a Licensee herein, that he is authorized to execute and file the foregoing information in the name and on behal' of the Licensees herein, and that the statements contained in said information are true and correct to the best of his knowledge and belief.

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