ML20086H451

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Allowed Outage Time Exceeded for Turbine Driven AFW Pump Which Tripped on Overspeed
ML20086H451
Person / Time
Site: Comanche Peak Luminant icon.png
Issue date: 07/14/1995
From: Terry C
TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC)
To: Woodlan D
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20086H454 List:
References
TXX-95190, NUDOCS 9507180146
Download: ML20086H451 (2)


Text

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a Log

  1. TXX 95190 File # 10200 Ref. # 10CFR50.73(a)(2)(1) r

=

1UELECTRIC July 14, 1995 C. Lance Terry Group Vice President. Nuclear U. S. Nuclear Regulatory Commission i

Attn:

Document Control Desk

}

Washington, DC 20555 l

SUBJECT:

COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)-UNIT 1 DOCKET N05. 50-445 l

k CONDITIONS PRDHIBITED BY TECHNICAL SPECIFICATIONS LICENSEE EVENT REPORT 445/95 004 00 REF:

1) TV Electric Letter logged TXX-95196 from Mr. C. L. Terry to the NRC dated July 14, 1995 l
2) TV Electric Letter logged TXX-95167 from Mr. C. L. Terry to the NRC dated June 14, 1995 requesting enforcement discretion for testing of Turbine Driven Auxiliary Feedwater Pump at Mode 3 1
3) NRC letter dated June 15, 1995 from Mr. L. J. Callan to l

Hr. C. L. Terry granting enforcement discretion (N0ED Tracking 95-4 0005)

Gentlemen:

Enclosed is Licensee Event Report (LER) 95 004 00 for Comanche Peak Steam l

l Electric Station Unit 1. " Allowed Outage Time was Exceeded for the Turbine l

Driven Auxiliary Feedwater Pump which Tripped on Overspeed."

Via Reference 1 TU Electric has submitted its Licensee Event Report (LER)95-003 00 for Comanche Peak Steam Electric Station Unit 1. " Loss of Both Condensate and Both Feedwater Pumps Due To Failure of Non-safety Related f

Inverter Resulted in a Manual Reactor Trip." During this aforementioned l

event the Turbine Driven Auxiliary Feedwater Pump actuated due to lo lo l

Steam Generator alarms and subsequently tripped on overspeed. Reference 2 i

requested enforcement discretion to allow CPSES Unit 1 to remain in Mode 3.

I Hot Standby, while testing on the Unit 1 Turbine Driven Auxiliary Feedwater (TDAFW) pump was being performed. The enforcement discretion was granted via reference 3.

The subject Licensee Event Report is being submitted to satisfy the requirements of 10CFR50.73(a)(2)(1)(B), because the time requirements for the action statement were not met (see Reference 2).

Additionally, on June 21, 1995, a TDAFW pump overspeed trip was experienced on CPSES Unit 2 in an event unrelated to this LER.

TV Electric is in the process of evaluating the Unit 2 TDAFW trip, and will submit the evaluation in a supplement to the enclosed LER.

9507180146 c50714 4

PDR ADOCK CS000445 rEu S,

PDR m

Energy Plaza 1601 Bryan Street Dallas, Texas 75201 3411 llI

Y TXX-95190 Page 2 of 2 The supplement to this LER, describing final conclusions of both the Unit 1 and Unit 2 TDAFW pump overspeed trips including the causes and corrective actions, will be issued at a later date.

Sincerely, C. L. Terry O

By:

D. R. Woodlan Docket Licensing Manager OB:ob Enclosure cc:

Mr. L. J. Callan, Region IV Hr. D. F. Kirsch, Region IV Resident Inspectors, CPSES

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