ENS 42063
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ENS Event | |
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05:57 Oct 19, 2005 | |
Title | Automatic Reactor Trip Due to Low 2 Steam Generator Water Level |
Event Description | Unit 2 reactor trip on low 2 S/G level. 2A CD/CB (condensate and condensate booster pump set is driven by a single motor) tripped while 2D CD/CB was out of service. The auto turbine runback was unsuccessful and turbine was runbacked manually. ESF actuations: AF (Auxiliary Feedwater) activation and FWI (Feedwater Isolation)." Only indication on the condensate and condensate booster pump trip was an over current flag.
All rods fully inserted into the core. Both the motor driven and the diesel driven auxiliary feedwater pumps are operating. All Emergency Core Cooling systems and the Emergency Diesel Generators are fully operable if needed. The NRC Resident Inspector was paged by the licensee. |
Where | |
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Byron Illinois (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-3.3 h-0.138 days <br />-0.0196 weeks <br />-0.00452 months <br />) | |
Opened: | Ed Bandis 02:39 Oct 19, 2005 |
NRC Officer: | John Mackinnon |
Last Updated: | Oct 19, 2005 |
42063 - NRC Website
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Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
Byron with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 540202019-04-22T18:24:00022 April 2019 18:24:00
[Table view]10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Initiation of the Auxiliary Feedwater System in Response to a Loss of Feedwater ENS 534912018-07-06T05:00:0006 July 2018 05:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Transformer Failure Causes Loss of Offsite Power to Unit 2 ENS 522952016-10-12T18:38:00012 October 2016 18:38:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Spurious Feedwater Isolation ENS 508592015-03-03T17:01:0003 March 2015 17:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Main Power Transformer Bushing Short ENS 499192014-03-15T16:02:00015 March 2014 16:02:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Momentary Loss of Shutdown Cooling Due to a Loss of Offsite Power ENS 488382013-03-21T00:51:00021 March 2013 00:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Generator Stator Cooling Water ENS 477082012-02-28T23:31:00028 February 2012 23:31:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Due to Loss of Offsite Power ENS 476442012-02-06T23:19:0006 February 2012 23:19:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Rps Actuation Due to Turbine Trip ENS 476242012-01-30T16:01:00030 January 2012 16:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unusual Event Due to Loss of Offsite Power Greater than 15 Minutes ENS 458672010-04-19T10:03:00019 April 2010 10:03:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rps and Afw Actuation Signals While Shutdown in Mode 4 ENS 420632005-10-19T05:57:00019 October 2005 05:57:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Low 2 Steam Generator Water Level 2019-04-22T18:24:00 | |
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