ENS 42687
ENS Event | |
---|---|
07:52 Jul 6, 2006 | |
Title | Reactor Trip Due to Generator Differential |
Event Description | Indian Point Unit 3 tripped on Generator Differential (Direct Generator Trip). Current conditions are stable, mode 3 operation with all automatic actions occurring properly. Steam Generators levels are stable on aux. feed water.
Unit 2 was unaffected by the trip. All control rods inserted fully and decay heat is being removed via steam dump to the condenser. All required safety related systems are working properly and the electrical buses and diesel generators are in their normal alignment. The licensee will notify the NRC Resident Inspector.
The Auxiliary Feedwater System actuated and the Auxiliary Feedwater Pump started as designed due to the reactor trip. The actuation of the Auxiliary Feedwater System was the result of Steam Generator shrink/swell effect due to the reactor trip at full power. The actuation of the Auxiliary Feedwater System is an eight-hour non-emergency event reportable under 10 CFR 50.72(b)(3)(iv). The licensee will notify the NRC Resident Inspector. Notified R1DO (P. Henderson) |
Where | |
---|---|
Indian Point New York (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-3.45 h-0.144 days <br />-0.0205 weeks <br />-0.00473 months <br />) | |
Opened: | Phil Santini 04:25 Jul 6, 2006 |
NRC Officer: | Arlon Costa |
Last Updated: | Jul 6, 2006 |
42687 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 42687\u003C/a\u003E - \u003Ca href=\"/Indian_Point\" title=\"Indian Point\"\u003EIndian Point\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EReactor Trip Due to Generator Differential\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 42687 - Indian Point\n","link":"","lat":41.26799722222222,"lon":-73.9514,"icon":"/w/images/7/79/Entergy_icon.png"}],"imageoverlays":null} | |
Unit 3 | |
---|---|
Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
Indian Point with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 539542019-03-24T18:45:00024 March 2019 18:45:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Automatic Trip on Turbine Trip ENS 539372019-03-15T17:00:00015 March 2019 17:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Generator Trip ENS 536112018-09-18T04:00:00018 September 2018 04:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to a Steam Leak on a High Pressure Feedwater Heater ENS 533482018-04-20T01:07:00020 April 2018 01:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Turbine Issue ENS 532162018-02-16T07:01:00016 February 2018 07:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Trip Due to Loss of Excitation on Main Generator ENS 530522017-11-04T00:22:0004 November 2017 00:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Indian Point Unit 3 Reactor Trip on Low Steam Generator Level ENS 528292017-06-26T04:00:00026 June 2017 04:00:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Main Feedpump ENS 520672016-07-06T13:38:0006 July 2016 13:38:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip While Performing Testing ENS 517752016-03-07T15:18:0007 March 2016 15:18:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generators Auto-Started on Valid Actuation Signal ENS 516062015-12-15T00:06:00015 December 2015 00:06:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Main Generator Lockout ENS 515862015-12-05T22:31:0005 December 2015 22:31:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Initiated Due to Multiple Dropped Control Rods ENS 512112015-07-08T18:25:0008 July 2015 18:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Lowering Steam Generator Water Levels ENS 511562015-06-15T23:20:00015 June 2015 23:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Turbine Trip ENS 510602015-05-09T21:50:0009 May 2015 21:50:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Main Transformer Fire ENS 503612014-08-13T15:57:00013 August 2014 15:57:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 498022014-02-06T20:53:0006 February 2014 20:53:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unanticipated Auxiliary Feedwater Pump Start After Securing Emergency Diesel Generator ENS 496982014-01-07T02:15:0007 January 2014 02:15:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Steam Generator Water Level Due to a Failed Main Feedwater Reg Valve ENS 491712013-07-03T11:41:0003 July 2013 11:41:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Following Loss of Instrument Air to Main Feedwater Regulating Valves ENS 488542013-03-27T10:01:00027 March 2013 10:01:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Safety Injection Actuation During Testing ENS 487502013-02-13T18:55:00013 February 2013 18:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip on Low Steam Generator Water Level ENS 484542012-10-30T02:41:00030 October 2012 02:41:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Rps Actuation on Generator Trip ENS 479992012-06-06T10:12:0006 June 2012 10:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Experienced an Automatic Reactor Trip on Turbine Main Generator Trip ENS 475822012-01-10T09:36:00010 January 2012 09:36:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Excessive Leakage from Rcp Seal Return ENS 471772011-08-19T22:05:00019 August 2011 22:05:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Partial Loss of Offsite Power Resulting in Edg Autostart ENS 466492011-03-01T16:00:0001 March 2011 16:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generators Start on a Loss of Power from 138 Kv Circuit ENS 464002010-11-07T23:39:0007 November 2010 23:39:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Alert Declared Due to Explosion in the 21 Main Transformer ENS 462412010-09-10T01:29:00010 September 2010 01:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Service Water Leak in the Main Generator Exciter Housing ENS 462292010-09-03T14:58:0003 September 2010 14:58:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Experienced an Automatic Reactor Trip Due to High Steam Generator Level ENS 456242010-01-11T20:59:00011 January 2010 20:59:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Trip Due to Main Generator Electrical Trip ENS 454742009-11-03T02:41:0003 November 2009 02:41:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Turbine Trip Caused by a Generator Lock-Out Relay Actuation ENS 453062009-08-27T23:45:00027 August 2009 23:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip ENS 452552009-08-11T00:32:00011 August 2009 00:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Indian Point Unit 3 Automatically Tripped During Thunderstorm ENS 450982009-05-28T10:25:00028 May 2009 10:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Resulting from a High Steam Generator Level Turbine Trip ENS 450692009-05-15T05:53:00015 May 2009 05:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Failure of the Main Feedwater Regulating Valve ENS 449672009-04-03T15:36:0003 April 2009 15:36:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of 21 Mbfp ENS 447492009-01-02T15:09:0002 January 2009 15:09:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unexpected Autostart of Emergency Diesel Generator During Surveillance Testing ENS 445542008-10-09T16:54:0009 October 2008 16:54:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator and Auxillary Feedwater Actuation Due to Bus Undervoltage ENS 443832008-08-04T16:00:0004 August 2008 16:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuation - Both Auxiliary Boiler Feedwater Pumps Started Unexpectedly ENS 441532008-04-21T15:25:00021 April 2008 15:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Lowering Steam Generator Water Level ENS 440912008-03-25T15:18:00025 March 2008 15:18:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Inadvertent Actuation of Emergency Diesel Generator During Surveillance Testing ENS 440892008-03-24T02:16:00024 March 2008 02:16:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip - Loss of Speed on Mbfp ENS 432852007-04-06T15:11:0006 April 2007 15:11:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Main Generator Transformer Explosion - No Impact on Plant Safety Related Systems ENS 432722007-04-03T08:16:0003 April 2007 08:16:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip While Performing Boiler Feed Pump Maintenance ENS 431992007-02-28T11:35:00028 February 2007 11:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Following Malfunction of Pressure Transmitter ENS 430162006-11-30T19:45:00030 November 2006 19:45:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auxiliary Feedwater Pump Automatic Start ENS 429932006-11-15T19:00:00015 November 2006 19:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip During Electrical Main Generator Troubleshooting ENS 428002006-08-24T15:35:00024 August 2006 15:35:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Main Feedwater Pump Trip During Startup ENS 427972006-08-23T14:35:00023 August 2006 14:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Scram Due to Mismatch of Primary Power and Secondary Load Indications ENS 427202006-07-21T14:30:00021 July 2006 14:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Sparks from Under Main Generator ENS 426872006-07-06T07:52:0006 July 2006 07:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Generator Differential ENS 423782006-03-01T19:35:0001 March 2006 19:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip as a Result of Dropped Control Rods ENS 422202005-12-22T10:50:00022 December 2005 10:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation Signal Due to High Steam Generator Water Level ENS 422172005-12-22T07:08:00022 December 2005 07:08:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Afw Start During Main Feedwater Pump Trip ENS 417622005-06-10T13:24:00010 June 2005 13:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Service Water Leak in Exciter Cabinet ENS 417012005-05-16T14:39:00016 May 2005 14:39:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Afw Actuation During Surveillance Testing ENS 416732005-05-06T14:32:0006 May 2005 14:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Steam Flow/ Feed Flow Mismatch Signal ENS 412272004-11-26T18:22:00026 November 2004 18:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rps Actuation Due to Turbine Trip Caused by Loss of Stator Cooling Water ENS 411872004-11-10T04:39:00010 November 2004 04:39:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of the Emergency Ac Electric Power System ENS 410662004-09-24T15:55:00024 September 2004 15:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip with No Complications Due to Lowering Steam Generator Water Level ENS 410032004-09-01T04:05:0001 September 2004 04:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Oscillating Steam Generator Water Level ENS 400672003-08-14T20:25:00014 August 2003 20:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Loss of Offsite Power Greater than 15 Minutes. ENS 400692003-08-14T20:23:00014 August 2003 20:23:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unusual Event Declared Due to Loss of Offsite Power Greater than 15 Minutes. 2019-03-24T18:45:00 | |