ENS 48475
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ENS Event | |
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06:42 Nov 2, 2012 | |
Title | Manual Reactor Trip Due to High Reactor Coolant Pump Motor Bearing Temperature |
Event Description | At 0142 CDT, Comanche Peak Nuclear Power Plant Unit 1 was manually tripped due to high temperature indications on the 1-04 reactor coolant pump motor radial bearing concurrent with a high / low oil reservoir level alarm. The trip was uncomplicated; all control rods and shutdown rods fully inserted; neither emergency diesel generator started; all safety systems functioned as designed. Both motor driven and the turbine driven auxiliary feed water pumps started as required to restore steam generator levels as a result of the trip. The turbine driven AFW pump was stopped per procedure and returned to auto-start status. Currently, Unit 1 is in Mode 3, no load Tave of 557 degrees F, with temperature being maintained with AFW and steam dumps to the main condenser. All electrical busses are powered from offsite and grid conditions are stable.
The licensee has notified the NRC Resident Inspector. |
Where | |
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Comanche Peak Texas (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-3.2 h-0.133 days <br />-0.019 weeks <br />-0.00438 months <br />) | |
Opened: | Don Cherny 03:30 Nov 2, 2012 |
NRC Officer: | Steve Sandin |
Last Updated: | Nov 2, 2012 |
48475 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
Comanche Peak with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 570332024-03-17T20:15:00017 March 2024 20:15:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Main Feedwater Pump Trip ENS 570242024-03-12T13:16:00012 March 2024 13:16:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 565802023-06-16T23:32:00016 June 2023 23:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to LO-LO Steam Generator Level ENS 560912022-09-06T04:45:0006 September 2022 04:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip ENS 552952021-06-07T20:27:0007 June 2021 20:27:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip on Turbine Trip Due to Fault and Fire in the Main Transformer ENS 544602020-01-01T18:53:0001 January 2020 18:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip and Specified System Actuation ENS 540642019-05-15T02:51:00015 May 2019 02:51:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Voltage Transient Due to Loss of Offsite Switchyard ENS 539062019-03-02T09:17:0002 March 2019 09:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Feedwater Isolation Valve Closure ENS 537672018-12-03T06:00:0003 December 2018 06:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of Blackout Sequencers Due to Loss of One Offsite Power Source ENS 535502018-08-13T05:00:00013 August 2018 05:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Generator Lockout ENS 530912017-11-26T02:25:00026 November 2017 02:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Main Feed Water ENS 529452017-09-02T02:40:0002 September 2017 02:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Two Dropped Rods ENS 528982017-08-11T16:24:00011 August 2017 16:24:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Comanche Peak Automatic Turbine Trip from 10 Percent Power ENS 514442015-10-03T15:00:0003 October 2015 15:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip During Shutdown for a Refueling Outage ENS 497432014-01-18T14:40:00018 January 2014 14:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Turbine Trip ENS 496062013-12-04T19:50:0004 December 2013 19:50:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event - Loss of Startup Power Due to a Cut Cable ENS 494972013-11-02T02:47:0002 November 2013 02:47:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip During Solid State Protection System Testing ENS 485142012-11-17T16:23:00017 November 2012 16:23:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Steam Generator Water Level ENS 484752012-11-02T06:42:0002 November 2012 06:42:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to High Reactor Coolant Pump Motor Bearing Temperature ENS 468632011-05-19T19:07:00019 May 2011 19:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip After a Main Condenser Tube Leak ENS 467482011-04-13T03:15:00013 April 2011 03:15:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Esf Actuation Following Loss of a Safeguard Bus During Edg Testing ENS 458332010-04-12T12:21:00012 April 2010 12:21:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of Blackout Sequencers Due to Loss of One Offsite Power Source ENS 456172010-01-09T16:28:0009 January 2010 16:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip on Sudden Pressure in Output Transformer ENS 440672008-03-16T16:37:00016 March 2008 16:37:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Broken Sensing Line ENS 429452006-10-29T21:20:00029 October 2006 21:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Trip Due to Lowering Steam Generator Level ENS 429372006-10-27T08:08:00027 October 2006 08:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Loss of Both Main Feed Pumps ENS 414322005-02-23T07:53:00023 February 2005 07:53:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auxiliary Feedwater Action Following Momentary Power Interruption ENS 411342004-10-19T10:28:00019 October 2004 10:28:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Normal Power Supply to "2E" Switchgear Resulted in Afw Autostart ENS 404062003-12-22T14:27:00022 December 2003 14:27:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Main Turbine Trip 2024-03-17T20:15:00 | |
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