ENS 48638
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ENS Event | |
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13:03 Dec 29, 2012 | |
Title | Emergency Diesel Generator Auto-Start and Load Upon Trip of Reserve Station Transformer |
Event Description | At 0803 EST on 12/29/2012 With Unit 1 and Unit 2 operating at 100%, the Supply breaker to 'B' Reserve Station Transformer (RSST), 0-EP-BKR-252 tripped on an instantaneous over current of the B-C phases due to a Pelican contacting the lines. This resulted in a lockout of the 'B' RSST and loss of power to the Unit 2 'H' Emergency Bus from its normal off site power supply. #2 Emergency Diesel Generator auto started on under voltage and loaded onto the Unit 2 'H' Emergency Bus. The Operations staff entered abnormal operating procedure 2-AP-10.07, Loss of Unit 2 Power, to recover from the electrical transient. All equipment performed as expected during the event and there were no unexplained occurrences. Maintenance has verified there is no damage to the line, breaker or 'B' RSST and at 1242 EST offsite power was restored to Unit 2 'H' Emergency Bus. At 1501, #2 Emergency Diesel Generator was secured in accordance with Station Operating procedures.
Currently Unit 1 is operating at 100%, 922 MWE. Currently Unit 2 is operating at 100%, 915 MWE. All electrical distribution systems were restored to a normal alignment. No adverse radiological consequences resulted from this event. There were no radiation releases due to this event, nor were there any personnel injuries or contamination events. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) due to the auto start of #2 Emergency Diesel Generator. The licensee has notified the NRC Resident Inspector. |
Where | |
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Surry Virginia (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+2.3 h0.0958 days <br />0.0137 weeks <br />0.00315 months <br />) | |
Opened: | Bret Rickert 15:21 Dec 29, 2012 |
NRC Officer: | Bill Huffman |
Last Updated: | Dec 29, 2012 |
48638 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 537362018-11-12T05:00:00012 November 2018 05:00:00
[Table view]10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuation ENS 536622018-10-11T04:00:00011 October 2018 04:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of Emergency Diesel Generator Due to Transformer Trip ENS 531702018-01-17T14:52:00017 January 2018 14:52:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auto-Start of Emergency Diesel Generator Due to Transformer Fuses Being Disconnected ENS 522922016-10-09T06:54:0009 October 2016 06:54:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Following Main Generator Differential Lockout Turbine Trip ENS 514672015-10-13T22:15:00013 October 2015 22:15:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip After a Turbine Trip ENS 514022015-09-17T00:14:00017 September 2015 00:14:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Start and Loading of the #2 Emergency Diesel Generator ENS 505292014-10-13T11:58:00013 October 2014 11:58:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Spurious Overpower / Delta Temperature Signal ENS 486382012-12-29T13:03:00029 December 2012 13:03:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Auto-Start and Load Upon Trip of Reserve Station Transformer ENS 469052011-05-30T12:08:00030 May 2011 12:08:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuation - Afw Initiation ENS 467612011-04-16T22:55:00016 April 2011 22:55:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Loss of All Offsite Power from Tornado Damage ENS 465842011-02-02T10:33:0002 February 2011 10:33:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Rcs Coolant Flow in One Loop ENS 459862010-06-08T13:48:0008 June 2010 13:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Reactor Trip with Safety Injection Due to Loss of Vital Ac Bus ENS 442212008-05-17T13:04:00017 May 2008 13:04:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Failed Relay Causes Emergency Diesel Generator to Start ENS 441522008-04-21T02:16:00021 April 2008 02:16:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Manual Reactor Trip Due to Main Turbine Vibrations ENS 413832005-02-08T01:23:0008 February 2005 01:23:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip During Startup Due to Indication of Misaligned Rod ENS 407692004-05-22T01:08:00022 May 2004 01:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Generator Leads Failure ENS 401682003-09-18T13:00:00018 September 2003 13:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Expected Severe Weather 2018-11-12T05:00:00 | |
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