05000388/LER-2020-002-01, Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Switch Caused by Lack of Requirements for Acclimation of the Instrument to the Operating Environment
| ML21182A044 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 07/01/2021 |
| From: | Cimorelli K Susquehanna, Talen Energy |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| PLA-7917 LER 2020-002-01 | |
| Download: ML21182A044 (4) | |
| Event date: | |
|---|---|
| Report date: | |
| Reporting criterion: | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability |
| 3882020002R01 - NRC Website | |
text
Kevin Cimorelli Site Vice President Attn: Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555-0001 Susquehanna Nuclear, LLC 769 Salem Boulevard Berwick, PA 18603 Tel. 570.542.3795 Fax 570.542.1504 Kevin.Cimorelli@TalenEnergy.com SUSQUEHANNA STEAM ELECTRIC STATION LICENSEE EVENT REPORT 50-388/2020-002-01 UNIT 2 LICENSE NO. NPF-22 PLA-7917 TALEN~
ENERGY 10 CPR 50.73 Docket No. 50-388 Attached is Licensee Event Report (LER) 50-388/2020-002-01. The LER supplement reports an event involving drifting of Reactor Pressure Steam Dome -Low permissive switches (Microswitch 2). This event was determined to be reportable as a condition prohibited by Technical Specifications in accordance with 10 CPR 50.73(a)(2)(i)(B), a condition that could have prevented fulfillment of a safety function in accordance with 10 CPR 50.73(a)(2)(v)(D),
and a common cause in operability of independent trains or channels in accordance with 10 CPR
- 50. 73(a)(2)(vii).
There were no actual consequences to the health and safety of the public as a result of this event.
This letter contains no new or revised regulatory commitments.
K. Cimorelli Attachment: LER 50-388/2020-002-01 Copy:
NRC Region I Ms. A. Klett, NRC Project Manager Mr. C. Highley, NRC Senior Resident Inspector Mr. M. Shields, PA DEP/BRP July 1, 2021
Abstract
On August 10, 2020, the Unit 2 D Reactor Steam Dome Pressure - Low permissive pressure switch, Microswitch 2, was found outside of the Technical Specification (TS) 3.3.5.1 allowable value. The switch drifted outside of the upper allowable value which is intended to ensure that the reactor dome pressure has fallen to a value below the Core Spray and Residual Heat Removal (RHR)/Low Pressure Coolant Injection (LPCI) maximum design pressures to preclude over-pressurization of the low pressure systems prior to low pressure injection initiation.
Based on the information available, the condition existed for longer than allowed by TS 3.3.5.1, TS 3.5.1, and TS 3.0.3. As such, this is a condition prohibited by TS and is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B). In addition, since the C channel (PIS-B21-2N021C) was surveillance tested just prior to identification of the drift of the D channel (PS-B21-2N021D), redundant channels were inoperable at the same time impacting both Core Spray and LPCI functions; therefore, this is also considered a condition that could have prevented fulfillment of a safety function (10 CFR 50.73(a)(2)(v)(D)) and a common cause inoperability of independent trains or channels (10 CFR 50.73(a)(2)(vii)).
Drifting outside of the TS allowable value on August 10, 2020 is attributed to vendor documents not specifying requirements related to soaking, acclimating, or exposing the instrument to the environment prior to installation and the switch not meeting vendor published repeatability of 0.25% of full scale. Key corrective actions include changing the Susquehanna vendor manual associated with the pressure transmitters to identify the need to acclimate new (or refurbished) switches to in service conditions for at least 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to placing in service and calibrating.
There were no actual consequences to the health and safety of the public as a result of this event.
NRC FORM 366 (08-2020)
CONDITIONS PRIOR TO EVENT
Unit 1 - Mode 1, approximately 100 percent Rated Thermal Power Unit 2 - Mode 1, approximately 100 percent Rated Thermal Power There were no structures, systems, or components that were inoperable at the start of the event that contributed to the event.
EVENT DESCRIPTION
Prior to September 2017, Susquehanna Steam Electric Station (SSES) had been utilizing International Telephone and Telegraph (ITT)-Barton 288A pressure switches in the Reactor Steam Dome Pressure -
Low channels [EIIS System/Component Identifier: JE/PS] that provide the injection permissive for the Core Spray system [EIIS System Identifier: BM] (Technical Specification (TS) 3.3.5.1, Function 1d) and the Residual Heat Removal (RHR)/Low Pressure Coolant Injection system (LPCI) [EIIS System Identifier:
BO] (TS 3.3.5.1, Function 2d). Due to instrument drift concerns, all eight obsolete ITT-Barton 288A pressure switches were replaced with General Electric (GE) recommended Cameron-Barton 288A pressure switches between September 6, 2017 and November 15, 2017. Following replacement, instrument drift continued to be an issue, and additional corrective action was determined necessary to resolve the drift concerns. The additional corrective action included procuring and installing Cameron-Barton 288A instruments that had been modified to remove an over-range condition and the movement assembly/associated linkages that were determined to be affecting instrument drift. The first of these modified instruments was installed and calibrated on July 8, 2020 in the Unit 2 D channel (pressure switch for PS-B21-2N021D).
On August 10, 2020, the new PS-B21-2N021D switch, Microswitch 2, was tested for its first surveillance interval and found to be outside of TS acceptance criteria. The switch drifted 1.2 psig outside of the upper allowable value which is intended to ensure that the reactor dome pressure has fallen to a value below the Core Spray and RHR/LPCI maximum design pressures to preclude over-pressurization of the low pressure systems prior to low pressure injection initiation.
Based on the information available, the condition existed for longer than allowed by TS 3.3.5.1, Emergency Core Cooling System (ECCS) Instrumentation, TS 3.5.1, ECCS-Operating, and TS 3.0.3.
As such, this is a condition prohibited by TS and is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B). In addition, since the C channel (PIS-B21-2N021C) was surveillance tested just prior to identification of the drift of the D channel (PS-B21-2N021D), redundant channels were inoperable at the same time impacting both Core Spray and LPCI functions; therefore, this is also considered a condition that could have prevented fulfillment of a safety function (10 CFR 50.73(a)(2)(v)(D)) and a common cause inoperability of independent trains or channels (10 CFR 50.73(a)(2)(vii)).
CAUSE OF EVENT
Drifting outside of the TS allowable value on August 10, 2020 is attributed to vendor documents not specifying requirements related to soaking, acclimating, or exposing the instrument to the environment prior to installation and the switch not meeting vendor published repeatability of 0.25% of full scale.
ANALYSIS/SAFETY SIGNIFICANCE
All components in the LPCI and Core Spray would have been able to withstand a pressure of 456.2 psig (434.2 psig with water head removed which allows direct comparison to TS value) which was the maximum recorded pressure for instrument PS-B21-2N021D. Therefore, Core Spray and RHR would have been able to perform its safety function and the condition described herein did not result in a safety system functional failure. Accordingly, this event will not be counted as a safety system functional failure in the Reactor Oversight Process Performance Indicators. There were no actual consequences to the health and safety of the public as a result of this event.
CORRECTIVE ACTIONS
The switch was acclimated and returned to within the TS allowable values. Key corrective actions include the following:
- 1. Changed the Susquehanna vendor manual associated with the pressure transmitters to identify that acclimation of new (or refurbished) switches to in service conditions for at least 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to placing in service and calibrating is required.
COMPONENT FAILURE INFORMATION
The switches installed in the application affected by this condition are Cameron-Barton 288A pressure indicating switches manufactured by Cameron. The switch that drifted in the event described in this LER had been modified to remove an over-range condition and the movement assembly/associated linkages; with the indication function removed, this switch was a pressure switch.
PREVIOUS OCCURRENCES
As indicated by the previous occurrences listed below, the condition of drifting pressure indicating switches is a known issue at SSES. Previously reported Corrective Actions are in progress; additional corrective actions will be dictated by the Susquehanna Corrective Action Program.
LER 50-387(388)/2018-005-01, Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Switches, dated December 16, 2019.
LER 50-388/2017-010-01, Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Switches, dated December 16, 2019.
LER 50-388(387)/2015-001-01, Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Steam Dome-Low Switches, dated February 10, 2016.