ML20072E829
| ML20072E829 | |
| Person / Time | |
|---|---|
| Site: | Callaway |
| Issue date: | 07/31/1994 |
| From: | Blosser J, Mcinvale J UNION ELECTRIC CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| ULNRC-3055, NUDOCS 9408230108 | |
| Download: ML20072E829 (6) | |
Text
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, favn M > ,,,n E525 i August 8,1994 Uvio,v ILCTitlC a
Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 ULNRC-3055
Dear Sir:
DOCKET NUMBER 50-483 CALLAWAY PLANT UNIT I FACILITY OPERATING LICENSE NPF-30 MONTiiLY OPERATING REPORT JULY.1994 The enclosed Monthly Operating Report for July,1994 is submitted pursuant to section 6.9. l.8 of the Callaway Unit i Technical Specifications.
, . D. Blosser Manager, Callaway Plant JDB/DEY/J 1/fAM/ .Werd Enclosure cc: Distribution attached 220C03 9408230108 940731 PDR ADOCK 05000483 ' I 5
R PDR g
cc distribution for ULNRC-30$$
with enSlqELrgs Alr. M. J. Farber, Chief Reactor Projects Section 3C U.S. Nuclear Regulatory Commission Region til 801 Warrenville Road Lisle, IL 60532-4351 Mr. L. R. Wharton (2 copics)
OfTice of NucIcar Reactor Regulation U.S. Nuclear Regulatory Commission 1 White Flint, North, Mail Stop 13E21 1155 Rockville, MD 20852 NRC Resident inspector Manager, Electric Department Missouri Public Service Commission P.O. Box 360 JefTerson City, MO 65102 l
l j
I DOCKET NO. 50-483 UNIT NAME CALLAWAY UNIT I DATE 08-08-94 COMPLETED BY J. B. McInvale TELEPilONE 314/676-8247 PART A OPERATIONS
SUMMARY
The plant operated at approximately 100% power for the month of July with the following exceptions:
Power was reduced to 93% to repair a low pressure heater tube leak on 7-7 94.
Power was reduced to approximately 70% for two days beginning on 7-8-94 for planned repair of a feedwater pump check valve.
Power was reduced to 91% on 7-19 94 for repair of a circulating water pump. The plant was returned to powcr on 7-20-94.
Power was reduced to 97% briefly for instrument calibrations on 7-22-94.
PART B PORV AND SAFETY VALVE
SUMMARY
None l
i Page 1 of 4
l PART C AVERAGE DAILY UNIT POWER LEVEL DOCKET NO 50-483 UNIT Callaway Unit i DATE 08-08-94 COMPLETED BY J. B. McInvale TELEP110NE 314/676-8247 MOVTH: JULY 1994 AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY (MWe-Net) DAY (MWe-Net) i i134 17 1140 I
j 2 1139 18 II34 3 1140 19 1102 4 1106 20 1012 5 1126 21 1126 6 1127 22 1126 7 1079 23 II32 8 939 24 1122 9 763 25 1119 10 798 26 1143 11 1123 27 1147 12 l139 28 II49 13 1135 29 1147 14 1140 30 1149 15 1142 31 1144 16- 1140 i l
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PART D OPERATING DATA REPORT DOCKET NO. 50-483 UNIT NAME CALLAWAY UNIT 1 DATE 08-08-94 COMPLETED BY J. B. McInvalc TELEPHONE 314/676-8247 OPERATING STNIUS (YTD) (CUM)
- 1. REPORTING PERIOD. JULY 1994 GROSS llOURS IN REPORTING PERIOD: 744 5087 84,252.5 2 CURRENTLY AtrrilORIZED POWER LEVEL (MWi). 3565 MAN. DEPEND. CAPACITY (MWe-Net): 1115 DESIGN ELECTRICAL RATING (MWeNet): 1171
- 3. POWER LEVEL TO WillCil RESTRICTED (IF ANY)(MWe-Net):
- 4. REASONS FOR RESTRICTION (IF ANY):
Jills MONI].1 YR TO DATE CUMULATIVE
- 5. NUMilER OF IlOURS REACTOR WAS CRITICAL. 744 5087 74,033 7
- 6. REACTOR RESER VE SIIlfrDOWN IIOURS... 0 0 0
- 7. IlOURS GENERATOR ON I INE.. 744 5053.7 72,608.8
- 8. UNIT RESERVE SiltrrDOWN llOURS... 0 0 0
- 9. GROSS TilERMAL ENEROY GENEP ATED(MWil).. 2,549,178 17,690.536 244,555,624
- 10. GROSS ELECTRICAL ENERGY GENERATED (MWil)... 857,827 6,047,611 83,4I8,734
- 11. NET ELECTRICAL ENERGY GENERAT ED (MWil) 817,462 5,773,581 79,337,632 12 REACFOR SERVICE FACTOR I00.0 100.0 87.9 13 REACTOR AVAILAlllLTTY FACTOR .. 100.0 100.0 87.9
- 14. UNIT SERVICE FACTOR 100.0 99.3 86.2
- 15. UNIT AVAll All!LTTY FACTOR.. 100.0 99.3 86.2
- 16. LNIT CAPACITY FACTOR (Using MDC),... 98.5 101.8 84 5
- 17. UNIT CAPACITY FACTOR (Using Design MWe)... 93.8 - 96.9 80.4 18 UNIT I ORCED OUTAGE RATE . 0.0 0.0 236 j
- 19. SilUTDOWNS SCIIEDULED OVER NEXT 6 MONTilS (TYPE, DATE, AND DURATION OF EACll); l l
- 20. IF Siltrr DOWN AT END OF REPORTING PERIOD, ESTIMATE DATE OF STARTUP: N'A Page 3 of 4
d PART E
- UNTT Sl!UTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-483 UNIT NAME CALIAWAY UNIT I DATE 084J8-94 COMPLETED BY I B. McInvale TELEPIIONE 314'676-8247 REPORT MONTII: WLY 1994 METIIOD OF TYPE SIIUTTING DO%W F: FORCED DURATION TIIE REACTOR OR
>_Q DATE S: SCIIEDULED . (IIOURS) REASON REDUCING POWER CORRECTIVE / ACTIONS COMMENTS 2 7-8-94 S 53 4 A I A managemera decision u as made to reduce power for repair of a check valve.
SUMifARY Power was reduced to 70% so that one feedwater pump could be sin:tdown for repair of a leak on its discharge check vahe.
REASON METIIOD A EQUIPMENT FAILURE (EXPLAIN) I: MANUAL B: MAINT. OR TEST 2: MANUALSCRAM C: REFUELING 3: ALTOMATIC SCRAM D: REGUIATORY RESTRICTION 4: OTIIER(EXPLSIN)
E: OPERATORTRAINING AND LICENSE EXAMINATION F: ADMINISTRATION G: OPERATIONAL ERROR (EXPLAIN)
II: OTilER(EXPLALN)
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