ENS 56059
ENS Event | |
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04:42 Aug 20, 2022 | |
Title | Technical Specification Required Shutdown |
Event Description | The following information was provided by the licensee via fax or email:
At 2342 CDT on August 19, 2022, with Grand Gulf Nuclear Station in Mode 1 and at 40 percent power, the station initiated a normal shutdown to comply with its Technical Specifications (TS). The station entered Mode 3 at 0000 CDT August 20, 2022 to comply with (LCO) 3.5.1 Condition G Action G.1 due to the condition reported to NRC previously (EN 56058). This event is being reported under 10 CFR 50.72(b)(2)(i) as a shutdown required by the plant's technical specifications. The NRC Senior Resident Inspector was notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The plant is now in a 36-hour LCO to be in Mode 4 due to Low Low Set Valves inoperability per TS 3.6.1.6.
Grand Gulf Nuclear Station (GGNS) is performing this notification to retract event EN 56059 that was reported on August 20, 2022. Previously, GGNS notified the NRC that it had initiated a shutdown required by Technical Specifications to comply with Limiting Condition of Operation (LCO) 3.5.1 Condition G.1 due to the inoperability of four Automatic Depressurization System (ADS) valves. Following the shutdown, GGNS completed walkdowns and determined that the condition affected only one ADS valve. As a result, the shutdown to satisfy the required actions of TS LCO 3.5.1 Condition G.1 was not required. The NRC Resident Inspector has been notified of the retraction. R4DO (Kellar) was notified |
Where | |
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Grand Gulf Mississippi (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+-2.52 h-0.105 days <br />-0.015 weeks <br />-0.00345 months <br />) | |
Opened: | Paul Lyne 02:11 Aug 20, 2022 |
NRC Officer: | Bethany Cecere |
Last Updated: | Oct 14, 2022 |
56059 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (40 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 560592022-08-20T04:42:00020 August 2022 04:42:00
[Table view]10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown ENS 529362017-08-29T17:00:00029 August 2017 17:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown ENS 522252016-09-08T08:00:0008 September 2016 08:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown Due to Loss of Residual Heat Removal Pump 2022-08-20T04:42:00 | |