ML20202B092

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Forwards Response to Notice of Violation from Insp Rept 50-354/86-20.Corrective Actions:Filtration,Recirculation & Ventilation Sys Controls Placed in Automatic Mode & Shift Supervisors Instructed to Keep Controls on Automatic
ML20202B092
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 06/19/1986
From: Corbin McNeil
Public Service Enterprise Group
To: Murley T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
NUDOCS 8607100198
Download: ML20202B092 (3)


Text

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Electric and Gas '

company. .

.Crrbin A. McNeill,Jr. Pubhc Service Electric and Gas Company P.O. Bdx 236, HancockeBridge, NJ 08038 609 339-4800

. Vice President *

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J'u ne. 19 , 1986 .

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U. S. Nucle'a'r Regulatory Commission ,,.

' :" Region I- ,

631 Park Avenue '

. King of' Prussia, PK 19406 ', -

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Attention:* Dr. Thomas E. Murley, Administrator -

Office of Inspection'and Enforcement -

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. Gentlemen:

'NRC INSPECTION REPORT #86-20

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DOCKET'NO. 50-354 - ' '

  • HOPE CREEK GENERATING STATION

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-Public Service Electric'and Gas Company (PSE&G) is in receipt, of your letter' dated May 20, 1986, which transmitted a Notice of Violation concernin,g two .(2) failures to comply with ,

Technical Specification requirements. , ,

Pursuant *to the provisions 6f 10CFR2.201,'our. response to the -

Noticee of Violation is pro.vided in Attachment 1.

e Sincerely, .

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Attachment ,

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C Office of Inspection and Enforcement

. Division of Reactor Construction Inspection

. Washingtod, D. C. 20555' .

NRC Resident Inspector ' *

. P. O. Box 241 .

l Hancocks Bridge, NJ 08038 .

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l= B607100198 860619 ADOCK 05000354' i PDR l; G g PDR' i gs -

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. ATTACHMENT 1 .s

.g 10 CFR 2.201 INFORMATION.

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PUBLIC SERVICE ELECTRIC AND GAS' *

- HOPE CREEK GENERATING STATION RESPONSE TO NOTICE- OF VIOLATION s ,.

A. Your 1.etter dated May 20, 1986 identified one violation-of -

o T'echnical' Spec,ification 3.6 5 3 which rbquires that fivg3 .

Filt, ration, Recirculation and Ventilation System (FRVS)

  • recirculation units and two ventilation units shall.be 6pera-

, ble during core;al'terations. The FRVS' controls were'found in the locked out position, thereby disabling;all automatic

' start functions. ,,

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  • 1. PUBLIC SERVIC'E ELECTRIC AND GAS DOES NOT DISPUTE THE.' . .

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, VIOLATION.

2. THE ROOT CAUSE OF.THE VIOLATION WAS PERSONNEL ERRORON THE PART OF THE* CONTROL ROOM OPERATOR IN FAILING TO -

. t REALIZE THAT THE'TRVS'WAS TECHNICALLY INOPERABLE *WITH*

  • ', THE CONTROLS LOCKED'OUT AND IN FAILING TO RE' STORE THE ,

. FRVS (*0NTROLS TO THE. AUTOMATIC MODE TO SUPPORT CORE .

ALTERATION A.CTIVITIES. ,

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3. IMMED ATE CORRECTIVE, ACTIONS: g ,

. . C a) The FRVS recirculation anci ventilation corntrols wei e ,

- *immediately placed'in the automat,ic mode.

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b) dn April 16', 1986, all shift supervisors w.ere

. advised of this v.iolation and instructed to keep

, the.FRVS contro1s on automatic. *

4. LONG' TERM' CORRECTIVE AC' CIONS: * .

-a) Prior *.to fuel loading, the FRVS controls"had been , .

locked out as an acceptable m,bthod of protecting ,

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the FRVS charcoal beds from vapors, generated by ,

,

  • painting activities in the Reactor Building. In the' future, this will be accomplished by maintaining. *-

the Reactor Building Ventilatioh System (REVS) in

, , the.hormal or refuel modes. .

, b). To raise the Control hoom Operator's awareness of FRVS operability, the statiuq of *each FRVS recircu '

~ 1ation and ventilatiory unit has. been added to the

. Control' Room console check'llst 'used at shift turnover '

( OP-AP . Z E-l&7Q )'.

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'c-) On Jurie 16, 1986, a copy of this response and the ,

applicable pages from Inspection Report #86-20 wer,e put in the Eope Creek Operations Required, Reading Book to be read by all licensed operators. ,

5. FULL COMPLIANCE WAS ACH.IEVED ON JUNE 16, 1986. .

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. . . e B. ' Failure to veri ~fy'that the Standby Liquid Contr'ol (SBLC).

System is operable in mode 5. when.any' coritrol rod is moved.

1. PUBLIC SERVICE ELECTRIC AND GAS' DdES NOT DISPUTE THE
VIOLATION. . ,,

, . - .s THE ROOT .CAUSE,OF THE VIOLATION WAS A. PROCEDURAI9 2s

, IMADEQUACY IN.THAT.OP-DL.ZZ-026(Q)'DID NOT, PROVIDE SUFFICIENT INSTRUCTIONS.- .

3. -I'MMEDIATE CORREC.TIVE ACTIONS: . .

. On April 24, 1986, all shift supervisors wefe instructed -  : .

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th'at for a given plant condition, all required ' surveillance

'. activities specified in the. log shall be performed even -

if the, surveilletnc*e activity is only required for a

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special evolution within the plant condition. ,,

4. 'LONG k'ERM CORRECTIVE . ACTIONSt e , , p.

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a) On May 8, 1986, the Operat' ions Department s'urveillance log, OP-DL.ZZ'026(Q) was revised to reflecA.t,he ,

ihs'trdctions described in. item 3,' above.

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b) On Jyne 16, 1986, a copyrof this response and the '

applicable pag'es fr'om Inspection Report #.86-20 were

'put i,n the Hope Cr'eek ' Operations . Required Reading - '

Book to be ' read by all 1,icensed opergtors.

5. FULL COMPLIANCE WAS ACHIEVED ON JONE 16, 1986.

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