05000260/LER-1981-054, Updated LER 81-054/03X-1:on 811010,hydrogen Analyzer B Sample Return Pump Found Inoperable.Caused by Tripped Motor Overloads Due to Motor Current Being 10-15% High Due to High Supply Voltage

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Updated LER 81-054/03X-1:on 811010,hydrogen Analyzer B Sample Return Pump Found Inoperable.Caused by Tripped Motor Overloads Due to Motor Current Being 10-15% High Due to High Supply Voltage
ML20054J881
Person / Time
Site:  Tennessee Valley Authority icon.png
Issue date: 06/17/1982
From: Carter S
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20054J880 List:
References
LER-81-054-03X, LER-81-54-3X, NUDOCS 8206300146
Download: ML20054J881 (1)


LER-2081-054, Updated LER 81-054/03X-1:on 811010,hydrogen Analyzer B Sample Return Pump Found Inoperable.Caused by Tripped Motor Overloads Due to Motor Current Being 10-15% High Due to High Supply Voltage
Event date:
Report date:
2602081054R00 - NRC Website

text

P"C F Or.*,1366 U. S. NUCLEAR PEGULATORY COMMISSIOrd

  • UPDATE REPORT.. , . LICENSEE EVENT REPORT PREVIOUS REPORT DATE 11/6/81

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/ 8 60 61 DOCK ET NUMBER ha 69 EVENT DATE e4 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 1012l l During normal operation, it was discovered that hydrogen analyzer "B" sample return ]

[Oi3l l pump was inoperable. (T.S. 3.7.H.2) There was no danger to the health or safety of l 1 O I 4 l l the public. Redundant systems were available and operable. l 10151 l l lo is I l I 10171 l l 10181 l I 7 8 9 80 SYSTEN1 CAUSE CAUSE COYP. VALVE CODE CODE SU8 CODE COMPONENT CODE SUSCODE SUBCODE lO191 is la l@ [E_J@ l A l@ l R l E l L l A l Y l X l@ lX ]@ [Z_j @

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li i2l l Supply transformer taps are set high to maintain required I&C bus voltage l I i I 3 I I (NRC commitment). Evaluation of shutdown board and unit station service transformer l lilaI l tan settines expected hv 7/1/82. I I 6 3 80 STA S  % POWER OTHER STATUS ISCO RY DISCOVERY DESCRIPTION l l1 15i W h l0!9l9l@l NA l lAl@l Operator observed l ACTIVITY CO TENT l RELE ASEO OF RELE ASE AMOUNT O7 ACTivtTY j LOCATION OF RELEASE j jil6j d @ W@l NA l l NA l PERSONNEL EXPOS ES l NUU8ER TY9E DE SCRIPTION l

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a 1 to b6 69 80 5 l NAME OF PREPARER Stan Carter PHONE A(205) 729-0798 E I