ENS 53662
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ENS Event | |
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04:00 Oct 11, 2018 | |
Title | Actuation of Emergency Diesel Generator Due to Transformer Trip |
Event Description | On 10/11/18 at 2304, with both Surry Units at 100% power, the 'A' Reserve Station Service Transformer (RSST) tripped on a pilot wire lockout. This resulted in electrical isolation of the 'A' RSST, the 'D' Transfer Bus and the Unit 1 'J' Emergency Bus. The #3 Emergency Diesel Generator (EDG) started and loaded on the Emergency Bus, as designed. Operations entered the appropriate Abnormal Procedures and stabilized the unit. All equipment operated as expected during the event.
A report of a flash at the 'A' RSST was received (at approximately the time of the initiating event) but there were no reports of visible damage, smoke or fire from the RSST or any associated breakers on subsequent investigation. The #3 EDG is running with normal parameters. There was heavy wind/rain in the area associated with Tropical Storm Michael. All other electrical distribution systems are in a normal alignment. The organization is staffing to evaluate the lockout and required actions for recovery. No radiological consequences resulted from this event. This event is being reported IAW [in accordance with] 10 CFR 50.52(b)(3)(iv)(A) due to the actuation of the #3 EDG. The NRC Resident [Inspector] was notified |
Where | |
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Surry Virginia (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+21.23 h0.885 days <br />0.126 weeks <br />0.0291 months <br />) | |
Opened: | Jeremy Riddick 01:14 Oct 12, 2018 |
NRC Officer: | Ossy Font |
Last Updated: | Oct 12, 2018 |
53662 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 537362018-11-12T05:00:00012 November 2018 05:00:00
[Table view]10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuation ENS 536622018-10-11T04:00:00011 October 2018 04:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of Emergency Diesel Generator Due to Transformer Trip ENS 531702018-01-17T14:52:00017 January 2018 14:52:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auto-Start of Emergency Diesel Generator Due to Transformer Fuses Being Disconnected ENS 522922016-10-09T06:54:0009 October 2016 06:54:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Following Main Generator Differential Lockout Turbine Trip ENS 514672015-10-13T22:15:00013 October 2015 22:15:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip After a Turbine Trip ENS 514022015-09-17T00:14:00017 September 2015 00:14:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Start and Loading of the #2 Emergency Diesel Generator ENS 505292014-10-13T11:58:00013 October 2014 11:58:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Spurious Overpower / Delta Temperature Signal ENS 486382012-12-29T13:03:00029 December 2012 13:03:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Auto-Start and Load Upon Trip of Reserve Station Transformer ENS 469052011-05-30T12:08:00030 May 2011 12:08:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuation - Afw Initiation ENS 467612011-04-16T22:55:00016 April 2011 22:55:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Loss of All Offsite Power from Tornado Damage ENS 465842011-02-02T10:33:0002 February 2011 10:33:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Rcs Coolant Flow in One Loop ENS 459862010-06-08T13:48:0008 June 2010 13:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Reactor Trip with Safety Injection Due to Loss of Vital Ac Bus ENS 442212008-05-17T13:04:00017 May 2008 13:04:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Failed Relay Causes Emergency Diesel Generator to Start ENS 441522008-04-21T02:16:00021 April 2008 02:16:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Manual Reactor Trip Due to Main Turbine Vibrations ENS 413832005-02-08T01:23:0008 February 2005 01:23:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip During Startup Due to Indication of Misaligned Rod ENS 407692004-05-22T01:08:00022 May 2004 01:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Generator Leads Failure ENS 401682003-09-18T13:00:00018 September 2003 13:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Expected Severe Weather 2018-11-12T05:00:00 | |
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