ML20004D623

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LER 81-003/03L-0:on 810217,engineered Safety Features Actuation Sys Channel 2D 12 Steam Generator Pressure Isolator Found Out of Spec.Caused by Transmation Isolator w/non-liner Output.Isolator Replaced
ML20004D623
Person / Time
Site: Calvert Cliffs 
Issue date: 03/19/1981
From: Rizzo P, Wenderlich R
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20004D617 List:
References
LER-81-003-03L-01, LER-81-3-3L-1, NUDOCS 8106090591
Download: ML20004D623 (2)


Text

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REPORT DATE 7 8 60 61 DOCKET NUMBER ,

EVENT'oESCAIPTioN AND PROB ABLE CONSEQUENCES 01o 10121 1 Ouring power' operation at 1300, discovered that ESFAS Cnannel Z0 No.12 l In tai l Steam Generator pressure 1-E/E-1023A isolator was out of specification  ;

l O 1. ] l in the non-conservative direction (T.S. 3.3.2.1). The E/E module was re- l l O i 31 ; placed, and Channel Z0 No.12 Steam Generator pressure was back in ser- l [

.IO is 1 l vice at 1630. All redundant channels remained operable during this time  ;

t lOl2ll period. This event had no impact on the public health or safety. LERs l l 0 l8 ] l ~

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41 42 43 44 47 CAUSE CESCRIPTION AND CORAECTIVE ACTICNS ,

lil0ll Transmation Isolator (2301T) 1-E/E-1023A was found to have a non-linear- 1 i s ii i l' outout. It was replaced with a spare. The instrument would have allowed I i ,121 I one of four Steam Generator Low Pressure Block bistables to reset at I gii3 l less tnan 685 osia reouired by Technical Soecifications. Facility Chance 1 i,isi 1 30-25 will modify these isolators to increase their .eliability. I

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LER NO. 81-03/3L -

DOCKET NO. 50-317 ,

LICENSE NO. OPR-33 EV".NT DATE 02-17-81 REPORT DATE 03-19-81 '

ATTACHMENT r

CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (CONT'D)  ;

Transmation Isolator (Model 230lT)1-E/E-1023A was found to have a non- l linear output af ter plant operators noted a deviation among indications of [

Steam Generator #12 Pressure. .

i As found readings showed its effect on the Channel ZD No.12 Steam Generator Low Pressure Trip bistable was negligible. Hewever, in the  ;

range of the No.12 Steam Generator Low Pressure Block bistable, its i

output was high such that the Channel ZD Block bistable would have reset -

approximately 13 psia below its limit.

j The blocking function is enabled by a 3 of 4 channel trip matrix and is  !

removed automatically'when 2 of 4 channels are reset. Technical Specifications require the automa+ic removal of the Block (or Bypass) [

function at or above 685 psia Steam Generator Pressure, A facility change (No. 80-25) will be performed on this and similar instruments to increase their reliability. The change replaces capacitors with high failure rates with more durable components.

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