ML20006E572

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Provides Written Notification That Nine Commitments Re Generic Ltr 88-14 Complete,Per Util 890223 Ltr
ML20006E572
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 02/14/1990
From: Michael Ray
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
GL-88-14, NUDOCS 9002260037
Download: ML20006E572 (4)


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TENNESSEE VALLEY AUTHORITY.

, , CH ATTANOOGA. TENNESSEE 37401 I

SN 157B Lookout Place FEB 141990 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Gentlemen:

In the Matter of .

) Docket Nos. 50-327.

Tennessee Valley Authortty

) 50-328

, SEQUOYAfi NUCLEAR PLANT (SQN) - COMPLETION OF COMMITMENTS FOR GENERIC LETTER 88 INSTRUMENT AIR SUPPLY SYSTEM PROBLEMS AFFECTING SAFETY-RELATED EQUIPMENT-

Reference:

Letter from TVA to NRC dated Februa.y 23, 1989, " Browns Ferry Nuclear Plant (BFN), Sequoyah Nuclear Plant (SQN), and Watts Bar.

Nuclear Plant (WBN) - Response to Generic. Letter 88 '

Instrument Air Supply System Problems Affecting Safety-Related Equipment" This. letter provides written notification that all actions associated with the nine SQN commitments contained in the reference letter are complete, Enclosed' _.

is a listing of the commitments made for SQN in Enclosure 4 of the referenced.

' letter and the-~ completion date for each.

Please direct questions concerning this issue to D. V.-Goodin at -

(615) 843-7734'. ,

Very truly yours, TENNESSEE VALLEY AUTHORITY h

Managei,Nuclea%/

H r Licensing 4 i and Regulatory Affairs

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Enclosure ,

cc: See.Page 2

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I-9gRo2260037 900214 g ADOCK0500g7

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An Equal opportunity Employer k

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  • LU.S. Nuclear Regulatory Commission .FEB 14 B90 L^ , -+

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! ", .MS. S. C.-Black, Assistant Director  :

L' for Projects l L' LTVA Projects Division _ l o U.S. Nuclear Regulatory Commission. ,

, One White Flint, North L

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,' l _11555 Rockville Pike -

[ Rockville, Maryland 20852 l

Mr. B. A. Wilson, Assistant Director for Inspection Programs;  ;

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TVA Projectt Division

! U.S. Nuclear Regulatory Commission ,

F Region II. -

F 101 Marietta. Street, NW, Suite 2900  ;

Atlanta, Georgia 30323 lNRC Resident Inspector

'n !Sequoyah Nuclear Plant.

2600 Igou. ferry Road r Soddy Daisy, Tennessee 37379 a ,

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f ENCLOSURE  ;

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M- GENERIC LETTER 88-14. -.

SUMMARY

LIST Of COMMITMENTS

,e SQN. 1

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1. "PMT-84,.which is still open, will be revised to require air quality '

l verification for. lubricant content at the rotary screw compressor's discharge downstream of the 2-stage pipeline filter. The scoping document for PMT 84 will be revised by May 4, 1989, and PMT-84 will be ,

performed by July 31, 1989."

h  ; Completed April 24. 1989,' and July 28, 1989, respectivaly, e

'*  : 2. . " Plant procedures will.be revised to require routine. set point l

, verification of moisture elements in the ACA and SCSA systems by l h July 31, 1989." j

/ e Completed August 28, 1989.

Y :3. " Routine air quality testing will be impleinented by August 28,:1989." '

Completed September 12, 1989.  !

4. "The need for local filters for 28 users will be evaluated by June 1, 1989."'

' Completed May 25, 1989.

5. "New procedures will be created or_ existing procedures will be revised by May,15, 1989, to. ensure adequate PM for syster drain traps."

Completed April 26, 1989.

6. "NE will perform a review of-A01-10 to ensure the. air systems events are

" adequately covered and responded to by Operations ~from an engineering standpoint. Any identified deficiencies will be transmitted to Operations to eliminate possible interface problem between NE and-Operations. This= review will be complete by September 29, 1989."

~ Completed September 27, 1989.

7. "As part of TVA's. review of SOER 88-01, a review is being conducted to a: ' identify improvements required to the SCSA and ACA pneumatic accumulators

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-and check valves and their maintenance testing procedures. Thh review p,1 ,

is being done to ensure that (1) accumulator check valves will' properly rescat upon both a gradual and rapid loss of upstream pressure, (2) check

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g' valves are properly designed for air service, (3) low accumulator tank 4

. . pressure _is properly annunciated, and (4) accumulator tank design 1s-properly documented by calculations. This review will be complete by April;3, 1989."

L -Completed Apr11 3, 1989.

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q ; mem of :g,, "An evalu'atio.will?be n performediby' September 15,21989, to determinelif 0: .,;

-;the failure ~ position ofc18 unmarked users:should;beishown.:and drawings

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@QF ,

A will:be/ revised *accordingly."  ;

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Completed September 30, 1989. >

,t-U,y , 9.1 '.An

' evaluation ~cf the proper failure po'sition:of 10.' air-operated '

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, ventilation dampers will be completed by May 4 1989."'

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Comple'te'd'Aprili21, 1989. .

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