ML19261F292
| ML19261F292 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 05/01/1974 |
| From: | Arnold R METROPOLITAN EDISON CO. |
| To: | |
| References | |
| NUDOCS 7910250745 | |
| Download: ML19261F292 (2) | |
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FRC' : . DATE OF ECC DA~E REC'D LTR I li;;;0 12T 012 Metropolitan Edison Company Reading, Pa. 19603 5-1-74 5-6-74 X R. C. Arnold TO: CRIG CC CTHER SE!.T AEC ?"R N _
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XXX 1 50-289 DESCRIlTION: E';CLCSURE.S :
Ltr reporting abnormal occurrence A0-74-2 on 4-22-74, regarding setpoint error........ ,
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Gcatlemen:
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Operating License DPR-50 Docket No. 50-289 V'M CM'd .
Abnor=al Occurrence No. A0-Th-2 In accordance with Technical Specificaticns for the Three Mile Island Nuclear Statica Unit 1, Secticn 6.7 2.a.h. , we are reporting the folleving incident as an abnormal occurrence ( AO-Th-2) as defined by Section 1.8.a.
At 1100 on April 22,197L, during initial fuel loading, the pressure svitches for the High Peacter Building Pressure reactor trip were decreased by Instrument Technicians frc= L.0 psig to a =cre conservative setting of 3 75 psig to account fcr pctential set point errors. The Test Ccordi-nator, in reviewing the test results, discovered that the as-found setting for Channel A was 4.1 psig and for Channel D was h.15 psig, which ecnsti-tutes safety system settings less conservative than the li=it of h.0 psig as defined by Section 2 3.1 and Table 2 3-1 Ite 8 of Technical Specifica-tiens.
Based upon a review by on-site engineering persennel of the Technical Manualc- for the associated equipment, the pctential set pch errer was concluded to be +C.135 psig. The Plant operatiens Review
_ -4ttee (FCRC) met prc=ptly after the incident, concurred with the analysis of the set point error, and recc==?nded to the Plant Superintendent that the new set point of 3 75 psig was adequate to prevent recurrence. The Plant Superintendent has ccccurred in this finding.
Sincerely,
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'"iOLD Vice President-Generaticn -
RCA:DNG:sh ec: Directcrate of Regulatory Cperations, Regien 1 U. S. Atc=ic Energy Cc==issicn 631 Park Avenue King of Prussia, Pennsylvania 4()f2 19hc6