ML19253A096

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Notification of Violation of Tech Spec 3.4.1 on 790628. During Surveillance Testing on Reactor Protection Sys Channel 4,instrument & Control Technician Shorted Several Terminals W/Allegator Clip
ML19253A096
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 06/29/1979
From: Murray T
TOLEDO EDISON CO.
To:
References
NUDOCS 7907170005
Download: ML19253A096 (1)


Text

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June 29, 1979 OIE Region III USNRC 799 Roosevelt Road Glen Ellyn, Illinois 60137 ATTENTION: Tom Tambling, Inspector - Operations Branch

SUBJECT:

Violation of Technical Specification 3.4.1 Davis-Besse Unit 1 - Mode 5, Power (MWT) = 0, and Load (MWE) = 0 At 0157 hours0.00182 days <br />0.0436 hours <br />2.595899e-4 weeks <br />5.97385e-5 months <br /> on June 28, 1979, while conducting surveillance testing on the i Reactor Protection System (RPS) Channel 4, the Instrument and Control Technician shorted several terminals with an allegator clip. The 120 Volt AC power supply .

to RPS Channel 4 Y4 was 1 cst causing a loss of power to the Safety Features Actuation System (SFAS) Channel 4. The SEAS Channel 4 Bistables tripped as j designed upon a loss of pnwer. The reip of one SFAS channel does not actuate any SFAS incide... le.1 bui -.. e Lt e v! 371.3 C'.~nael 4 does actuate the Bistable

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  • which closed the Decay Heat (DH) Normal Cooldown Isolation Valve DH 11.

The closure of DH 11 isolated the DH System and since there were no Reactor Coolant Pumps in operation, placed the unit in violation of Technical Specifi-cation 3.4.1. The Decay Heat Pump was manually shutdown before all DH flow was lost to protect the pump.

By 0215 hours0.00249 days <br />0.0597 hours <br />3.554894e-4 weeks <br />8.18075e-5 months <br />, Y4 was re-ancrgized, DH 11 was re-opened, DH Pump 1-2 was re-started, and a Decay Heat Flowrate of greater than 2800 GPM was established.

Tom Tambling, Region III NRC was notified of the violation at 1010 hours0.0117 days <br />0.281 hours <br />0.00167 weeks <br />3.84305e-4 months <br /> on June 29, 1979.

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Terry Murray Station Superintendent Davis-Besse Nuclear Power Station Unit #1 L 0'

TDM/SNB/cjb Io 2091 139 THE TCLECO EDISCN COMPANY EDISCN PLAZA 3CO MACISCN AVENUE TCLECO. CH:0 43552 (N E 7 9 0717 0(0(De$I~

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