ML19253B890
| ML19253B890 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 06/08/1976 |
| From: | Lawyer L METROPOLITAN EDISON CO. |
| To: | |
| Shared Package | |
| ML19253B889 | List: |
| References | |
| NUDOCS 7910310628 | |
| Download: ML19253B890 (3) | |
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UNIT Three aila T c 11. n d DATE June 8, 1076 L. L. Lawyer COMPLETED BY TEL. No. 215-929-3601 DAILY PLANT PCWER OUTPUT MONTH MAY DAY AVERAGE DAILY fGe-net DAY AVERAGE DAILY MWe-net
- 1 -9 21 -39
~12 '
2 22 ~~ 1.
-11 3 h2 23 ,
b -10 2h h2 5
-11 -a2
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25 6 -11 -25 26
-11 1k1 7 27
-13 265 8 28
-15 h92 9 .- 29
-15 592 10 30 11 -15 '
31 12 -lk 13 -13 1h -lh 15 -13
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-lk 16
-22 1505 26, 17 18 -27
-27 19 7910810 2p
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e SL!MAhY:
UNIT NAME Three Mile Island - Unit 1
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DATE June 8, 1976
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COMPLETED BY b* I'* b"*Y'I TEL. NO. 929-3601 Ext. 111 fiPORT MONTH
- PLANT SHUTD0WNS
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Typt MFTif0D OF F-F0hCED I,U*ATILtj SHIIITING DOWN Na. LME S-SCHEDULED (.iOUhs ) REASGN (1) THE REACTOR (2) COhMENTS 2 2/./0/(6 S 620.8 C A Con:pletion of Befuelis.g 3 5/27/'(6 F T G C Durir.g power escalation nuclear instrun:entation indicated power was 46% while actual power, as calculated by a reactor heat lalance, was f 5%. Huclear Instrumentation power range crannel NI 6 was calitrated t.o 25% power while power range channel NI-5 was ec;ntrolling Integrate :
Control System's (ICS) functions. After N1-6 calit> ration was cc u pletel, ICS control was switched from 13I-5 to NI-6 prior to changing the ec.ntrol cod drive system cont rol to the manual ;csition. Since den.and was at 46% tefore the switch, the ICS systen "saw" that reactor power had fropped lower than denand (i.e. 25% vs. h6%) and started pullir.g control rods to increase power. Henctor Protection System (RIS)
~ channels A&C tripped on overpower at 50% power (BPS trip setpoints had
@ been set to 50% power for reactor physics tests purpose:5).
O Ln N (1) REASON: (2) METHOD:
@ A-EQUIPMENT FAILUBE (EXPLAIN) A-MANUAL g ) B-MAINT. OR TEST B-ftANUAL SchAM C-REFULLING C-AlfrOMATIC SUGd4 D-BEGULA'IDHY RESTRICTION E-OPERATOR TRAINING AND LICENSE EXAMINATION F-AININISTRATIVE G-OPEPATIONAL EbHOH f vvn. r "O
! . , , - - =
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Three "f 4 Island
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- une 9, 1976 parg COMPLETED M L. L. Dr.yar TEL. NO. ~'c v -* r.~ ..
OPERATING STATUS 0001, 76c501 THRcucH 2aCO, 76C531
- 1. REPORTING PERIOD:
I'*k GROSS HCURS IN REPORTING PERICD:
2535 MWe-NET 792 (MAXIMLN DEPE!CA2LE
- 2. CURRENTLY AUTHORIZED PCWER LEVEL MWt CAPACITY - MCC)
NCne 3 PCVER LEVEL 'ID WHICH RECTRICTED (IF ANY):
NA
- k. REASONS FOR RESTRICTICNS (IF ANY):
TdIS CUMULAT!VE MONTH YR-TC-DATE '"O DA*E
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... . 18k.6 1360.7 11332.?
I 5 HOURS REACTOR WAS CRITICAL 0 0 0
.....
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' 6. REACTOR RESERVE SHUTDCWN HOURS .
!
. . . 116.2 1293.7 1105L.6
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7 HOURS CENERA"CR CN-LINE
, O C 0
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- 8. UNIT RESERVE SHUTDOWN HCURS
.913, 21
. . 176 h36 3.087 J21 9 CROSS THERMAL PCWER GE:ERATED (MWH) 56,570 1 CLO,7;L 9,C71,203 e
- 10. GROSS ELECTRICAL POWER GENERATED (MWH) .
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37,325 953,572 3,k?2,907
- 11. NFI ELECTRICAL PCWG C".! ERA *ED lWM) .
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2k.S 37.6 Th.3
' 12. REACTCR AVAILA3ILITY FACTOR (1) 15.6 35.5 72.2
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13 UNIT AVAILABILITY FACTCR (2)
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6k 33 0 69.0
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- 14. UNIT CAPACITY FACTOR (3) 5.7 3.9 ,
3.3
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15 KRCED CL'TAGE RATE (k) .
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NA 17 IF SHUTDCVN AT END CF REPCRT PERICD. ESTIMATED DATE CF STARTUP:
'iOT APPLICABLc
- 18. UNI 3 IN TEST STATUS (PRIOR TD CCMICRCIAL CPERATICN):
'~u 'l^d (1) REAC' OR AVAII.A. BILIN FAC"UR= " " ;N* "~
- 4A3 CFFERIuc
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NCO3 HCURS REPCET!:10
.:ve
~
.--ru p" q " ....e ""'%
., cc (2) UNIT AVAILABILITY FAC*CR= G?% HOURS' T "'^^ IN REPGRTIL FE?!CD r' r - ' m~n aprgp".-en
'" aacoc scc?s :N FErcsT::w : p ; w
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( 3) UNIT CAPAC!'"Y FAC"tR N& M;c" r'. u"q~e - aA.
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- neu *
. ," r r" vc sr~ q' " w' m' " e'
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(k) FCRCED OUTA0E PATE EOURS GENERATCH G -u:2 + fcrJID CUTAJE HOUPC 1505 263