ML19210D067

From kanterella
Revision as of 03:15, 15 August 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 79-087/03L-0:on 791025,torus Water Temp Reached 106 F, Exceeding Allowable Max.Caused by Extended Operation of HPCI Turbine to Obtain Bearing Temp Data.Procedures Which Necessitate High Temps Being Revised
ML19210D067
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 11/16/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19210D059 List:
References
LER-79-087-03L, LER-79-87-3L, NUDOCS 7911200491
Download: ML19210D067 (1)


Text

NRC ,rORg,cs. . . . . . . . . . . . . . . . . . .. . . . . . .

LICENSEE EVENT REPORT CONTROL 8LQCK: l llllllh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 foTTI I n i c i n l v I g l i I@15n in l_ lo lo io lo lo I l ol ol @l4 Iilililil@l I l@7 8 9 LICENSEE CODE 14 LICENSE NUM8ER 2$26 LICENSE TYPE JO

$7 GAT b8 CON'T 0 % it.l@loI5loI-Io 312 15 l@l il of 21 51 7 9l@l I I I I l@o i 7 8 60 4l DOCKET NUMBER 68 69 EVENT DATE 14 7S REPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h o 2 lWhile performing PT 9.2. HPCI Pump and Valve operability Check. and PT 9.5. HPCI

[TTTII 1000# Flow Rate Test, torus water temperature reached 106*F. exceeding the allowed I o 4 I enximum value of 105'F.

Torus cooling was in ooeration durine -nae nf ch4= roaringl M i o 6 i I.o 7ll--en ITITI lTechnical Soecification 3.6.2. 6.9.1.9b l80 7 8 9 oE Co0E SUSC E COMPONENT CODE se D'E SU E FoTTI I s I A lh [3_)h [f_lh l Z l Z l Z l Z l Z l Z lh [Z_jh [Z_j h 7 8 9 10 11 12 13 18 19 20 SEQUENTI AL OCCURRENCE REPORT REVISloN ,,,.LER EVENT YE AR R EPoRT NO.

CooE TYPE N O.@ ,ag'Ro 17191l-llo 8 71 y{ol31 y[--j lol ,a;u 31 J2 21 22 23 24 26 27 28 29 30-K N ACT o ONP NT M HOURS 58 i POR B.SUP Li MANU ACTURER L.xj@lc@l Zl@LZ._l@lofol0101l Yl@[Y,j@lNl@lZI9l9l9l@

33 J4 J5 2 37 40 el 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h W The high enrun u,Per ep per, cure una enused by extended'ooeration of the HPCI li i enrkina nacon=4 e, cad hv n vennfro-one en nhe,4n henvine en-ner,eure dnen.

The MPcTI' i 2 lrurbine una accured nnd rho en-nevnture una raduced to less thnn 95'F.

Present i enn14ng en he pinced in nper,rien at 05' F uhen surveil-l i 3 lnenenanroe ennnfroA enene 4m.sh4ch e d r8 e home en the enrng.

Theme nrocedtayes (cont'd)

I 4linnro *oce4ng to n egroce 7 8 9 So 5A 5% POWE R OTHER STATUS dis RY otSCOVERY oESCRIPTioN NAl(l_j@lPeriodicTest lW @ ni118l@l

'""****1 5" A!TiviTv Co'4 TENT

AuouNT eP ACriv Tv @ l toCATioN oP RELEASE @

RELEASE @ocPaELEast(,g_j@

lNAlNA 8 1 6'****PERsoNNEI ExPCsVAEs

'oEsCRiPTioN @

NuMeER TYPE'l o 01 ol@[ Z,j@l NAli 7 ,_, y-]] (\ [LW i T%o*Di'"' PERsoNNE't iN;UVits

'D DoEsCRiPTioN@

U NuMeERl0 o ol@l NA-,n-i a-, ,. 9 n i2 i )of inu.0 LoS5 OP oR oAMAGE TO PACIL TY Q t TYPE DESCRIPTION N/[Z_j@[NAli 9 7 s 9 i0 s0*DESCRIPTION IS$UE@l j NAlllllllllllllj 2 n P 3 9 10 68 69 80. E A. C. Tollison, Jr. 7011200

[pgong;919-457-9521 E, NAME OF PREPARER

.

.M..LER CONTINUATION - RO# 1-79-87 Facility: BSEP Unit # 1 Eyent Date: 10-25-79

.are being revised to require that torus cooling be placed in service when the torus water temperature reaches 90* F.

....e 6 0 m O e e S 4.O 9 1367 141