ML17285B404
| ML17285B404 | |
| Person / Time | |
|---|---|
| Site: | Columbia |
| Issue date: | 08/02/1990 |
| From: | Sorensen G WASHINGTON PUBLIC POWER SUPPLY SYSTEM |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| GO2-90-133, NUDOCS 9008070082 | |
| Download: ML17285B404 (4) | |
Text
ACCELERATED DI, TRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9008070082 DOC.DATE: 90/08/02 NOTARIZED:
NO FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe AUTH.NAME AUTHOR AFFILIATION SORENSEN,G.C.
Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUBJECT:
Submits justification for continued operation w/emergency diesel generator 2 shorted turns.DISTRIBUTION CODE: AOOID COPIES RECEIVED:LTR (ENCL~SIZE: TITLE: OR Submittal:
General Distribution NOTES'OCKET 05000397 RECIPIENT ID CODE/NAME PD5 LA ENG, P.L.INTERNAL: ACRS NRR/DOEA/OTSB11 NRR/DST/SELB 8D NRR/DST/SRXB 8E 0~MB G-~ITE~IEITE1~02 EXTERNAL: LPDR NSIC COPIES LTTR ENCL 1 5 RECIPIENT ID CODE/NAME PD5 PD NRR/DET/ECMB 9H'RR/DST 8E2 NRR/DST/SICB 7E NUDOCS-ABSTRACT OGC/HDS2 RES/DSIR/EIB NRC PDR COPIES LTTR ENCL NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE iVASTE!CONTAC1 THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR 27 ENCL~0
~q I I l' WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O.Box 968~3000 George Washington Way~Richland, Washington 99352 August 2, 1990 G02-90-133 Docket No.50-397 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Gentlemen:
Subject:
NUCLEAR PLANT NO.2, OPERATING LICENSE NPF-21 EMERGENCY DG-2 SHORTED TURNS;JUSTIFICATION fOR CONTINUED OPERATION
Reference:
Letter, G02-90-130, GC Sorensen (SS)to NRC, same subject, dated July 27, 1990 The reference discussed a shorted turn condition that exists on the generator rotor of the Division 2 emergency diesel generator.
The reference committed to perform the monitoring and trending activities described in the attachment to the reference.
One of the described activities was periodic rotor pole a.c.voltage drop testing.This testing will be performed on a quarterly basis.The procedure to accomplish this testing will include a specific value of the difference in the voltage drop across two in-series poles that will require further review to establish operability.
The procedure will require that when this value is exceeded a Plant Evaluation Request will be written that will result in the test result being brought to the Management Review Committee for evaluation.
This process will ensure that the Justification for Continuted Operation included with the reference remains valid.The procedure will also require that the Plant Manager and the NRC resident inspector be immediately informed of the test result.Yery truly yours, G.C.Sorensen, Manager Regulatory Programs AGH/bk cc: JB Hartin-NRC RV NS Reynolds-BCPSR RB Samworth-NRC DL Williams-BPA/399 NRC Site Inspector-901A 9008070082 900802 PDR ADOCK 05000397 P PDC/Ijgd/~I.o
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