05000313/LER-1980-039-03, /03L:on 801028,exhaust Fan VEF-37A on Lead Hydrogen Purge Sys Tripped.Caused by Short in Control Sys Due to High Resistance Connections at Solenoid Valve Terminals.Rectifier & Control Fuse Replaced & Leads Cleaned

From kanterella
Revision as of 15:55, 23 December 2024 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
/03L:on 801028,exhaust Fan VEF-37A on Lead Hydrogen Purge Sys Tripped.Caused by Short in Control Sys Due to High Resistance Connections at Solenoid Valve Terminals.Rectifier & Control Fuse Replaced & Leads Cleaned
ML20002B108
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 11/25/1980
From: Bramlett L
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20002B099 List:
References
LER-80-039-03L-01, LER-80-39-3L-1, NUDOCS 8012090445
Download: ML20002B108 (2)


LER-1980-039, /03L:on 801028,exhaust Fan VEF-37A on Lead Hydrogen Purge Sys Tripped.Caused by Short in Control Sys Due to High Resistance Connections at Solenoid Valve Terminals.Rectifier & Control Fuse Replaced & Leads Cleaned
Event date:
Report date:
3131980039R03 - NRC Website

text

.

m m.

- ___m I

a W

t w

NRC FORM 356 U S NUCL E AR REGUL ATO9Y @MM117.lON

., (?-778 LICENSEE EVENT REPORT EXHIBIT A CONTROL BLOCl(: l l l l l l l iPLE ASE PRINT OR TYPE ALL REQUIREDINFORMATION) s t

8 l AIR I AIN 1011 l@15l 0101 -10101010101-l 010 Ig4111 lill lig i Ig

+

7 8 le LICEN5(4 CODE i4 LitkN5L Nuv8&H 26 26 LactN51 Tvrt JW 6 7 L A I tsai 1

CcN*T f

O LL_J@l0 I 5 I O! 010131113 l@l 110 I 21 a 8 to i@il 11 !2 i s i 810 l@

o '

3 8

60 61 DOCatThuwSER 64 69 (vtNT DATE

  1. 4 7's REPONT O475 80 4

EVENT DESCRIPTION AND PROBA8LE CONSEQUEN;ES h f oTT11 Durino a monthly surveillance on the lead Hydrogen purge system, the

[

loialI exhaust fan (VEF-37A) tripped.

The standby Hydrogen purge system was rirTTl Ioperable. There have been no similar occurrences.

Reportable per i

ioisiiT.S. 6.12.3.2.(b).

i l o is l l l

fliTTI I l

I o ta l l d

I Ect c'ois' su N E

'I^l L;Y;"d P g.dnNut accNE sMs 8,

I S I ElO L,,EJO LAl@ IV I

! I gg gg u,

n n

~

i.e Tv..a i.',n,7 "WPT

"' ? *

@,aaq,,o u

O In inI L--J l 013I 91 Igj i 013 i L_LJ l--J LJ

_ 21 22 23 24 26 27 28 29 30 3t 3J K 4 A 0

ON 8LANT U T

=*OURS 22 su tTT FO 4m LIJ@L2J@ LLJ@

LZ_J@

10!0101 I W@

Q @ su A inl@1DACTinEn1?l01@

I JJ 34 h

36 II 40 41 43 43 at op CAUSE DESCRIPTION AND CORREC DVE ACTIONS i

li lo l 1 The cause of the exhaust fan trio was determined to be from a short in I

i the enntrol system.

The short occurred due to high resistance connec-I i i Lu U i tions at the teminals of the solenoid valve which suoDlies service wateri u L.J l to seal the fan.

This caused the valve rectifier to fail and in turn i

I caused the control transfomer fuse to blow.

Since (see attachment) i

=>

STANs sPOWEA Cf *ER STATUS SCO H o.;.t.UV E N Cf CloPTsON i

li Is l [E_J@ 1019 I 81@l NA I LB_J@l Surveillance (' Routine) l t

=

' JT,vi,,

can~T 1

e6

.. oust o,,ci.v,T @ J m.,,oso,,,u.a@

u.5o o,.eu n LLLJ LZ.J@ LZJ@l NA l

NA

]

" ' rusoNon e,,o:, Sis ao j

NUV9fM

' TY88 DISCAsPTION 9 Ii I 71'101010 l@[]J@l NT l

-,t SoNN,r,ms, ot:c.,,,,%@

uo.t.

ITTG l d 01 Ol@l NA l

u u

L ! O5 0R AMAG 10 F AC.LITY 0

. 2.J @ l

[

NA

,'S I

io DE 9tPvtON bHCU6EUblY 8, 1@@l NA i

i rigiggiiiiiij 2

NAME OF PREPARER l.

. Bram e d

%h%@MM

,noyg i

l so12osoty5 o**o

  • paup w

n.

F t

t o

L.E.R. # 50-313/80-039 November 25, 1980 l

ANO Unit 1 Cause Description & Corrective Action the fan and solenoid valve are powered through the same control transformer fuse, the fan tripped.

The rectifier and control fuse were replaced.

The solenoid valve was inspected, leads were cleaned and the valve tested.

The system was tested and proved operable.