05000313/LER-1980-040-99, /99X-0:on 801001,during Routine Plant Tour,Rx Bldg Emergency Hatch Local Leak Rate Test Connections Found Uncapped.Caused by Failure to Specify Connections on P&Ids, Test Procedures or Checklists.Caps Replaced

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/99X-0:on 801001,during Routine Plant Tour,Rx Bldg Emergency Hatch Local Leak Rate Test Connections Found Uncapped.Caused by Failure to Specify Connections on P&Ids, Test Procedures or Checklists.Caps Replaced
ML19345A894
Person / Time
Site: Arkansas Nuclear 
Issue date: 11/19/1980
From: Bramlett L
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19345A839 List:
References
LER-80-040-99X, LER-80-40-99X, NUDOCS 8011250380
Download: ML19345A894 (2)


LER-1980-040, /99X-0:on 801001,during Routine Plant Tour,Rx Bldg Emergency Hatch Local Leak Rate Test Connections Found Uncapped.Caused by Failure to Specify Connections on P&Ids, Test Procedures or Checklists.Caps Replaced
Event date:
Report date:
3131980040R99 - NRC Website

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'4 REroHfoAff AJ EVENT DESCRIPTION AND PRO 9 ABLE CONSEGUENCES O'o 10121 LDuring a routine plant tour the Rx building emergency hatch local leak lu i21 I rate test connections were found uncapped. The missing caps effectively i ITTT1 I caused the outer hatch door to be bypassed by a 3/4" connection.

The t oisi i immediate actions were to reinstall the caps.

The emergency doors were ;

Ioperable.

There have been no similar occurrences.

This occurrence is o e Io lil I reported for infonnation.

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2 40 41 42 43 44 of CAUSE DESCRIPTION AND CORRf C fiVE ACTIONS h w 1 A review indicated that the local leak rate connections were not specif-i lilii i ically identified on the olant piping and instrument diagrams, on the i

i local leak rate test Drocedure or on the containment DreheatuD integrity I i i lii31I checklists. See attachment for corrective actions.

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LER 50-313/80-040 ANO-Unit 1 Cause Description & Corrective Actions:

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The caps were replaced and all other hatches, Unit I and II, were verified secured.

The following actions were assigned to prevent reoCCurrenCO.

1.

The local leak rate test procedures are to be revised to require specific signoff steps assuring that the test connections are isolated.

2.

Plant preheatup containment integrity checklists are to be revised to include local leak rate connections on hatches.

3.

Design changes will be initiated as necessary to install isolation valves for local leak rate test connections.

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