ENS 40642
ENS Event | |
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05:30 Apr 5, 2004 | |
Title | Loss of Safety Function for Emergency Diesel Generators During Surveillance Testing |
Event Description | At 0030 [ET] during setup for Unit 1 Division 1 LOCA/LOOP Surveillance testing, the controlling procedure required making the Loss of Power instrumentation for the 1A and 1C ESS buses inoperable. The specification has a 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> time limit for restoration, or the associated Diesel Generators must be declared inoperable. Due to delays during the setup of equipment the time requirements were not met, and the associated Diesel Generators were declared inoperable at 0130. The Susquehanna Safety Analysis requires three operable Diesel Generators to safely shutdown. Therefore, this condition is reportable for Unit 2 under 10CFR50.72(b)(3)(v). Unit 1 is in Mode 5 and therefore not impacted. The Loss of Power instruments were restored, and the Diesel Generators declared operable at 0223.
The licensee notified the NRC Resident Inspector.
The following is a retraction of ENS Notification#40642 AND #40646: On April 5, 2004, PPL Susquehanna, LLC reported three events to the NRC associated with Unit 1 Division 1 LOCA/LOOP surveillance testing. In each case, the safety function of two (out of 4) emergency diesel generators was brought into question during the testing. In two of these events, the E (substituting for A) and C diesel generators were administratively declared inoperable per Technical Specifications. This was necessary because Loss of Power instrumentation for the 1A and 1C buses, rendered inoperable in support of the test procedure, was not restored within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. In the third event, the E (for A) and C emergency diesel generators were, again, declared inoperable when two ESW pump start timers failed to meet acceptance criteria thus bringing the proper start sequencing of emergency loads into question. Because the Susquehanna Safety Analysis requires three diesel generators to safely shutdown an operating unit, the potential compromise of the diesel generator safety function was a concern for Unit 2 in each instance. (NOTE: Unit 1 was in Refueling Mode 5 and was, therefore, not impacted by these events.) Accordingly, Control Room personnel conservatively initiated ENS reporting under 10CFR50.72(b)(3)(v) in response to the apparent loss of safety function for Unit 2. Subsequent engineering analysis has concluded that, although the declaration of diesel generator inoperability was correct and in accordance with Technical Specifications, fulfillment of these administrative actions did not result in an actual loss of safety function during any of the above described events. Details of the analysis show that the diesel generators were available to supply emergency power to the ESS buses and/or that sufficient redundant equipment was available to fulfill the safety function needs of Unit 2. These analysis conclusions provide the basis for retraction of the ENS reports made on April 5, 2004." The licensee notified the NRC Resident Inspector. Notified R1DO (R. Conte) |
Where | |
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Susquehanna Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor | |
Time - Person (Reporting Time:+-1.47 h-0.0613 days <br />-0.00875 weeks <br />-0.00201 months <br />) | |
Opened: | Jim Hufford 04:02 Apr 5, 2004 |
NRC Officer: | Mike Ripley |
Last Updated: | May 27, 2004 |
40642 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |