ENS 57194
ENS Event | |
---|---|
05:59 Jun 27, 2024 | |
Title | Shutdown Required by Technical Specifications |
Event Description | The following information was provided by the licensee via email:
At 0159 EDT on 6-27-24, DC Cook Unit 2 commenced a controlled shutdown to address identified leakage through 2-QRV-251, CVCS [chemical and volume control system] charging pumps discharge flow control valve, valve packing. The leakage started at 2303 EDT on 6-26-24 and was determined to be greater than the 10 gallons per minute limit per technical specification 3.4.13 allowable leakage. The leakage was determined to not be repairable at power. Per 10CFR 50.72(b)(2) this is a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> non-emergency report for Technical Specification required shutdown." The NRC Resident Inspector was notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: A normal shutdown is expected to be completed by 0900 EDT. There are no radiological releases. Unit 1 was not affected. There is no estimate for the time of the repairs. |
Where | |
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Cook Michigan (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+-1.48 h-0.0617 days <br />-0.00881 weeks <br />-0.00203 months <br />) | |
Opened: | Ted Dey 04:30 Jun 27, 2024 |
NRC Officer: | Natalie Starfish |
Last Updated: | Jun 28, 2024 |
57194 - NRC Website
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Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (99 %) |
After | Power Operation (71 %) |
WEEKMONTHYEARENS 571942024-06-27T05:59:00027 June 2024 05:59:00
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