ML16358A654

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Biweekly Notice of Issuance of Amendment No. 199, Request for One-Time Extension of the Diesel Generator Completion Time (Emergency Circumstances)
ML16358A654
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 12/27/2016
From: Siva Lingam
Plant Licensing Branch IV
To:
Division of Operating Reactor Licensing
Lingam S, NRR/DORL/LPLIV, 415-1564
References
CAC MF8961
Download: ML16358A654 (3)


Text

December 27, 2016

MEMORANDUM TO: Biweekly Notice Coordinator

FROM: Siva P. Lingam, Project Manager

/RA APulvirenti for/ Plant Licensing Branch IV Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation

SUBJECT:

REQUEST FOR PUBLICATION IN BIWEEKLY FR NOTICE - NOTICE OF ISSUANCE OF AMENDMENT TO RENEWED FACILITY OPERATING LICENSE, FINAL DETERMINATION OF NO SIGNIFICANT HAZARDS CONSIDERATION, AND OPPORTUNITY FOR HEARING (EMERGENCY CIRCUMSTANCES) (CAC NO. MF8961)

Arizona Public Service Company, et al., Docket No. STN 50-530, Palo Verde Nuclear Generating Station, Unit No. 3, Maricopa County, Arizona Date of application for amendment: December 21, 2016, as supplemented by letter dated December 23, 2016. Brief description of amendment: The emergency amendment revised the Technical Specifications (TSs) for a one-time extension of the emergency diesel generator (DG) completion time described in TS 3.8.1.B.4. Specifically, the emergency amendment extended the TS required action 3.8.1.B.4 completion time from 10 days to 21 days for the purpose of collecting and analyzing data associated with the failure of train B DG and continuing with the repair of the DG. During surveillance testing on December 15, 2016, the DG suffered a failure of the number nine right cylinder connecting rod and piston. Current plans to collect and analyze data associated with the engine failure and continue with the repair will exceed the TS required action completion time of 10 days. As a result, the licensee evaluated the defense-in-depth and compensatory measures and is requesting a one-time deterministic license amendment to extend the completion time based upon the guidance of Standard Review Plan Biweekly Notice Coordinator Branch Technical Position 8-8, "Onsite (Emergency Diesel Generators) and Offsite Power Sources Allowed Outage Time Extensions." Date of issuance: December 23, 2016. Effective date: As of the date of issuance and shall be implemented prior to the expiration of the 10-days completion time, or December 25, 2016, at 3:56 AM PST.

Amendment No.: Unit 3 - 199. A publicly-available version is in ADAMS under Accession No. ML16158A676; documents related to this amendment are listed in the Safety Evaluation enclosed with the amendment.

Renewed Facility Operating License No. NPF-74: The amendment revised the Operating License and TSs.

Public comments requested as to Proposed no significant hazards consideration (NSHC): No. The Commission's related evaluation of the amendment, finding of emergency circumstances, state consultation, and final NSHC determination are contained in a safety evaluation dated December 23, 2016. Attorney for licensee: Michael G. Green, Senior Regulatory Counsel, Pinnacle West Capital Corporation, P.O. Box 52034, Mail Station 8695, Phoenix, Arizona 85072-2034. NRC Branch Chief: Robert J. Pascarelli.

ML16358A654 OFFICE NRR/DORL/LPL4/PM NRR/DORL/LPL4/LA OGC - NLO NRR/DORL/LPL4/BC NRR/DORL/LPL4/PM NAME SLingam PBlechman (JBurkhardt for)BMizuno RPascarelli (LRegner for) SLingam (APulvirenti for) DATE 12/23/16 12/23/16 12/27/16 12/23/16 12/27/16