ML030080299: Difference between revisions

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{{#Wiki_filter:Stephen A. Byrne Senior Vice President, Nuclear Operations 803.345.4622 A SCANA COMPANY                                                       December 30, 2002 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555 Ladies and Gentlemen:
{{#Wiki_filter:Stephen A. Byrne Senior Vice President, Nuclear Operations 803.345.4622 A SCANA COMPANY December 30, 2002 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555 Ladies and Gentlemen:


==Subject:==
==Subject:==
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The LPMS remains out of service. An investigation is currently being done by Plant Support Engineering with vendor support to determine the cause of the failure and the corrective actions to be taken to return the system to service. The system will be returned to service as soon as cause and corrective actions are identified. The condition has been entered in the station's corrective action program.
The LPMS remains out of service. An investigation is currently being done by Plant Support Engineering with vendor support to determine the cause of the failure and the corrective actions to be taken to return the system to service. The system will be returned to service as soon as cause and corrective actions are identified. The condition has been entered in the station's corrective action program.
Should you have any questions, please call Ms. Susan Reese at (803) 345-4591 at your convenience.
Should you have any questions, please call Ms. Susan Reese at (803) 345-4591 at your convenience.
Very truly yours, Stephen A. Byrne SBR/SAB/sr c:   N. 0. Lorick                                                             K. M. Sutton N. S. Cams                                                               INPO Records Center T. G. Eppink                                                             NSRC R. J. White                                                               RTS (0-C-02-3665)
Very truly yours, Stephen A. Byrne SBR/SAB/sr c:
L. A. Reyes                                                               File       (818.08)
N. 0. Lorick K. M. Sutton N. S. Cams INPO Records Center T. G. Eppink NSRC R. J. White RTS (0-C-02-3665)
K. R. Cotton                                                             DMS (RC-02-0209)
L. A. Reyes File (818.08)
NRC Resident Inspector SCE&G I VirgilCSummer NulearStation*P.O Box88.Jenkinsville,South (arolina 290651T(803)345.5209 www.scono.com}}
K. R. Cotton DMS (RC-02-0209)
NRC Resident Inspector SCE&G I VirgilCSummer NulearStation*P.O Box88.Jenkinsville,South (arolina 290651T(803)345.5209 www.scono.com}}

Latest revision as of 13:24, 16 January 2025

Special Report 2002-002
ML030080299
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 12/30/2002
From: Byrne S
South Carolina Electric & Gas Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
Download: ML030080299 (1)


Text

Stephen A. Byrne Senior Vice President, Nuclear Operations 803.345.4622 A SCANA COMPANY December 30, 2002 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555 Ladies and Gentlemen:

Subject:

VIRGIL C. SUMMER NUCLEAR STATION DOCKET NO. 50/395 OPERATING LICENSE NO. NPF-12 SPECIAL REPORT 2002-002 South Carolina Electric & Gas Company (SCE&G) is submitting this report pursuant to the requirements of Technical Specification 3.3.3.10, Action a.

On November 24, 2002, at 1245 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.737225e-4 months <br />, the Loose-Part Monitor System (LPMS) was declared inoperable. The equipment was taken out of service due to a faulty component. The faulty component appears to be the Control Unit, which provides alarm indication, but does not impact the actual operation of the monitoring system. The Control Unit had indications of failed components. The Control Unit was removed and sent to Framatone ANP for repair. The repaired unit was received onsite and installed on December 20, 2002. The Control Unit failed approximately two hours after installation.

The LPMS remains out of service. An investigation is currently being done by Plant Support Engineering with vendor support to determine the cause of the failure and the corrective actions to be taken to return the system to service. The system will be returned to service as soon as cause and corrective actions are identified. The condition has been entered in the station's corrective action program.

Should you have any questions, please call Ms. Susan Reese at (803) 345-4591 at your convenience.

Very truly yours, Stephen A. Byrne SBR/SAB/sr c:

N. 0. Lorick K. M. Sutton N. S. Cams INPO Records Center T. G. Eppink NSRC R. J. White RTS (0-C-02-3665)

L. A. Reyes File (818.08)

K. R. Cotton DMS (RC-02-0209)

NRC Resident Inspector SCE&G I VirgilCSummer NulearStation*P.O Box88.Jenkinsville,South (arolina 290651T(803)345.5209 www.scono.com