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| {{Adams
| | #REDIRECT [[05000321/LER-1980-085-03, /03L-0:on 800720,w/unit at 300 Mwt & O Mwe,Reactor Water Not Sampled & Analyzed for Chlorides & Ph.Caused by Personnel Oversight.Retraining Session for Responsible Employees Conducted]] |
| | number = ML19331B596
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| | issue date = 08/07/1980
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| | title = LER 80-085/03L-0:on 800720,w/unit at 300 Mwt & O Mwe,Reactor Water Not Sampled & Analyzed for Chlorides & Ph.Caused by Personnel Oversight.Retraining Session for Responsible Employees Conducted
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| | author name = Rogers W
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| | author affiliation = GEORGIA POWER CO.
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| | addressee name =
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| | addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
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| | docket = 05000321
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| | license number =
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| | contact person =
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| | document report number = LER-80-085-03L-01, LER-80-85-3L-1, NUDOCS 8008120479
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| | package number = ML19331B583
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| | document type = LICENSEE EVENT REPORT (SEE ALSO AO,RO), TEXT-SAFETY REPORT
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| | page count = 2
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| }}
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| | |
| =Text=
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| {{#Wiki_filter:NRC FORM 364 . U.S. NUCLEAR REGULATCRY COMMISSION
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| . (7 77) ,
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| t LICENSEE EVENT REPORT O. -
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| CONTROL BLOCK: l 1
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| l l l l l lh 6
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| (PLEASE PRINT CR TYPE ALL REQUIRED INFORMATION) l1l@l1 l1 l@
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| 0 1 l 7 8 l G l A l E l I l H l 1 l@15l 0 l0 l- l 0 l0 l0 l0 l0 l'-LICENSE 9 LICENSEE CODE 14 LICENSE NUMBER 25 26 l0 l0TYPEl@l4 Jo 57l1CAT 58 CON'T "E
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| i o
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| 8 3ou l60L l@l 68 015 lDOCKET 0l0 l0 l 3 l 268 l1 69l@l0EVENT
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| : t. UMBER l7 DATE l2 l018 l0 l@l0 74 75 l8 l0DATEl71810 REPORT
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| ~
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| 80 l@
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| EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h IT]T1 1On 7-20-80, with the unit at 300 MWT and 0 MWE reactor water was not i O 3 l sampled and analyzed for chlorides and pH at 1530 and 2330 hours as i O 4 frequired by Tech Spec Sections 4.6.F.2.c.2 and 4.6.F.2.c.3. This is l 0 s la non-repetitive occurrence. There were no effects on public health ' i l Tis ] land safety due to this event. I l
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| c 7 [
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| I ITITI I 80 DE CODE S BC E COMPONENT CODE SUS dE SU E O 9 l9 Zl Zl@ @ (_D_j h l Zl Zl Z l Z l Z l Z l@ [Z_J @ [ Z_J 20 10 11 12 13 18 19 7 8 REVISION SEQUENTIAL OCCURRENCE REPORT EVENT YE AR REPORT NO. CODE TYPE NO.
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| LE R/RO O ,RE, 1810 l l-l 10 l8 15 l (g_] 10 l3l [LJ (--J [Q_j 32 22 23 24 26 27 28 29 30 31
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| _ 21 ON P NT M O HOURS S8 IT FOR 8. SUPPLI MANUFAC RER T N AC O LnJ@LZJ@ LZJ@ LZ_J@ lo lo 10 l0 l l41 Yl@ [Nj@ [jyj@ lZ 44 l9 l9 l947l@
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| 3J 34 3h 36 31 40 42 43 7
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| CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 8 iThe cause of these events can be attributed to an oversight by the l l personnel responsible for taking samples. A re-training session for l i i 1 2 lall personnel who collect and analyse reactor water has been conducted l i 3 l stressing the Tech Spec requirements for reactor water sampling. l I
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| 1 4 I a0 7 8 9 DIS O / RY DISCOVERY DESCR:PTION i 5 STA (E_j@ l0l1l2l@l
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| % POWER OTHER STATUS O/A l [Z_J@l N/A j ACTivlTY CO TENT AMOUNT OF ACTIVITY LOCATION OF RELEASE P.ELEASE@D OF RELE ASE_Zj@l N/A l 7
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| 1 6 8 9 (Z] 10 11 N/A 44 l l 45 , , ,
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| . 80 PERSONNEL FxPOSURES DESCRIPTION --
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| NUYHER TYPE i 7 l0l0l0l@(_gj@l N/A I
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| ' ' ' ,ERSONN d',N,uL S ''
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| ~uvet R DESCniPTioN@ l
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| > a lo l0 lo l@l N/A 80 7 8 9 11 12 LO*.S OF OR DAMAGE TO FACILITY #
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| TYPE DESCRIPTION 1 9 [3j@l '
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| N/A 80 l
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| 7 8 9 10
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| """ ~ ann o~Lv 2 O ,SSUl[@LLPT.ON@
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| l 800823o%77N/A -
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| l lllllllllt1Il[
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| [3_ 6R 69 83 5 7 8 9 to NAurmamumn W. H. Ibgers Health Physics PHONE: 912-367-7781
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| {
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| c LERG: .'50-321/1980-085:
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| Licensce: Georgia Ptraer Company Facility Nane: llidin I Ilatch Ibcket #: 50-321 NMIRATIVE REPORP
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| . futIRt 50-321/1980-085 On 7-20-80, with the unit at 300 M1r and 0 MP, the reactor water conductivity exceeded 2.0 umho/cm due to a condenser tube leak and only oin reactor water c1can up punp in service. ' Tech Spec Sections 4.6.F.2.c.2 and.4.6.F.2.c.3 require a pII and chloride r.rasurcrent to be taken every cight hours.should the reactor water conductivity exceed-2.0 unho/cm. '1ko consecutive eight nour samples were missed after this occurrence. Subsequent sample analyses indicate, hoaever, that pil and chloride values were well within Tcdi Si n: 1 requirennnts for reactor water. fnis is a non-repetitive occurrence. 'Ihere
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| .were In effects on the public health and safety due to this event.-
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| The cause of these events can be $ttributed to an oversight by the personnel responsible for taking sanples. A re-training session for all personnel who
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| - collect and analyze reactor water has been conducted, stressing the Tech Spec requirements for reactor water samples on both Units 1 and 2.
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