PNO-IV-90-034, on 900929,Unit 1 Manually Tripped & Will Remain Shutdown to Allow Repairs to Bellows in Low Pressure Turbine.Unit 2 Entered First Refueling Outage: Difference between revisions

From kanterella
Jump to navigation Jump to search
StriderTol Bot insert
 
StriderTol Bot change
 
Line 14: Line 14:
| page count = 2
| page count = 2
}}
}}
{{#Wiki_filter:-                                                 .          ..                    -  -      .  .
{{#Wiki_filter:-
  '
October 1, 1990
* October 1, 1990
' PREL'IMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE -- PNO-IV-90-34 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region IV staff on this date.
    ' PREL'IMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE -- PNO-IV-90-34 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received               ,
i FACILITY: Houston Lighting & Power Company Licensee Emergency Classification:
without verification or evaluation, and is basically all that is known by the                   >
South Texas Project, Units 1 and 2 Notification of Unusual Event (Dockets: 50-498;50-499)
Region IV staff on this date.                                                                 i FACILITY: Houston Lighting & Power Company         Licensee Emergency Classification:         ,
Alert i
South Texas Project, Units 1 and 2           Notification of Unusual Event         -
~
(Dockets: 50-498;50-499)               ~
Site Area Emergency i
Alert                                 i Site Area Emergency                 i General Emergency                   i T~ Not Applicable                         .
General Emergency i
T~ Not Applicable


==SUBJECT:==
==SUBJECT:==
UNIT 1 FORCED SHUTDOWN TO EXCEED 72 HOURS AND UNIT 2 BEGINS FIRST REFUELING OUTAGE On September 29,1990, at 2:30 a.m., Unit 1 was manually tripped from 100 percent power. A partial stroke test of the "A" feedwater 1 solation valve (FWIV) was                 ,
UNIT 1 FORCED SHUTDOWN TO EXCEED 72 HOURS AND UNIT 2 BEGINS FIRST REFUELING OUTAGE On September 29,1990, at 2:30 a.m., Unit 1 was manually tripped from 100 percent power. A partial stroke test of the "A" feedwater 1 solation valve (FWIV) was ongoing when an instrumentation and control tecnnician placed his test leads on the incorrect terminal, resulting in the FWIV fully closing. The reactor operator insiediately initiated a tranual reactor scram. A test push button which would normally be utilized, was inoperable at the t'me.
ongoing when an instrumentation and control tecnnician placed his test leads on               ,
This required the technician to utilize an engineering procedure, which requird Se placement of jumpers.
the incorrect terminal, resulting in the FWIV fully closing. The reactor operator insiediately initiated a tranual reactor scram. A test push button which would                 '
Following the manual trip a second engineered safety activrtion of the auxiliary feedwater (AFW) system occurred because of a shrink in the "C' steam generator, Anoperatorhadopenedthe"C"steamgeneratorpoweroperatorreliefvalve(PORV) from 10 to 35 percent open. An indicated level swell occurred because of the pressure decrease from the open PORV. When the PORY was closed, the actuation-setpoint for AFW in initiation was reached on the indciated low steam generator level.
normally be utilized, was inoperable at the t'me. This required the technician to utilize an engineering procedure, which requird Se placement of jumpers.
Licensee management has decided to maintain the unit shutdown urtil a fontalized self-verification training program has been established and givrn to all i
Following the manual trip a second engineered safety activrtion of the auxiliary feedwater (AFW) system occurred because of a shrink in the "C' steam generator,               ,
maintenance and operations personnel. The unit will remain shu c - Nr approximately 10 days to allow repairs to a bellows in a low pre nuce turbine.
Anoperatorhadopenedthe"C"steamgeneratorpoweroperatorreliefvalve(PORV)                         ,
The licensee indicated that the unit was taken to Hode 4 because the need to establish the formalized training, l
from 10 to 35 percent open. An indicated level swell occurred because of the                   ,
Unit 2 entered their first refueling outage at approximately 1 a.m. en September 29, 1990.
pressure decrease from the open PORV. When the PORY was closed, the actuation-setpoint for AFW in initiation was reached on the indciated low steam generator level.
Following the trip of Unit 1, the second units' caoloown was delayed to ensure sufficient steam was available to efficiently cooldown the first unit. Unit ? entered Mode 5 at 4:a7 a.m. on October 1,1990. %c licensee will perform a complete fuel off load during this refueling outage.
Licensee management has decided to maintain the unit shutdown urtil a fontalized self-verification training program has been established and givrn to all                       i maintenance and operations personnel. The unit will remain shu c - Nr approximately 10 days to allow repairs to a bellows in a low pre nuce turbine.
The licensee indicated that the unit was taken to Hode 4 because # the need to establish the formalized training,                                                             ,
l      Unit 2 entered their first refueling outage at approximately 1 a.m. en September 29, 1990. Following the trip of Unit 1, the second units' caoloown was delayed to ensure sufficient steam was available to efficiently cooldown the first unit. Unit ? entered Mode 5 at 4:a7 a.m. on October 1,1990. %c licensee will perform a complete fuel off load during this refueling outage.
Neither the licensee nor the NRC plans to issue a press release.
Neither the licensee nor the NRC plans to issue a press release.
The state of Texas will be informed.
The state of Texas will be informed.
Region lY received notification of this occurrence by telephone from SRI at 9 a.m. on September 29, 1990. Region IV has informed EDO, NRR, and PA.
Region lY received notification of this occurrence by telephone from SRI at 9 a.m. on September 29, 1990. Region IV has informed EDO, NRR, and PA.
This information has been confirmed with a licensee representative.
This information has been confirmed with a licensee representative.
        .M                 A                                                                   l RIV:D:DRP/.       RA W                                                               ,il       i SJCollinsP'       RDMartin                                                         62
.M A
      /t/(/90       /d / / /90                                                       }U 9010120052 901001                                                   \       .
RIV:D:DRP/.
OD E           g_1Mo_o34 esu-
RA W
,il l i
SJCollinsP' RDMartin 62
/t/(/90
/d / / /90
}U 9010120052 901001
\\
OD E g_1Mo_o34 esu-


c   ,
c w
w i     . GONTACT DISTRIBUTION:
i GONTACT DISTRIBUTION:
OWFN                     NMBB NL       MAIL: DCS(Orig.IE34)
OWFN NMBB NL MAIL: DCS(Orig.IE34)
Chan, carr     CA NM55 EUU   RS             00T (Transp. Only)
Chan, carr CA NM55 EUU RS 00T (Transp. Only)
Cose. Rogers   OGC NRR   IRH Cose. Curtiss GPA SLITP OIG   FAX:   (5520: 8/j/909 /cf g Cosen. Remick PA DE         1W0           Egions & HQ)
Cose. Rogers OGC NRR IRH Cose. Curtiss GPA SLITP OIG FAX:
ACRS           EDO             PDR l                                   L.St NSAC i
(5520: 8/j/909 /cf g Cosen. Remick PA DE 1W0 Egions & HQ)
FBf   RRI EW-W NRC OPS Ctr X5TKP Licensee (Reactor) i l
ACRS EDO PDR l
_ _ _ . .}}
L.St NSAC i
FBf RRI EW-W NRC OPS Ctr X5TKP Licensee (Reactor) i l
_ _ _..}}


{{PNO-Nav|region=IV}}
{{PNO-Nav|region=IV}}

Latest revision as of 01:44, 17 December 2024

PNO-IV-90-034:on 900929,Unit 1 Manually Tripped & Will Remain Shutdown to Allow Repairs to Bellows in Low Pressure Turbine.Unit 2 Entered First Refueling Outage
ML20059N353
Person / Time
Site: South Texas  
Issue date: 10/01/1990
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
References
PNO-IV-90-034, PNO-IV-90-34, NUDOCS 9010120052
Download: ML20059N353 (2)


-

October 1, 1990

' PREL'IMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE -- PNO-IV-90-34 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region IV staff on this date.

i FACILITY: Houston Lighting & Power Company Licensee Emergency Classification:

South Texas Project, Units 1 and 2 Notification of Unusual Event (Dockets: 50-498;50-499)

Alert i

~

Site Area Emergency i

General Emergency i

T~ Not Applicable

SUBJECT:

UNIT 1 FORCED SHUTDOWN TO EXCEED 72 HOURS AND UNIT 2 BEGINS FIRST REFUELING OUTAGE On September 29,1990, at 2:30 a.m., Unit 1 was manually tripped from 100 percent power. A partial stroke test of the "A" feedwater 1 solation valve (FWIV) was ongoing when an instrumentation and control tecnnician placed his test leads on the incorrect terminal, resulting in the FWIV fully closing. The reactor operator insiediately initiated a tranual reactor scram. A test push button which would normally be utilized, was inoperable at the t'me.

This required the technician to utilize an engineering procedure, which requird Se placement of jumpers.

Following the manual trip a second engineered safety activrtion of the auxiliary feedwater (AFW) system occurred because of a shrink in the "C' steam generator, Anoperatorhadopenedthe"C"steamgeneratorpoweroperatorreliefvalve(PORV) from 10 to 35 percent open. An indicated level swell occurred because of the pressure decrease from the open PORV. When the PORY was closed, the actuation-setpoint for AFW in initiation was reached on the indciated low steam generator level.

Licensee management has decided to maintain the unit shutdown urtil a fontalized self-verification training program has been established and givrn to all i

maintenance and operations personnel. The unit will remain shu c - Nr approximately 10 days to allow repairs to a bellows in a low pre nuce turbine.

The licensee indicated that the unit was taken to Hode 4 because the need to establish the formalized training, l

Unit 2 entered their first refueling outage at approximately 1 a.m. en September 29, 1990.

Following the trip of Unit 1, the second units' caoloown was delayed to ensure sufficient steam was available to efficiently cooldown the first unit. Unit ? entered Mode 5 at 4:a7 a.m. on October 1,1990. %c licensee will perform a complete fuel off load during this refueling outage.

Neither the licensee nor the NRC plans to issue a press release.

The state of Texas will be informed.

Region lY received notification of this occurrence by telephone from SRI at 9 a.m. on September 29, 1990. Region IV has informed EDO, NRR, and PA.

This information has been confirmed with a licensee representative.

.M A

RIV:D:DRP/.

RA W

,il l i

SJCollinsP' RDMartin 62

/t/(/90

/d / / /90

}U 9010120052 901001

\\

OD E g_1Mo_o34 esu-

c w

i GONTACT DISTRIBUTION:

OWFN NMBB NL MAIL: DCS(Orig.IE34)

Chan, carr CA NM55 EUU RS 00T (Transp. Only)

Cose. Rogers OGC NRR IRH Cose. Curtiss GPA SLITP OIG FAX:

(5520: 8/j/909 /cf g Cosen. Remick PA DE 1W0 Egions & HQ)

ACRS EDO PDR l

L.St NSAC i

FBf RRI EW-W NRC OPS Ctr X5TKP Licensee (Reactor) i l

_ _ _..