05000000/LER-1977-005, Updated LER 77-005/1T:on 770114,failure of High Pressure Svc Water/Emergency Svc Water & Emergency Cooling Water Pumps to Meet FSAR Seismic Requirements Noted.Caused by Change in Calculation Techniques: Difference between revisions
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| Docket = 05000000 | | Docket = 05000000 | ||
| LER year = | | LER year = 1977 | ||
| LER number = 5 | | LER number = 5 | ||
| LER revision = | | LER revision = 0 | ||
| Event date = | | Event date = | ||
| Report date = | | Report date = | ||
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{{#Wiki_filter:- | {{#Wiki_filter:- | ||
O- | O-O PHILADELPHIA ELECTRIC COMPANY j | ||
2301 MARKET ST.* LEET l | |||
PHILADELPHIA. PA.19101 (215) 84 t-4000 i | |||
PHILADELPHIA. PA.19101 | January 28, 1 U7 l | ||
../ | |||
Mr. J. P. O'Rel liy l | l Mr. J. P. O'Rel liy l | ||
Director, Region 1 Office or Inspection and Enforcement U. S. Nucicar Regulatory Comnission 631 Park Avenue y | |||
King of Prussia, PA 19406 Daar Mr. O'Reilly: | |||
U. S. Nucicar Regulatory Comnission 631 Park Avenue | ' ' ~~ y' | ||
Daar Mr. O'Reilly: | |||
==SUBJECT:== | ==SUBJECT:== | ||
hortable Occurrence Folicw-up Report-1, Office of Inspection and Enforcement 14, | hortable Occurrence Folicw-up Report-1, Office of Inspection and Enforcement on JanuaryThe following occurren 14, 1977 Written notification was made to Mr. George I. car, Chief, Operating Reactors Branch | ||
#3, Division of Reactor Licensing and Mr. J. P. O'Reilly, Director, Region 1, Office of Inspection and Enfc,rcement on January 14, 1977. | |||
for Unit 2 and OPR-56 for Unit 3, Peach Bottom. Atomic Power Station, the following | In accordance with Section 6 9.2.a of the Technical Specifications, Appendix A of DPR - | ||
for Unit 2 and OPR-56 for Unit 3, Peach Bottom. Atomic Power Station, the following information is being provided to supplement the attached i.icensee Event Report. | |||
==Reference:== | ==Reference:== | ||
Docket Nos. 50-277 and 50 278-Technical Specification Reference 6 9 2.a(9) | |||
I Report No.: | |||
2-77-5/1T Report Date: | |||
January 28, 1977 l-Occurrence Date: | |||
Ja.uary 14, 1977 Facility: | |||
Feach Cottom Atomic Power Station Units 2 and 3 R.9. 1, Delta, Pennsylvania 17314 l | |||
==Event Description== | |||
== Description | |||
During the perforr.iance of a sar'ety e val'aation of a proposed | During the perforr.iance of a sar'ety e val'aation of a proposed | ||
,PIant modification, as.equired by the Peach Bottom Unit.1 2 & 3 qualit assurance progr.w, it we. four.d thac the High Pressure Service Water / y Ernergency Service Vate.-/ Emery ncy Coolir.g ht.sr aumos do not meet FSAR seisn.ic c* assification requiruvents. | |||
seisn.ic c* assification requiruvents. Tr.e. e have beer. no previous occur-tences. | Tr.e. e have beer. no previous occur-i tences. | ||
8312130068 771005 l | 8312130068 771005 l | ||
PDR | PDR ADOCK 05000277 S | ||
PDR l | |||
..,o j | |||
j | |||
~ / | |||
the | 1 l | ||
-.'J. P. O 'Rei l ly | |||
~o O 2 77-5/ir | |||
[ Jan~uary 28, 1977 Pago 2 l | |||
g use Description: | |||
The purchase specification for these pumps required a seismic analysis. | |||
This analysis was made using an equivalent static analysis technique which converts a dynamic loading to a static loading. | |||
of this analysis were received by our Architect Engineer (Bechtcl) on Results January 14, 1972. | |||
These results show that the pumps were capable of withstanding the design scismic events well within quoted allowable stresses. | |||
The Architect Engineer, however, aware of pending project scismic specification changes relating to calculational techniques deferred his detailed review. | |||
In March 1974, the vendor was provided with the Philadelphia Electric Company approved General Project Class I Seismic Requirements Specifica*. ion. The vendor performed a seismic re-analysis using the dynamic analysis technique in accordance with the Specification to verify his equipment capability to withstand the design basis seismic events. | |||
The results of his re-analysis were reported to. | |||
our Architect Engincer in November 1974, and indicated that the pumps were not capable of withstanding the design basis seismic events with - | our Architect Engincer in November 1974, and indicated that the pumps were not capable of withstanding the design basis seismic events with - | ||
in allowable stresses. The report also contained suggested minor modi = | in allowable stresses. | ||
The report also contained suggested minor modi = | |||
fications to restore scismic Class I capability. | fications to restore scismic Class I capability. | ||
Philadelphic Electric Company. was advised of this recommended corrective action in Bechtel's letter to Philadelphia Electric dated April 9,1975 (BLP 12313); af ter which Philadelphia Electric authorized the preparation | Philadelphic Electric Company. was advised of this recommended corrective action in Bechtel's letter to Philadelphia Electric dated April 9,1975 (BLP 12313); af ter which Philadelphia Electric authorized the preparation of the engineering work package, including quality docu-mentation requirements. | ||
Because of the language in this letter, our engineers, although approving the work, did not assign a high priority to the | Because of the language in this letter, our engineers, although approving the work, did not assign a high priority to the modifications.' This was an error, and is responsible:for the'.,. | ||
delay in corrective action. | |||
It was not until late 1976.that.the nee - | |||
not until late 1976.that.the nee - | essary modification sign-offs were sought. | ||
assurance phase that the defici' n'cy | It was during this quality, | ||
assurance phase that the defici' n'cy of not meeting' the FSAR 'scisniic--- | |||
requirements was identified and prompt corrective action was initiated. | e requirements was identified and prompt corrective action was initiated. | ||
Corrective Action | |||
Equipment procurement is underway. Field work is expected to start on ESV and ECW pumps on January 31, 1977 | ==Corrective Action== | ||
Equipment procurement is underway. Field work is expected to start on ESV and ECW pumps on January 31, 1977 Work on the HPSW punps will start shortly thereaf ter. We plan to complete this work as soon as possibic. | |||
follows: | Specific modifications and schedules are as follows: | ||
l. | |||
a.. Column flange bolts will be replaced with higher | High Pressure Service Water Pumps: | ||
strength material; | a.. Column flange bolts will be replaced with higher strength material; 8 | ||
b. | |||
February 11, 1977. Efforts are being made to | Bolts, are on order and delivery is expected on February 11, 1977. | ||
expidite delivery, t | Efforts are being made to expidite delivery, t | ||
4 6 | 4 6 | ||
e' | e' | ||
.... f. | |||
'M. J. P. O'Rei l ly - O O | |||
January 28, 1977 | sn 9or January 28, 1977 page 3 l | ||
t Installation will begin upon receipt of materials c. | |||
and is expected to be complete by April 15, 1977 2 | |||
Emergency Service Water Purnps and Ernergency Cooling Water Pumps: | |||
a. | |||
l | Lateral supports will be added at the top to the bowl assemblics f or these pumps. | ||
In addition, the motor hold down bolts for the Emergency Service Water Pumps will be replaced with higher strength material. | |||
b. | |||
Material for lateral supports was roccived on site on January 27, 1977. | |||
l c. | |||
Installation will start on January 31, 1977 and will be errnpleted March 18, 1977. | |||
With regard to the error in 'our quality review program whidh'" | With regard to the error in 'our quality review program whidh'" | ||
f ailed to note the importance of this item and resulted in delayed implementation of corrective action, it is not expected that this type.. | f ailed to note the importance of this item and resulted in delayed implementation of corrective action, it is not expected that this type.. | ||
error will recur. Modifications to the Peach Bottom Plant are under - | error will recur. Modifications to the Peach Bottom Plant are under - | ||
strict administrative procedure control. This procedure requires section review of all proposed plant modifications and docurrentation of such review on approved document control forms. | strict administrative procedure control. This procedure requires section review of all proposed plant modifications and docurrentation of such review on approved document control forms. | ||
In 1975, when the deficiency regarding the seitmic design of the pumps was first brought to the attention of Philadelphia Electric, the use of this procedure was in its inf ancy. Considerable progress has been.mado -in complying % | |||
with it. | with it. | ||
Safety Imolications:_, | Safety Imolications:_, | ||
This occurrence .is believed to have minimal effect on plant safety because of tbc low pr obability of the occurrence of a scismic event of intensity equal to the design basis scismic event, and the short period of time required to impicracnt corrective action. The Operation and Safety Revi-w Conmittee has reviewed this matter and cpproved this course of action. | This occurrence.is believed to have minimal effect on plant safety because of tbc low pr obability of the occurrence of a scismic event of intensity equal to the design basis scismic event, and the short period of time required to impicracnt corrective action. The Operation and Safety Revi-w Conmittee has reviewed this matter and cpproved this course of action. | ||
I | I i | ||
l | |||
.Very truly yours, i | |||
1 hj | |||
cc | .k. | ||
Opera-ing Reactorc Or. nch #.7 | J Cooney Su.intendent Generatlon civision-Nuclear Attechment cc Mr. Geo. ge Lc?r, Chicf Opera-ing Reactorc Or. nch #.7 Divisic.n of Oper st'ng Recctors | ||
Divisic.n of Oper st'ng Recctors | ..e me | ||
}} | }} | ||
{{LER-Nav}} | {{LER-Nav}} | ||
Latest revision as of 02:18, 14 December 2024
| ML20086F137 | |
| Person / Time | |
|---|---|
| Site: | Peach Bottom, 05000000 |
| Issue date: | 01/28/1977 |
| From: | Cooney M PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC |
| To: | James O'Reilly NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| Shared Package | |
| ML20086F058 | List: |
| References | |
| LER-77-005-01T-02, LER-77-5-1T-2, LER-LER-77-5-1T, NUDOCS 8312130068 | |
| Download: ML20086F137 (3) | |
| Event date: | |
|---|---|
| Report date: | |
| 0001977005R00 - NRC Website | |
text
-
O-O PHILADELPHIA ELECTRIC COMPANY j
2301 MARKET ST.* LEET l
PHILADELPHIA. PA.19101 (215) 84 t-4000 i
January 28, 1 U7 l
../
l Mr. J. P. O'Rel liy l
Director, Region 1 Office or Inspection and Enforcement U. S. Nucicar Regulatory Comnission 631 Park Avenue y
King of Prussia, PA 19406 Daar Mr. O'Reilly:
' ' ~~ y'
SUBJECT:
hortable Occurrence Folicw-up Report-1, Office of Inspection and Enforcement on JanuaryThe following occurren 14, 1977 Written notification was made to Mr. George I. car, Chief, Operating Reactors Branch
- 3, Division of Reactor Licensing and Mr. J. P. O'Reilly, Director, Region 1, Office of Inspection and Enfc,rcement on January 14, 1977.
In accordance with Section 6 9.2.a of the Technical Specifications, Appendix A of DPR -
for Unit 2 and OPR-56 for Unit 3, Peach Bottom. Atomic Power Station, the following information is being provided to supplement the attached i.icensee Event Report.
Reference:
Docket Nos. 50-277 and 50 278-Technical Specification Reference 6 9 2.a(9)
I Report No.:
2-77-5/1T Report Date:
January 28, 1977 l-Occurrence Date:
Ja.uary 14, 1977 Facility:
Feach Cottom Atomic Power Station Units 2 and 3 R.9. 1, Delta, Pennsylvania 17314 l
Event Description
During the perforr.iance of a sar'ety e val'aation of a proposed
,PIant modification, as.equired by the Peach Bottom Unit.1 2 & 3 qualit assurance progr.w, it we. four.d thac the High Pressure Service Water / y Ernergency Service Vate.-/ Emery ncy Coolir.g ht.sr aumos do not meet FSAR seisn.ic c* assification requiruvents.
Tr.e. e have beer. no previous occur-i tences.
8312130068 771005 l
PDR ADOCK 05000277 S
PDR l
..,o j
~ /
1 l
-.'J. P. O 'Rei l ly
~o O 2 77-5/ir
[ Jan~uary 28, 1977 Pago 2 l
g use Description:
The purchase specification for these pumps required a seismic analysis.
This analysis was made using an equivalent static analysis technique which converts a dynamic loading to a static loading.
of this analysis were received by our Architect Engineer (Bechtcl) on Results January 14, 1972.
These results show that the pumps were capable of withstanding the design scismic events well within quoted allowable stresses.
The Architect Engineer, however, aware of pending project scismic specification changes relating to calculational techniques deferred his detailed review.
In March 1974, the vendor was provided with the Philadelphia Electric Company approved General Project Class I Seismic Requirements Specifica*. ion. The vendor performed a seismic re-analysis using the dynamic analysis technique in accordance with the Specification to verify his equipment capability to withstand the design basis seismic events.
The results of his re-analysis were reported to.
our Architect Engincer in November 1974, and indicated that the pumps were not capable of withstanding the design basis seismic events with -
in allowable stresses.
The report also contained suggested minor modi =
fications to restore scismic Class I capability.
Philadelphic Electric Company. was advised of this recommended corrective action in Bechtel's letter to Philadelphia Electric dated April 9,1975 (BLP 12313); af ter which Philadelphia Electric authorized the preparation of the engineering work package, including quality docu-mentation requirements.
Because of the language in this letter, our engineers, although approving the work, did not assign a high priority to the modifications.' This was an error, and is responsible:for the'.,.
delay in corrective action.
It was not until late 1976.that.the nee -
essary modification sign-offs were sought.
It was during this quality,
assurance phase that the defici' n'cy of not meeting' the FSAR 'scisniic---
e requirements was identified and prompt corrective action was initiated.
Corrective Action
Equipment procurement is underway. Field work is expected to start on ESV and ECW pumps on January 31, 1977 Work on the HPSW punps will start shortly thereaf ter. We plan to complete this work as soon as possibic.
Specific modifications and schedules are as follows:
l.
High Pressure Service Water Pumps:
a.. Column flange bolts will be replaced with higher strength material; 8
b.
Bolts, are on order and delivery is expected on February 11, 1977.
Efforts are being made to expidite delivery, t
4 6
e'
.... f.
'M. J. P. O'Rei l ly - O O
sn 9or January 28, 1977 page 3 l
t Installation will begin upon receipt of materials c.
and is expected to be complete by April 15, 1977 2
Emergency Service Water Purnps and Ernergency Cooling Water Pumps:
a.
Lateral supports will be added at the top to the bowl assemblics f or these pumps.
In addition, the motor hold down bolts for the Emergency Service Water Pumps will be replaced with higher strength material.
b.
Material for lateral supports was roccived on site on January 27, 1977.
l c.
Installation will start on January 31, 1977 and will be errnpleted March 18, 1977.
With regard to the error in 'our quality review program whidh'"
f ailed to note the importance of this item and resulted in delayed implementation of corrective action, it is not expected that this type..
error will recur. Modifications to the Peach Bottom Plant are under -
strict administrative procedure control. This procedure requires section review of all proposed plant modifications and docurrentation of such review on approved document control forms.
In 1975, when the deficiency regarding the seitmic design of the pumps was first brought to the attention of Philadelphia Electric, the use of this procedure was in its inf ancy. Considerable progress has been.mado -in complying %
with it.
Safety Imolications:_,
This occurrence.is believed to have minimal effect on plant safety because of tbc low pr obability of the occurrence of a scismic event of intensity equal to the design basis scismic event, and the short period of time required to impicracnt corrective action. The Operation and Safety Revi-w Conmittee has reviewed this matter and cpproved this course of action.
I i
l
.Very truly yours, i
1 hj
.k.
J Cooney Su.intendent Generatlon civision-Nuclear Attechment cc Mr. Geo. ge Lc?r, Chicf Opera-ing Reactorc Or. nch #.7 Divisic.n of Oper st'ng Recctors
..e me