ML20086J213: Difference between revisions

From kanterella
Jump to navigation Jump to search
StriderTol Bot insert
 
StriderTol Bot change
 
Line 18: Line 18:
=Text=
=Text=
{{#Wiki_filter:E
{{#Wiki_filter:E
                                                                                                                                                    ]
]
o                                                                           p 4   ..
o pO 4
O PHILADELPHIA ELECTRIC COMPANY 2301 MARKET STREET PHILADELPHIA, PA.19101                                                                 ' -'                    '
PHILADELPHIA ELECTRIC COMPANY 2301 MARKET STREET PHILADELPHIA, PA.19101 1 ~
i 1~ .
i i
i azisi e 41-4ooo                             ";;, ;      '
azisi e 41-4ooo d;=,.
y November 29, 1974                   d;=,.
y November 29, 1974 Mr. A. Giambusso Deputy Director of Reactor Projects United States Atomic Energy Commission Directorate of Licensing Washington, DC 20545
Mr. A. Giambusso Deputy Director of Reactor Projects United States Atomic Energy Commission Directorate of Licensing Washington, DC     20545


==Dear Mr. Giambusso:==
==Dear Mr. Giambusso:==
==Subject:==
==Subject:==
Abnormal Occurrence The following occurrenca was reported to Mr. Walt Baunack, A.E.C. Region 1 Regulatory Operations Office on November 20, 1974.
Abnormal Occurrence The following occurrenca was reported to Mr. Walt Baunack, A.E.C. Region 1 Regulatory Operations Office on November 20, 1974.
Written notification was made to Mr. James P. O'Reilly, Region 1 Regulatory Operations Office on November 20, 1974. In accordance with Section 6.7 2.A of the Technical Specifications, Appendix A of DPR-56 for Unit 3 Peach Bottom Atomic Power Station, the following report is being submitted to the Directorate of Licensing as an Abnormal Occurrence.
Written notification was made to Mr. James P. O'Reilly, Region 1 Regulatory Operations Office on November 20, 1974.
In accordance with Section 6.7 2.A of the Technical Specifications, Appendix A of DPR-56 for Unit 3 Peach Bottom Atomic Power Station, the following report is being submitted to the Directorate of Licensing as an Abnormal Occurrence.


==Reference:==
==Reference:==
License Number DPR-56 Technical Specification Reference Table 4.2.B Repor t No.:                       50-278-74-25 Report Date:                       November 29, 1974 Occurrence Date: November 19, 1974 Facility:                         Peach Bottom Atomic Power Station R.D. 1, Delta, Pennsylvania Identification of Occurrence:
License Number DPR-56 Technical Specification Reference Table 4.2.B Repor t No.:
50-278-74-25 Report Date:
November 29, 1974 Occurrence Date: November 19, 1974 Facility:
Peach Bottom Atomic Power Station R.D. 1, Delta, Pennsylvania Identification of Occurrence:
Failure of a torus high water level switch LS-3-23-91A to operate. This switch cperates to transfer the HPCI suction from the condensate storage tank to the suppression pool.
Failure of a torus high water level switch LS-3-23-91A to operate. This switch cperates to transfer the HPCI suction from the condensate storage tank to the suppression pool.
Conditions Prior to Occurrence:
Conditions Prior to Occurrence:
Unit 3 at greater than 90% power.
Unit 3 at greater than 90% power.
Description of Occurrence:
Description of Occurrence:
During a routine instrument surveillance test, LS 23 - 91 A failed to operate.                                                                                                                 pl d7 j' e Designation of Apparent Cause of Occurrence:
During a routine instrument surveillance test, LS 23 - 91 A pl d7 j' failed to operate.
y d55-The switch assembly flapper arm was found - to interfere slighplyp..
e d55-y Designation of Apparent Cause of Occurrence:
with the switch case.                                                                                                       D- '           /V Q 1 $ $ o ! !o1 fo M e                                                                                           COPY SENT REGION M c=
The switch assembly flapper arm was found - to interfere slighplyp..
S                   PDR         _ _ _ - - - _ - - _ _ _ _ - _ - - _ _ _ _ _
with the switch case.
D- ' V/
Q 1 $ $ o ! ! 1 fo M e COPY SENT REGION M c=
o S
PDR


Mr. A. Giambusso         (
(
s -
(
(          .+..
Mr. A. Giambusso s
November 29, 1974                                                 Page 2 Analysis of Occurrence:
. +..
November 29, 1974 Page 2 Analysis of Occurrence:
LS-3-23-31A and LS-3-23-91B operate independently to transfer the HPCI suction from the condensate storage tank to the suppression pool. LS-3-23-918 had just been tested and found to function properly.
LS-3-23-31A and LS-3-23-91B operate independently to transfer the HPCI suction from the condensate storage tank to the suppression pool. LS-3-23-918 had just been tested and found to function properly.
Because the f ailure of LS-3-23-91A to operate would not have interfered with the' proper operation of the system, the safety implications are minimal.
Because the f ailure of LS-3-23-91A to operate would not have interfered with the' proper operation of the system, the safety implications are minimal.
Line 53: Line 60:
Failure Data:
Failure Data:
No previous failures on this type of switch.
No previous failures on this type of switch.
Very truly yours, I. 1   ,
Very truly yours, I. 1 j k(['.l' i -:i " ' c -
j k(['
Cooneyf MJ Ass't Gen'1 Superintendent
MJ .l' iCooneyf
' Generation Division cc:
                                                                -:i " ' c -
Mr. J. P. O'Reilly Director, Region 1 United _ States Atomic Energy Commission 631 Park Avenue King of Prussia, PA 19406 l-I l
Ass't Gen'1 Superintendent
                                                    ' Generation Division cc:   Mr. J. P. O'Reilly Director, Region 1 United _ States Atomic Energy Commission 631 Park Avenue King of Prussia, PA     19406 l-I l
l l
l l
h d2 ~
h d2 ~
u}}
u}}

Latest revision as of 02:01, 14 December 2024

AO 74-25:on 741119,torus High Water Level Switch LS-3-23-91A Failed to Operate.Caused by Switch Assembly Flapper Arm Interfering Slightly W/Switch Case.Switch Readjusted
ML20086J213
Person / Time
Site: Peach Bottom 
Issue date: 11/29/1974
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Anthony Giambusso
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20086J217 List:
References
AO-74-25, NUDOCS 8401230321
Download: ML20086J213 (2)


Text

E

]

o pO 4

PHILADELPHIA ELECTRIC COMPANY 2301 MARKET STREET PHILADELPHIA, PA.19101 1 ~

i i

azisi e 41-4ooo d;=,.

y November 29, 1974 Mr. A. Giambusso Deputy Director of Reactor Projects United States Atomic Energy Commission Directorate of Licensing Washington, DC 20545

Dear Mr. Giambusso:

Subject:

Abnormal Occurrence The following occurrenca was reported to Mr. Walt Baunack, A.E.C. Region 1 Regulatory Operations Office on November 20, 1974.

Written notification was made to Mr. James P. O'Reilly, Region 1 Regulatory Operations Office on November 20, 1974.

In accordance with Section 6.7 2.A of the Technical Specifications, Appendix A of DPR-56 for Unit 3 Peach Bottom Atomic Power Station, the following report is being submitted to the Directorate of Licensing as an Abnormal Occurrence.

Reference:

License Number DPR-56 Technical Specification Reference Table 4.2.B Repor t No.:

50-278-74-25 Report Date:

November 29, 1974 Occurrence Date: November 19, 1974 Facility:

Peach Bottom Atomic Power Station R.D. 1, Delta, Pennsylvania Identification of Occurrence:

Failure of a torus high water level switch LS-3-23-91A to operate. This switch cperates to transfer the HPCI suction from the condensate storage tank to the suppression pool.

Conditions Prior to Occurrence:

Unit 3 at greater than 90% power.

Description of Occurrence:

During a routine instrument surveillance test, LS 23 - 91 A pl d7 j' failed to operate.

e d55-y Designation of Apparent Cause of Occurrence:

The switch assembly flapper arm was found - to interfere slighplyp..

with the switch case.

D- ' V/

Q 1 $ $ o ! ! 1 fo M e COPY SENT REGION M c=

o S

PDR

(

(

Mr. A. Giambusso s

. +..

November 29, 1974 Page 2 Analysis of Occurrence:

LS-3-23-31A and LS-3-23-91B operate independently to transfer the HPCI suction from the condensate storage tank to the suppression pool. LS-3-23-918 had just been tested and found to function properly.

Because the f ailure of LS-3-23-91A to operate would not have interfered with the' proper operation of the system, the safety implications are minimal.

Corrective Action:

The switch was reacjusted to allow proper operation of the switch. The switch was cycled a number of times using water to lif t the float to ensure reliable operation. and then rechecked using the appro-priate instrument surveillance test.

Failure Data:

No previous failures on this type of switch.

Very truly yours, I. 1 j k(['.l' i -:i " ' c -

Cooneyf MJ Ass't Gen'1 Superintendent

' Generation Division cc:

Mr. J. P. O'Reilly Director, Region 1 United _ States Atomic Energy Commission 631 Park Avenue King of Prussia, PA 19406 l-I l

l l

h d2 ~

u