ENS 41066: Difference between revisions

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| event date = 09/24/2004 11:55 EDT
| event date = 09/24/2004 11:55 EDT
| last update date = 09/24/2004
| last update date = 09/24/2004
| title = Manual Reactor Trip With No Complications Due To Lowering  Steam Generator Water Level
| title = Manual Reactor Trip with No Complications Due to Lowering  Steam Generator Water Level
| event text = On September 24, 2004, at 11:53 hours, operations noticed the 23 Main Feedwater (FW) regulating valve operating erratically and FW flow and 23 Steam Generator (SG) level decreasing.  At 11:55 hours operations initiated a manual trip of the reactor based on the degrading condition with FW flow and SG level.  All control rods fully inserted and safety equipment operated as expected.  Auxiliary Feedwater started as expected, the Emergency Diesel Generators did not start as offsite power remained available.  The plant is in Hot (Standby) at Normal Temperature and Pressure and there was no radiation releases.  The condition is under investigation and a post trip review is being conducted."  State was notified of this event by the licensee.
| event text = On September 24, 2004, at 11:53 hours, operations noticed the 23 Main Feedwater (FW) regulating valve operating erratically and FW flow and 23 Steam Generator (SG) level decreasing.  At 11:55 hours operations initiated a manual trip of the reactor based on the degrading condition with FW flow and SG level.  All control rods fully inserted and safety equipment operated as expected.  Auxiliary Feedwater started as expected, the Emergency Diesel Generators did not start as offsite power remained available.  The plant is in Hot (Standby) at Normal Temperature and Pressure and there was no radiation releases.  The condition is under investigation and a post trip review is being conducted."  State was notified of this event by the licensee.
The NRC Resident Inspector was notified of this event by the licensee.
The NRC Resident Inspector was notified of this event by the licensee.

Latest revision as of 21:22, 1 March 2018

ENS 41066 +/-
Where
Indian Point Entergy icon.png
New York (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-2.43 h-0.101 days <br />-0.0145 weeks <br />-0.00333 months <br />)
Opened: Dan Lyon
13:29 Sep 24, 2004
NRC Officer: John Mackinnon
Last Updated: Sep 24, 2004
41066 - NRC Website
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