ENS 41583: Difference between revisions

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| event date = 04/09/2005 11:11 EDT
| event date = 04/09/2005 11:11 EDT
| last update date = 04/09/2005
| last update date = 04/09/2005
| title = Automatic Reactor Trip On Turbine Trip Due To Low Auto Stop Oil Pressure On Pressure Switches
| title = Automatic Reactor Trip on Turbine Trip Due to Low Auto Stop Oil Pressure on Pressure Switches
| event text = At 11:11 Unit 1 Turbine Tripped initiating Reactor Trip.  Initial Indications are Turbine Trip due to Lo Auto Stop Oil Pressure on 2 pressure switches.  Investigating Switch Actuations.
| event text = At 11:11 Unit 1 Turbine Tripped initiating Reactor Trip.  Initial Indications are Turbine Trip due to Lo Auto Stop Oil Pressure on 2 pressure switches.  Investigating Switch Actuations.
#2 and #4 S/G [Steam Generator] Atmospheric Relief Valves did not control properly and RxOp [Reactor Operator] closed valves with Control Switch.
#2 and #4 S/G [Steam Generator] Atmospheric Relief Valves did not control properly and RxOp [Reactor Operator] closed valves with Control Switch.

Latest revision as of 21:21, 1 March 2018

ENS 41583 +/-
Where
Sequoyah Tennessee Valley Authority icon.png
Tennessee (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-1.85 h-0.0771 days <br />-0.011 weeks <br />-0.00253 months <br />)
Opened: Calvin Fields
13:20 Apr 9, 2005
NRC Officer: Wesley Held
Last Updated: Apr 9, 2005
41583 - NRC Website
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