ENS 42945: Difference between revisions

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| event date = 10/29/2006 15:20 CST
| event date = 10/29/2006 15:20 CST
| last update date = 10/29/2006
| last update date = 10/29/2006
| title = Manual Trip Due To Lowering Steam Generator Level
| title = Manual Trip Due to Lowering Steam Generator Level
| event text = Unit 2 was operating in Mode 1 at 80% power following refueling holding for stabilization xenon in preparation for incore - excore calibration.  An alarm condition for steam generator 2-03 indicating Steam - Feedwater flow mismatch was observed.  Manual control of the feed regulating valve was taken, but operators were unable to control feed flow while steam generator 2-03 level continued to decrease.  A manual reactor trip was initiated and the reactor was tripped.  Auxiliary feedwater automatically started on low-low level in steam generators.  All systems responded normally during and following the trip.  Unit 2 is being maintained in Mode 3 pending the event investigation.
| event text = Unit 2 was operating in Mode 1 at 80% power following refueling holding for stabilization xenon in preparation for incore - excore calibration.  An alarm condition for steam generator 2-03 indicating Steam - Feedwater flow mismatch was observed.  Manual control of the feed regulating valve was taken, but operators were unable to control feed flow while steam generator 2-03 level continued to decrease.  A manual reactor trip was initiated and the reactor was tripped.  Auxiliary feedwater automatically started on low-low level in steam generators.  All systems responded normally during and following the trip.  Unit 2 is being maintained in Mode 3 pending the event investigation.
All control rods fully inserted.  RCPs are in operation transferring decay heat to the steam generators.  The MSIV's are open with the steam generators discharging steam to the main condensers using the steam dumps.  AFW is maintaining steam generator water levels.  Unit 1 was not affected.   
All control rods fully inserted.  RCPs are in operation transferring decay heat to the steam generators.  The MSIV's are open with the steam generators discharging steam to the main condensers using the steam dumps.  AFW is maintaining steam generator water levels.  Unit 1 was not affected.   

Latest revision as of 22:17, 1 March 2018

ENS 42945 +/-
Where
Comanche Peak Luminant icon.png
Texas (NRC Region 4)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-3.3 h-0.138 days <br />-0.0196 weeks <br />-0.00452 months <br />)
Opened: Eugene Skelton
18:02 Oct 29, 2006
NRC Officer: Bill Gott
Last Updated: Oct 29, 2006
42945 - NRC Website
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