ML20127L226: Difference between revisions

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=Text=
=Text=
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                                                                        , eq q ;- *.._i ,- g, Muticclio, ti:mesota WM Septaber 15,1WS-Mr.. J'.. G. Ecppler, Director Regiom III Office of Inspecttm and Enforement' Unite:U States Nw1 car Reguistory Ccanissim-7B9 Rooswelt' Road' Glen Bilyn, Illinois- 60137.-
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Muticclio, ti:mesota WM Septaber 15,1WS-Mr.. J'.. G. Ecppler, Director Regiom III Office of Inspecttm and Enforement' Unite:U States Nw1 car Reguistory Ccanissim-7B9 Rooswelt' Road' Glen Bilyn, Illinois-60137.-


==Dear Mr. Keppler:==
==Dear Mr. Keppler:==
11NfImi.In Nik'*,1IAR QNERATING PLAhTF Docket No.. 50-263 License No.. DPR-22"                                     i Written correspendence witE your office an. January 16L 1975, discusses.                           l reportire of refueling outagc valve leabgo prohlansi As discussed:in that correspondence, penetration.and isointion valwleabge rates which-cxceed the acceptance crittria outlined in Section,4.7.K.2.f of the Technical: Specifications will be reported within 24' hcurs by telephcae.
11NfImi.In Nik'*,1IAR QNERATING PLAhTF Docket No.. 50-263 License No.. DPR-22" i
and: telegrcph to the'Directac, Regi<n III, Office of Inspection and Enfomcmcnt with.a carbca-copy to the. Director,. Div.ision- of Reactor:
Written correspendence witE your office an. January 16L 1975, discusses.
Licensing. A? Licensee Event Rcqxrrt will be sutnittedi to-the Director,..
l reportire of refueling outagc valve leabgo prohlansi As discussed:in that correspondence, penetration.and isointion valwleabge rates which-cxceed the acceptance crittria outlined in Section,4.7.K.2.f of the Technical: Specifications will be reported within 24' hcurs by telephcae.
and: telegrcph to the'Directac, Regi<n III, Office of Inspection and Enfomcmcnt with.a carbca-copy to the. Director,. Div.ision-of Reactor:
Licensing.
A? Licensee Event Rcqxrrt will be sutnittedi to-the Director,..
Divisi(n of. Reactor Licensisg within 10! days following repair of all-leaking valves..
Divisi(n of. Reactor Licensisg within 10! days following repair of all-leaking valves..
In accordance with these reporting requironents,. notification.is hereby.;
In accordance with these reporting requironents,. notification.is hereby.;
inaic that the foricwing. valves were founi' to.lcak in; excess of the-acceptance criteria for local leak tests specifitxi in Secticm.4'.72.2.f of the Technical Specifications:
inaic that the foricwing. valves were founi' to.lcak in; excess of the-acceptance criteria for local leak tests specifitxi in Secticm.4'.72.2.f of the Technical Specifications:
Core Spray Testchie Check Valve ,, A0'14-13A Core Spray Testable Check Valvo, A0;14-1310 Mtin Stems Drain Isointion Valve, FD 237.3-
Core Spray Testchie Check Valve, A0'14-13A Core Spray Testable Check Valvo, A0;14-1310 Mtin Stems Drain Isointion Valve, FD 237.3-10UI Exhaust Line Check. Valve, HPCI-9:
  '-                      10UI Exhaust Line Check. Valve, HPCI-9:
gaM The. total' testable penetntion and'isointicn valve Icakage rate acceptance criteria-specified; by Tecinical. Specification 4'.7 A.2.f.(2)(a). was exceeded
g a
&o 88 when the leabge through Core Spray Testablo Check Valve >D 14-133.was;
M              The. total' testable penetntion and'isointicn valve Icakage rate acceptance
+0 found to be 153.0<SCFH.,
    &o              criteria- specified; by Tecinical. Specification 4'.7 A.2.f.(2)(a). was exceeded 88             when the leabge through Core Spray Testablo Check Valve >D 14-133.was;
-:e
  +0               found to be 153.0<SCFH.,                                                                     .
$g Yours very t y,,
    -:e
~
    $g             Yours very t       y,,
SS
                                                                                                            ~
'M C..E..Lar
SS                               'M
*8 Plant Mmager g"
      -              C..E..Lar
bbaticello Nuclear Generating Pinnt CEL/mma cc:: R S Boyd,.G.Chamoff, Minnesota Polluticn Contr :3 Agency. Pile aten.
      *8 g"             Plant Mmager                                                            '
p a-p m i.m.
bbaticello Nuclear Generating Pinnt CEL/mma cc:: R S Boyd,.G.Chamoff, Minnesota Polluticn Contr :3 Agency . Pile p a- p m i.m .
-}}
aten.}}

Latest revision as of 16:59, 12 December 2024

Informs That Listed Valves Found to Leak in Excess of Acceptance Criteria for Local Leak Tests Specified in TS
ML20127L226
Person / Time
Site: Monticello 
Issue date: 09/15/1975
From: Larson C
NORTHERN STATES POWER CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
NUDOCS 9211230461
Download: ML20127L226 (1)


Text

L

.; c ::.~,

, r n u

~,~ r. 7 z :;
r. v v: :r. n c o.t. W et.n t'

,7,

, eq q ;- *.._i,- g, 1

Muticclio, ti:mesota WM Septaber 15,1WS-Mr.. J'.. G. Ecppler, Director Regiom III Office of Inspecttm and Enforement' Unite:U States Nw1 car Reguistory Ccanissim-7B9 Rooswelt' Road' Glen Bilyn, Illinois-60137.-

Dear Mr. Keppler:

11NfImi.In Nik'*,1IAR QNERATING PLAhTF Docket No.. 50-263 License No.. DPR-22" i

Written correspendence witE your office an. January 16L 1975, discusses.

l reportire of refueling outagc valve leabgo prohlansi As discussed:in that correspondence, penetration.and isointion valwleabge rates which-cxceed the acceptance crittria outlined in Section,4.7.K.2.f of the Technical: Specifications will be reported within 24' hcurs by telephcae.

and: telegrcph to the'Directac, Regi<n III, Office of Inspection and Enfomcmcnt with.a carbca-copy to the. Director,. Div.ision-of Reactor:

Licensing.

A? Licensee Event Rcqxrrt will be sutnittedi to-the Director,..

Divisi(n of. Reactor Licensisg within 10! days following repair of all-leaking valves..

In accordance with these reporting requironents,. notification.is hereby.;

inaic that the foricwing. valves were founi' to.lcak in; excess of the-acceptance criteria for local leak tests specifitxi in Secticm.4'.72.2.f of the Technical Specifications:

Core Spray Testchie Check Valve, A0'14-13A Core Spray Testable Check Valvo, A0;14-1310 Mtin Stems Drain Isointion Valve, FD 237.3-10UI Exhaust Line Check. Valve, HPCI-9:

gaM The. total' testable penetntion and'isointicn valve Icakage rate acceptance criteria-specified; by Tecinical. Specification 4'.7 A.2.f.(2)(a). was exceeded

&o 88 when the leabge through Core Spray Testablo Check Valve >D 14-133.was;

+0 found to be 153.0<SCFH.,

-:e

$g Yours very t y,,

~

SS

'M C..E..Lar

  • 8 Plant Mmager g"

bbaticello Nuclear Generating Pinnt CEL/mma cc:: R S Boyd,.G.Chamoff, Minnesota Polluticn Contr :3 Agency. Pile aten.

p a-p m i.m.

-