ENS 45833: Difference between revisions

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| event date = 04/12/2010 07:21 CDT
| event date = 04/12/2010 07:21 CDT
| last update date = 04/12/2010
| last update date = 04/12/2010
| title = Actuation Of Blackout Sequencers Due To Loss Of One Offsite Power Source
| title = Actuation of Blackout Sequencers Due to Loss of One Offsite Power Source
| event text = At 0721 [CDT] on 4/12/10 the Comanche Peak Nuclear Power Plant experienced a loss of 138 KV transformer XST1 due to a failed transmission line insulator.  Unit 1 is currently defueled per 1RF14 refueling outage schedule.  Unit 2 was subjected to actuation of both blackout sequencers causing an automatic start of both motor driven Aux Feedwater  (AFW) pumps as well as the turbine driven AFW pump.
| event text = At 0721 [CDT] on 4/12/10 the Comanche Peak Nuclear Power Plant experienced a loss of 138 KV transformer XST1 due to a failed transmission line insulator.  Unit 1 is currently defueled per 1RF14 refueling outage schedule.  Unit 2 was subjected to actuation of both blackout sequencers causing an automatic start of both motor driven Aux Feedwater  (AFW) pumps as well as the turbine driven AFW pump.
No emergency diesel generator started as per design.
No emergency diesel generator started as per design.

Latest revision as of 22:09, 1 March 2018

ENS 45833 +/-
Where
Comanche Peak Luminant icon.png
Texas (NRC Region 4)
Reporting
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-2.35 h-0.0979 days <br />-0.014 weeks <br />-0.00322 months <br />)
Opened: Pat Minahan
10:00 Apr 12, 2010
NRC Officer: Bill Huffman
Last Updated: Apr 12, 2010
45833 - NRC Website
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