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SCHOOL OF                     '
1 SCHOOL OF NUCLEAR ENGINEERING i
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i                                   Purdue University               ;
i Purdue University West Lafayette, Indiana 47907 l
West Lafayette, Indiana 47907 l
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4 4                                  REPORT ON REACTOR OPERATIONS 1
4 REPORT ON REACTOR OPERATIONS 4
;                              it For the Period
1 it For the Period January 1,1991 to December 31,1991 PURDUE UNIVERSITY REACTOR-1
;                                    January 1,1991 to December 31,1991 l
)
PURDUE UNIVERSITY REACTOR-1                                             )
PURDUE UNIVERSITY j
PURDUE UNIVERSITY                                                 l j                                       West Lafayette, Indiana 47907 1
West Lafayette, Indiana 47907 1
l                                                   June,1992 4
l June,1992 4
j                                               Prepared by
j Prepared by F. M. Clikeman Laboratory Director and Reactor Supervisor 1
:'              F. M. Clikeman Laboratory Director and Reactor Supervisor 1
 
: 1. INTRODUCTION s.
1.
This report is submitted to meet the requirements set forth in 10 CFR 50.59 and the         ,
INTRODUCTION s.
technical specifications of the Purdue University Reactor (PUR-1) for the period January     l 1,1991 to December 31,1991.
This report is submitted to meet the requirements set forth in 10 CFR 50.59 and the technical specifications of the Purdue University Reactor (PUR-1) for the period January 1,1991 to December 31,1991.
During the reporting period of 1991 a total of 548 persons visited the reactor facility. l
During the reporting period of 1991 a total of 548 persons visited the reactor facility.
;            Those persons included 130 different groups, of which 77 groups were for the purpose of maintenance or surveillance testing,11 groups were for class purposes, 28 groups wem pre-scheduled tours,5 groups were participants in our reactor sharing program and 9 were miscellaneous groups.
Those persons included 130 different groups, of which 77 groups were for the purpose of maintenance or surveillance testing,11 groups were for class purposes, 28 groups wem pre-scheduled tours,5 groups were participants in our reactor sharing program and 9 were miscellaneous groups.
: 2. PLANT DESIGN AND OPERATIONAL CHANGES 3
2.
2.1   Facility Design Changes e
PLANT DESIGN AND OPERATIONAL CHANGES 3
2.1 Facility Design Changes e
There were no design changes to the facility in 1991.
There were no design changes to the facility in 1991.
2.2   Performance Characteristics The operadon of the PUR-1 facility continued satisfactorily during the reporting period. During the visualinspection of the surfaces of two representative fuel plates no changes were identified. This inspection included any defects that might compromise the integrity of the cladding including any evidence of corrosion.
2.2 Performance Characteristics The operadon of the PUR-1 facility continued satisfactorily during the reporting period. During the visualinspection of the surfaces of two representative fuel plates no changes were identified. This inspection included any defects that might compromise the integrity of the cladding including any evidence of corrosion.
Satisfactory preformance of the fuel continued during the year.
Satisfactory preformance of the fuel continued during the year.
2.3   Changes in Operating Procedures Concerning Safety of Facility Operations             l No changes in the operating procedures of the facility were made during 1991 although several operating procedums were rewritten and approved by CORO.             1 2.4   Results of Surveillance Tests and Inspections 2.4.1 Reactivity Limits The reactivity worths of the control rods were determined to be as follows:
2.3 Changes in Operating Procedures Concerning Safety of Facility Operations No changes in the operating procedures of the facility were made during 1991 although several operating procedums were rewritten and approved by CORO.
1 2.4 Results of Surveillance Tests and Inspections 2.4.1 Reactivity Limits The reactivity worths of the control rods were determined to be as follows:
Shim-safety #1 - 5.00%
Shim-safety #1 - 5.00%
Shim-safety #2 - 2.65%
Shim-safety #2 - 2.65%
    .                                                    Regulating Rod - 0.25%
Regulating Rod - 0.25%
The worth curves of the control rods were checked after the inspection and the excess was detennined to be 0.44%. The shutdown margin was determined to
The worth curves of the control rods were checked after the inspection and the excess was detennined to be 0.44%. The shutdown margin was determined to


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:                                                                                                                      2       i l
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L                                           be 7.46% based on these values.                                                   1 J'..                                                                                                                         ,
{,.
The inspection of the control rods was completed on July 17,1991 with no         i g                                           evidence of change or deterioration observed.
a.
No experiment was placed in the reactor pool during the year that would           !
L be 7.46% based on these values.
:                                            require the determination ofits reactivity during the initial criticality       -l following its installation.
1 J'..
The inspection of the control rods was completed on July 17,1991 with no i
g evidence of change or deterioration observed.
No experiment was placed in the reactor pool during the year that would require the determination ofits reactivity during the initial criticality
-l following its installation.
2.4.2 Reactor Safety Syste'ms 1
2.4.2 Reactor Safety Syste'ms 1
:                                            Each prestartup check included a channel test for each safety system, provided the shutdown exceed 8 hours or if the system was repaired or de-
Each prestartup check included a channel test for each safety system, provided the shutdown exceed 8 hours or if the system was repaired or de-
[                                           energized.
[
energized.
a i
a i
Each reactor safety system had a channel check performed at time intervals of       ,
Each reactor safety system had a channel check performed at time intervals of less than'4 hours during operation.
a                                            less than'4 hours during operation.
a
(;
(
1       '
1 On October 22,1991 the electronic calibration of all safety channels was j
  ...                                      On October 22,1991 the electronic calibration of all safety channels was           j
completed.
!                                            completed.                                                                         l t
l t
i l*                                           The isradiation of gold foils for a power calibration was done on December I
i l*
i                                            19,1991. No significant change was identified from this irradiation.             ,
I The isradiation of gold foils for a power calibration was done on December i
:                                            During the prestartup which precedes each run, the radiation area momtors         ]
19,1991. No significant change was identified from this irradiation.
3 and the continuous air monitor were checked for normal operation. During           j 1991 the calibration of the radiation ama monitors and the continuous air     .]
During the prestartup which precedes each run, the radiation area momtors
monitor was completed on March 26 and September 13.-                               1 Following the control rod inspections, the rod drop times were measured on         I July 17,1991. The rod drop times fell between 607 and 667 milliseconds.
]
These values are consistent with past measuremen's and are well within the         j specification limits of I second.
3 and the continuous air monitor were checked for normal operation. During j
2.4.3 Primary Coolant System The weekly measurements of the pH of the primary coolant fell between 5.0
1991 the calibration of the radiation ama monitors and the continuous air
      .                                      and 6.5 during 1991. These value are within the specification limits of 5.5 +_
.]
l.0. In February, a new procedure for measuring pH in low conductivity
monitor was completed on March 26 and September 13.-
    ..                                      water was introduced and now yields much mom consistent readings.
Following the control rod inspections, the rod drop times were measured on I
I l
July 17,1991. The rod drop times fell between 607 and 667 milliseconds.
l i
These values are consistent with past measuremen's and are well within the j
specification limits of I second.
2.4.3 Primary Coolant System The weekly measurements of the pH of the primary coolant fell between 5.0 and 6.5 during 1991. These value are within the specification limits of 5.5 +_
l.0. In February, a new procedure for measuring pH in low conductivity water was introduced and now yields much mom consistent readings.
l l
i


i                                                                                                                     !
i I
I 3
3 During the prestartup check, which proceeds each run, the conductivity of the 4
l During the prestartup check, which proceeds each run, the conductivity of the     4
primary coolant was measumd and the values never exceeded 1.40 l
!*                                  primary coolant was measumd and the values never exceeded 1.40                   l
micrombos-cm. This represents a resistivity of more than 714,000 ohm /cm which exceeds the lower limit of 330,000 ohm /cm as given in the l
!                                  micrombos-cm. This represents a resistivity of more than 714,000 ohm /cm which exceeds the lower limit of 330,000 ohm /cm as given in the                 !
specifications.
specifications.
l i
i The specification of 13 feet of water was always either met or exceeded, according to the prestarted check list that was completed prior to each reactor run.
The specification of 13 feet of water was always either met or exceeded,         ;
I Monthly samples of the primary coolant was collected and analyzed by personnel from Radiological and Environmental Management for gross alpha and beta activity. No activity was identified in the samples which would indicate failum of the fuel plates.
according to the prestarted check list that was completed prior to each reactor   ,
l 2.4.4.. Containment -
run.                                                                             !
I Monthly samples of the primary coolant was collected and analyzed by personnel from Radiological and Environmental Management for gross alpha         !
and beta activity. No activity was identified in the samples which would           ,
indicate failum of the fuel plates.                                               l 2.4.4.. Containment -
Readings between 0.080 and 0.180 inches of water were recorded weekly for the negative pressure in the reactor room.
Readings between 0.080 and 0.180 inches of water were recorded weekly for the negative pressure in the reactor room.
l The semi-annual checks made in 1991 for the proper operation of the inlet         !
The semi-annual checks made in 1991 for the proper operation of the inlet and outlet dampers and the air conditioner were completed on May and October 1991. All worked satisfactorily.
and outlet dampers and the air conditioner were completed on May and             !
i Selected fuel plates were visually inspected on July 24,1991. The surface condition of fuel plate #4-3-73 indicated no change from the last inspection, I
October 1991. All worked satisfactorily.                                         i Selected fuel plates were visually inspected on July 24,1991. The surface condition of fuel plate #4-3-73 indicated no change from the last inspection,     I and the cladding of the other inspected plates identified no changes.
and the cladding of the other inspected plates identified no changes.
2.4.5 Experiments The mass of the singly encapsulated samples and the flux of the reactor are       ]'
2.4.5 Experiments The mass of the singly encapsulated samples and the flux of the reactor are
]
such that the complete release of all gaseous, particulate, and volatile components of the samples would not result in doses in excess of 10% of the equivalent annual doses as stated in 10 CFR 20.
such that the complete release of all gaseous, particulate, and volatile components of the samples would not result in doses in excess of 10% of the equivalent annual doses as stated in 10 CFR 20.
No samples of unknown composition or that required double encapsulation           ,
No samples of unknown composition or that required double encapsulation J
J wire submitted for irradiation.
wire submitted for irradiation.
2.5         Changes, Tests and Experiments Requiring Commission Authorization During 1991 no changes, or experiments which required authorization from the l
2.5 Changes, Tests and Experiments Requiring Commission Authorization During 1991 no changes, or experiments which required authorization from the l
Commission pursuant to 10 CFR 50.59 (a) were performed.
Commission pursuant to 10 CFR 50.59 (a) were performed.
l
l


l 4
l 4
l
I 2.6 Changes in Facility Staff On December 31,1990 Mr Eldon Stansberry retired from the University and as
.                                                                                                          I
)
'              2.6   Changes in Facility Staff l
reactor supervisor. He will continue to be on call and and will serve as a backup for j
On December 31,1990 Mr Eldon Stansberry retired from the University and as           )
F. Clikeman and E. Merritt j
reactor supervisor. He will continue to be on call and and will serve as a backup for j F. Clikeman and E. Merritt                                                           j
3.
: 3. POWER GENERATION 1
POWER GENERATION Operation of the PUR-1 during 1991 consisted of 14 runs which generated 130,420 watt-minutes of energy and covered an integrated running time of 67.9 hours.
Operation of the PUR-1 during 1991 consisted of 14 runs which generated 130,420 watt-minutes of energy and covered an integrated running time of 67.9 hours.                     !
l 4.
l
UNSCHEDULED SHUTDOWNS i
: 4. UNSCHEDULED SHUTDOWNS                                                                       i l
Three unscheduled shutdowns occurred during 1991. All of these shutdowns were associated with the log N channel with noise in the channel generating false period indications in CSA-2. Voltage checks and routine maintenance corrected these problems.
Three unscheduled shutdowns occurred during 1991. All of these shutdowns were
All of these unscheduled shutdowns were on the conservative side of safety and no unsafe condition existed at the time of shutdown.
                                                                                                            )
5.
associated with the log N channel with noise in the channel generating false period         l indications in CSA-2. Voltage checks and routine maintenance corrected these problems.       I All of these unscheduled shutdowns were on the conservative side of safety and no       )
MAINTENANCE Only routine maintenance was required during the reporting period.
unsafe condition existed at the time of shutdown.
6.
: 5. MAINTENANCE
CIIANGES, TESTS AND EXPERIMENTS No changes, tests or experiments were carried out without prior Commission approval pursuant to the requirements of 10 CFR 50.59 (b).
                                                                                                            )
7.
Only routine maintenance was required during the reporting period.
RADIOACTIVE EFFLUENT RELEASES No measurable amount of radioactive effluents were released to the environs beyond our effective control, as measured at or prior to the point of such release.
: 6. CIIANGES, TESTS AND EXPERIMENTS No changes, tests or experiments were carried out without prior Commission approval pursuant to the requirements of 10 CFR 50.59 (b).
: 7. RADIOACTIVE EFFLUENT RELEASES No measurable amount of radioactive effluents were released to the environs beyond our effective control, as measured at or prior to the point of such release.
e It}}
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Latest revision as of 09:21, 12 December 2024

Rept on Reactor Operations for Period Jan-Dec 1991
ML20132H117
Person / Time
Site: Purdue University
Issue date: 12/31/1991
From: Clikeman F
PURDUE UNIV., WEST LAFAYETTE, IN
To:
Shared Package
ML20132H016 List:
References
NUDOCS 9612270142
Download: ML20132H117 (6)


Text

..

T I

1 SCHOOL OF NUCLEAR ENGINEERING i

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J i

l l

1 i

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1 I

i i

i Purdue University West Lafayette, Indiana 47907 l

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i 9612270142 961212 i

PDR ADOCK 05000182 R

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1 4

4 REPORT ON REACTOR OPERATIONS 4

1 it For the Period January 1,1991 to December 31,1991 PURDUE UNIVERSITY REACTOR-1

)

PURDUE UNIVERSITY j

West Lafayette, Indiana 47907 1

l June,1992 4

j Prepared by F. M. Clikeman Laboratory Director and Reactor Supervisor 1

1.

INTRODUCTION s.

This report is submitted to meet the requirements set forth in 10 CFR 50.59 and the technical specifications of the Purdue University Reactor (PUR-1) for the period January 1,1991 to December 31,1991.

During the reporting period of 1991 a total of 548 persons visited the reactor facility.

Those persons included 130 different groups, of which 77 groups were for the purpose of maintenance or surveillance testing,11 groups were for class purposes, 28 groups wem pre-scheduled tours,5 groups were participants in our reactor sharing program and 9 were miscellaneous groups.

2.

PLANT DESIGN AND OPERATIONAL CHANGES 3

2.1 Facility Design Changes e

There were no design changes to the facility in 1991.

2.2 Performance Characteristics The operadon of the PUR-1 facility continued satisfactorily during the reporting period. During the visualinspection of the surfaces of two representative fuel plates no changes were identified. This inspection included any defects that might compromise the integrity of the cladding including any evidence of corrosion.

Satisfactory preformance of the fuel continued during the year.

2.3 Changes in Operating Procedures Concerning Safety of Facility Operations No changes in the operating procedures of the facility were made during 1991 although several operating procedums were rewritten and approved by CORO.

1 2.4 Results of Surveillance Tests and Inspections 2.4.1 Reactivity Limits The reactivity worths of the control rods were determined to be as follows:

Shim-safety #1 - 5.00%

Shim-safety #2 - 2.65%

Regulating Rod - 0.25%

The worth curves of the control rods were checked after the inspection and the excess was detennined to be 0.44%. The shutdown margin was determined to

[

l 2

i

{,.

a.

L be 7.46% based on these values.

1 J'..

The inspection of the control rods was completed on July 17,1991 with no i

g evidence of change or deterioration observed.

No experiment was placed in the reactor pool during the year that would require the determination ofits reactivity during the initial criticality

-l following its installation.

2.4.2 Reactor Safety Syste'ms 1

Each prestartup check included a channel test for each safety system, provided the shutdown exceed 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or if the system was repaired or de-

[

energized.

a i

Each reactor safety system had a channel check performed at time intervals of less than'4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> during operation.

a

(

1 On October 22,1991 the electronic calibration of all safety channels was j

completed.

l t

i l*

I The isradiation of gold foils for a power calibration was done on December i

19,1991. No significant change was identified from this irradiation.

During the prestartup which precedes each run, the radiation area momtors

]

3 and the continuous air monitor were checked for normal operation. During j

1991 the calibration of the radiation ama monitors and the continuous air

.]

monitor was completed on March 26 and September 13.-

Following the control rod inspections, the rod drop times were measured on I

July 17,1991. The rod drop times fell between 607 and 667 milliseconds.

These values are consistent with past measuremen's and are well within the j

specification limits of I second.

2.4.3 Primary Coolant System The weekly measurements of the pH of the primary coolant fell between 5.0 and 6.5 during 1991. These value are within the specification limits of 5.5 +_

l.0. In February, a new procedure for measuring pH in low conductivity water was introduced and now yields much mom consistent readings.

l l

i

i I

3 During the prestartup check, which proceeds each run, the conductivity of the 4

primary coolant was measumd and the values never exceeded 1.40 l

micrombos-cm. This represents a resistivity of more than 714,000 ohm /cm which exceeds the lower limit of 330,000 ohm /cm as given in the l

specifications.

i The specification of 13 feet of water was always either met or exceeded, according to the prestarted check list that was completed prior to each reactor run.

I Monthly samples of the primary coolant was collected and analyzed by personnel from Radiological and Environmental Management for gross alpha and beta activity. No activity was identified in the samples which would indicate failum of the fuel plates.

l 2.4.4.. Containment -

Readings between 0.080 and 0.180 inches of water were recorded weekly for the negative pressure in the reactor room.

The semi-annual checks made in 1991 for the proper operation of the inlet and outlet dampers and the air conditioner were completed on May and October 1991. All worked satisfactorily.

i Selected fuel plates were visually inspected on July 24,1991. The surface condition of fuel plate #4-3-73 indicated no change from the last inspection, I

and the cladding of the other inspected plates identified no changes.

2.4.5 Experiments The mass of the singly encapsulated samples and the flux of the reactor are

]

such that the complete release of all gaseous, particulate, and volatile components of the samples would not result in doses in excess of 10% of the equivalent annual doses as stated in 10 CFR 20.

No samples of unknown composition or that required double encapsulation J

wire submitted for irradiation.

2.5 Changes, Tests and Experiments Requiring Commission Authorization During 1991 no changes, or experiments which required authorization from the l

Commission pursuant to 10 CFR 50.59 (a) were performed.

l

l 4

I 2.6 Changes in Facility Staff On December 31,1990 Mr Eldon Stansberry retired from the University and as

)

reactor supervisor. He will continue to be on call and and will serve as a backup for j

F. Clikeman and E. Merritt j

3.

POWER GENERATION Operation of the PUR-1 during 1991 consisted of 14 runs which generated 130,420 watt-minutes of energy and covered an integrated running time of 67.9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br />.

l 4.

UNSCHEDULED SHUTDOWNS i

Three unscheduled shutdowns occurred during 1991. All of these shutdowns were associated with the log N channel with noise in the channel generating false period indications in CSA-2. Voltage checks and routine maintenance corrected these problems.

All of these unscheduled shutdowns were on the conservative side of safety and no unsafe condition existed at the time of shutdown.

5.

MAINTENANCE Only routine maintenance was required during the reporting period.

6.

CIIANGES, TESTS AND EXPERIMENTS No changes, tests or experiments were carried out without prior Commission approval pursuant to the requirements of 10 CFR 50.59 (b).

7.

RADIOACTIVE EFFLUENT RELEASES No measurable amount of radioactive effluents were released to the environs beyond our effective control, as measured at or prior to the point of such release.

e It