ENS 50314: Difference between revisions

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| event date = 07/27/2014 14:09 EDT
| event date = 07/27/2014 14:09 EDT
| last update date = 07/27/2014
| last update date = 07/27/2014
| title = Manual Reactor Trip Due To Loss Of Main Feed Pump During Testing
| title = Manual Reactor Trip Due to Loss of Main Feed Pump During Testing
| event text = VEGP [Vogtle Electric Generation Plant] Unit One was at 100 percent power, with a Main Feed Pump (MFP) Turbine A trip mechanism test in-progress, when MFP A Trip alarm was received in the Main Control Room.  Control Room crew identified MFP A speed and steam generator levels lowering and initiated a manual reactor trip.  All control rods fully inserted and nothing unusual was noted.  Auxiliary feed water and feedwater isolation actuated as expected.  The unit is currently stable in MODE 3 at normal operating temperature and pressure.  A forced outage response team has been formed to determine the cause of the MFP A trip and determine restart criteria and time of restart.
| event text = VEGP [Vogtle Electric Generation Plant] Unit One was at 100 percent power, with a Main Feed Pump (MFP) Turbine A trip mechanism test in-progress, when MFP A Trip alarm was received in the Main Control Room.  Control Room crew identified MFP A speed and steam generator levels lowering and initiated a manual reactor trip.  All control rods fully inserted and nothing unusual was noted.  Auxiliary feed water and feedwater isolation actuated as expected.  The unit is currently stable in MODE 3 at normal operating temperature and pressure.  A forced outage response team has been formed to determine the cause of the MFP A trip and determine restart criteria and time of restart.
The unit is in a normal shutdown electric plant lineup.  No effect on Unit 2.
The unit is in a normal shutdown electric plant lineup.  No effect on Unit 2.

Latest revision as of 21:50, 1 March 2018

ENS 50314 +/-
Where
Vogtle Southern Nuclear icon.png
Georgia (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-2.78 h-0.116 days <br />-0.0165 weeks <br />-0.00381 months <br />)
Opened: Dan Monahon
15:22 Jul 27, 2014
NRC Officer: Jeff Rotton
Last Updated: Jul 27, 2014
50314 - NRC Website
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