ENS 52791: Difference between revisions

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| event date = 06/06/2017 17:51 EDT
| event date = 06/06/2017 17:51 EDT
| last update date = 06/06/2017
| last update date = 06/06/2017
| title = Both Standby Steam Generator Feed Pumps Out Of Service For Pre-Planned Maintenance
| title = Both Standby Steam Generator Feed Pumps Out of Service for Pre-Planned Maintenance
| event text = This notification is in accordance with Turkey Point Technical Specification (TS) 3.7.1.6, Action b.1 to report the inoperability of both Standby Steam Generator Feedwater Pumps (SSGFPs) for greater than 24 hours.
| event text = This notification is in accordance with Turkey Point Technical Specification (TS) 3.7.1.6, Action b.1 to report the inoperability of both Standby Steam Generator Feedwater Pumps (SSGFPs) for greater than 24 hours.
On 6/6/17 at 1751 hours [EDT] both SSGFPs will be inoperable for greater than 24 hours in support of planned valve repairs that require isolation of the common suction and discharge piping. TS 3.7.1.6, Action b.1 requires a report within four hours if both SSGFPs have been inoperable for 24 hours providing the cause of the inoperability and restoration plans. The valve repairs are currently planned for completion on or about 2300 hours on 6/9/17 which will restore the 'A' pump to service and allow TS 3.7.1.6, Action b.1 to be exited. The diesel-driven 'B' pump will remain out of service for radiator repair which is currently planned for completion on or about 0800 hours on 6/14/17.
On 6/6/17 at 1751 hours [EDT] both SSGFPs will be inoperable for greater than 24 hours in support of planned valve repairs that require isolation of the common suction and discharge piping. TS 3.7.1.6, Action b.1 requires a report within four hours if both SSGFPs have been inoperable for 24 hours providing the cause of the inoperability and restoration plans. The valve repairs are currently planned for completion on or about 2300 hours on 6/9/17 which will restore the 'A' pump to service and allow TS 3.7.1.6, Action b.1 to be exited. The diesel-driven 'B' pump will remain out of service for radiator repair which is currently planned for completion on or about 0800 hours on 6/14/17.

Latest revision as of 21:42, 1 March 2018

ENS 52791 +/-
Where
Turkey Point NextEra Energy icon.png
Florida (NRC Region 2)
Reporting
Other Unspec Reqmnt
Time - Person (Reporting Time:+-6.05 h-0.252 days <br />-0.036 weeks <br />-0.00829 months <br />)
Opened: Thomas Wall
15:48 Jun 6, 2017
NRC Officer: Howie Crouch
Last Updated: Jun 6, 2017
52791 - NRC Website
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