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=Text= | =Text= | ||
{{#Wiki_filter: | {{#Wiki_filter:. | ||
NARRATIVE | NARRATIVE | ||
==SUMMARY== | ==SUMMARY== | ||
OF | OF MONTHLY OPERATING EXPERIENCE September 1985 i | ||
September 1 | September 1 The Unit entered the mcnth in Mode 5 as a result of a reactor trip / safety injection due to a | ||
September 2 | loss of instrument air which occurred on August 29, 1985. Plant heat up began on the 1st with the Unit entering Mode 4 at 1730 hours. | ||
September 3 | September 2 Plant heat-up continued with the Unit entering Mode 3 at 0108 hours. | ||
September 4 | September 3 Plant heat-up continued wi th reactor criticali ty achieved at 1247 hours and the Unit being synched to the grid at 1411 hours. | ||
September 5 | September 4 The Station operated at a reduced power level of approximately 57 percent as a result of maintenance being performed on feedwater pump [ FW-P-1A). | ||
September 6 | September 5 Repai rs to feedwater pump [ FW-P-1A] were completed at 1153 hours and power level was subsequently increased to a nominal 100 percent. | ||
September 16 | September 6 The Station was in Operational Mode 1 with reactor power through at a nominal 100 percent. | ||
September 17 | Reactor Coolant System was September 15 at a normal operating pressure and temperature. | ||
8512120118 DR | September 16 Inadve rtant grounding of Vital Bus #2 caused the Loop B OTAT and OPAT bistables to trip producing a reactor trip at 1026 hours. | ||
The reactor achieved criticality at 2203 hours and the Unit was synched to the grid at 2328 hours. | |||
September 17 The Station was in Operational Mode 1 with reactor through power at a nominal 100 percent. | |||
Reactor Coolant September 25 4 System was at normal operating pressure and temperature. | |||
8512120118 851003 DR ADOCK 05000334 PDR 1 | |||
September 1985 Summary of Monthly Operating Experience September 26 At 1023 hours the plant P250 computer began reading N42 and N43 approximately 20 percent low. This resulted in two channels calculating an erroneous targeta 0. | September 1985 Summary of Monthly Operating Experience September 26 At 1023 hours the plant P250 computer began reading N42 and N43 approximately 20 percent low. | ||
This resulted in two channels calculating an erroneous targeta 0. | |||
September 27 | At 1120 hours operators noticed the rod position indicators (RPI's) for control banks C and D reading 200 steps with the rods actually at 228 and 225 steps. At 1125 hours, the interaction between the plant variable computer and the plant P250 com t deenergized and both the operations were no$pu er was RPIs and the a monitor returned to normal. | ||
Plant t affected by this event. | |||
September 27 The Station was in Operational Mode I with reactor through power at a nominal 100 percent. | |||
Reactor Coolant System September 30 was at normal operating pressure and temperature. | |||
^ | ^ | ||
1 2 | 1 2 | ||
OPERATI G DATA REPORT DOCKET NO. 50-334 DATE 10/3/63 COMPLETED BY P. A. Smith | OPERATI G DATA REPORT DOCKET NO. 50-334 DATE 10/3/63 COMPLETED BY P. A. | ||
Smith TELEPHONE. 417-641-1825 OPERATING STATUS l | |||
I. Unit Name: Beaver Valley Power Station, Unit il | I. Unit Name: Beaver Valley Power Station, Unit il Notes September 1985 | ||
: 2. Reporting Period: | : 2. Reporting Period: | ||
: 3. t l===d Thermal Power (MWt): | : 3. t l===d Thermal Power (MWt): | ||
: 4. Nameplate Rating (Gross MWe): | 2W | ||
: 5. Design Electrial Rating (Net MWe): | : 4. Nameplate Rating (Gross MWe): | ||
: 6. Maximum Dependable Capacity (Gross MWe): | 923 835 | ||
: 7. Maximum Dependable Capacity (Net MWe): | : 5. Design Electrial Rating (Net MWe): | ||
: 6. Maximum Dependable Capacity (Gross MWe): | |||
860 | |||
: 7. Maximum Dependable Capacity (Net MWe): | |||
810 | |||
: 8. If Cheness Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: | : 8. If Cheness Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: | ||
e | e | ||
: 9. Power Level To Which Restricted.If Any (Net MWe): | : 9. Power Level To Which Restricted.If Any (Net MWe): | ||
: 10. Reasons For Restrictions,if Any: | None | ||
: 11. Hours In Reporting Period | : 10. Reasons For Restrictions,if Any: | ||
: 12. Number Of Hours Reactor Was Caitical | N/A This MontJi Yr. tete | ||
: 13. Reactor Reserve Shutdown Hours | ' Cumulative | ||
: 14. Hours Generator On-Line | : 11. Hours In Reporting Period 720.0 6',551.0 82,559.0 | ||
: 15. Unit Reserve Shutdown Hours | : 12. Number Of Hours Reactor Was Caitical 647.6 6,062.2 43,417.9 | ||
: 16. Gross Thermal Energy Generated (MWH) | : 13. Reactor Reserve Shutdown Hours 0.0 0.0 4.482.8 | ||
: 17. Gross Electrical Energy Generated (MWH) | : 14. Hours Generator On-Line 644.8 5.915.0 41.997.9 | ||
: 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0 | |||
: 18. Net Electrical Energy Generated (MWH) | : 16. Gross Thermal Energy Generated (MWH) 1.627.823.0 14,513,009.9 97,911,523.9 | ||
: 19. Unit Service Factor | : 17. Gross Electrical Energy Generated (MWH) 517,000.0 4,657,000.0 31,151,400.0 | ||
: 20. Unit Availability Factor | ~ | ||
: 21. Unit Capacity Factor (Using MDC Neti | : 18. Net Electrical Energy Generated (MWH) 485.300.0 4.366.550.0 28,991,393.0 | ||
: 22. Unit Capacity Factor iUsing DER Net) | : 19. Unit Service Factor 89.6 90.3 53.3 | ||
: 23. Unit Forced Outage Rate | : 20. Unit Availability Factor 89.6 90.3 53.3 | ||
: 21. Unit Capacity Factor (Using MDC Neti 83.2 82.3 46.9 | |||
: 22. Unit Capacity Factor iUsing DER Net) 80.7 79,8 45.5 | |||
: 23. Unit Forced Outage Rate 10.4 g,5 24.8 | |||
: 24. Shutdowns Scheduled Over Next 6 Months ! Type.Dete.snd Duration of Eacht: | : 24. Shutdowns Scheduled Over Next 6 Months ! Type.Dete.snd Duration of Eacht: | ||
: 25. If Shut Down At End Of Report Period. Estimated Date of Startup: | : 25. If Shut Down At End Of Report Period. Estimated Date of Startup: | ||
: 26. Units in Test Status (Priur to Commercial Operationi: | : 26. Units in Test Status (Priur to Commercial Operationi: | ||
Forecast Achieved INITIA L CRITICALITY N/A N/A INITIA L ELECTRICITY N/A_ | |||
N/A COMMERCIAL OPERATION N/A N/A 4 | |||
<,,77) | |||
\\\\ | |||
1 | |||
t MAJOR MAINTENANCE | t MAJOR MAINTENANCE 1. | ||
Maintenance of Feedwater Pump [FW-P-1 A]. | |||
2. | |||
Repaired Main Steam Trip Valves [TV-MS-101B] and [TV-MS-101C]. | |||
3. | |||
Maintenance of Station Air Compressor [SA-C-1A] and [S A-C-1B]. | |||
4. | |||
Inspected and repaired Steam Driven Auxiliary Feedwater Pump [FW-P-2]. | |||
4 a | 4 a | ||
t i | t i | ||
I | I r | ||
I e | |||
e | + - | ||
..m,, | |||
-+y-v-w:.1 v- | |||
=, | |||
---w-- | |||
---er-- | |||
+ | |||
-v- | |||
AVERAGE DAll UNIT POWER LEVEL. | |||
t DOCKET NO. | |||
DOCKET NO. | 50~334 UNIT 3V?S U::1: 41 10/3/85 DATE P.A. Smith COMPLETED BY TELEPHONE (412) 643-1825 SEPTEMBER Mom DAY AVERACE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) | ||
(MWe-Net) 0 g | |||
37 667 0 | |||
788 2 | |||
18 l | |||
22 7 | 3 135 827 39 784 20 582 784 23 783 6 | ||
g | 785 7 | ||
22 7 | |||
28 789 | 785 784 73 4 | ||
783 g | |||
On this format. fist the average d:ily unit power le.c!!n MWe. Net Or esch day in the reputtine month. Compute to the ne: rest whole mepwatt. | 24 786 785 25 789 9 | ||
742 10 26 788 II 827 829 27 747 j | |||
12 28 789 13 788 39 1 | |||
i-14 790 787 30 15 789 31 i | |||
.339 t | |||
16 INSTRUCTIONS On this format. fist the average d:ily unit power le.c!!n MWe. Net Or esch day in the reputtine month. Compute to t | |||
the ne: rest whole mepwatt. | |||
I 19/77 ) | I 19/77 ) | ||
. _ _., _ - ~.. | |||
UNITSHUTDOWNS ANDPOWER REDUCTIONS | UNITSHUTDOWNS ANDPOWER REDUCTIONS DOCKET NO. | ||
0 | 50-334 UNIT NAME BVPS Unit #1 DATE 10/3/85 REPORT MONIH SEPTEMBER COMPLETED BY P. A. | ||
* N | Smith TELEPilONE (412) 643-1825 "u | ||
en | |||
*#o 0 | |||
30 | * N C.0 t Licensee Cause, & Corrective g | ||
,a e | |||
No. | |||
Date | |||
%5 3UE Event | |||
!e Action to | |||
# e R | |||
"5 l | |||
5,E " | |||
Report # | |||
$3 eo Prevent Recurrence H | |||
E M | |||
y*y NU O | |||
8 30 850901 F | |||
62.2 A | |||
4 85-015 PA AIRDRY The Station remained off line follow-ing a reactor trip / safety injection due to a loss of instrument air caused by a broken line on the instrument air dryer. | |||
Repairs were made and the Station returned to service at 1411 hours on the 3rd. | Repairs were made and the Station returned to service at 1411 hours on the 3rd. | ||
31 | 31 850903 F | ||
(CONTINUED) 1 | 0 B | ||
A-Eiguipment Failure (Emplain) | 5 N/A CH PUMPXX The Station was operating at s' reduced power level as a result of maintenance being performed on feedwater pump [FW-P-1A]. | ||
G Operatiimal I s eios 11 aplaml | (CONTINUED) 1 2 | ||
3 4 | |||
F: F used Reasam: | |||
Hethod: | |||
1.mlubit G. Insisus siims S Schedueil A-Eiguipment Failure (Emplain) 1-Manual fin Psepasasi.m os Dana 8 | |||
B. Maintenance of Test 2-Manual scree I nis) Sheels l'w I kernce C Refuelint 3-Automatic Scram F$cn' Relant 81 l'RII de INllRI G D-Regulatoey Restricii.* | |||
4-Continued From Frevious Month Ultill I Openalais Tsaining A license Examinati"'' | |||
5-Ite<'uc tion I: Adnunistrative 9-Other 5 | |||
G Operatiimal I s eios 11 aplaml I sinhis I Same S. misc 08/77) | |||
II OtherflN plaiul | |||
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. | |||
oa | 50-334 UNIT NAME BVPS Unit il DATE - 10/3/85 REPORT MONIH SEPTEMBER COMPLETED BY P. | ||
A. | |||
Smith TELErtlONE (412) 643-1825 S | |||
cn | |||
% MO oa 0." t Licensee | |||
$#5 Cause, & Corrective a | |||
31 | No. | ||
Date 0 | |||
'E t', E Event f4 Action to R | |||
"5 5 | |||
5.E " | |||
Report # | |||
e o ao Prevent Recurrence H | |||
S M | |||
y*g NU O | |||
e 31 (CONTINUED) | |||
Repairs to feedwater pump [FW-P-1A] | |||
completed at 1153 hours on the 5th and power level was subsequently increased. | completed at 1153 hours on the 5th and power level was subsequently increased. | ||
32 | 32 850916 F | ||
13.0 A | |||
3 85-016 EG ZZZZZZ Inadvertant ground ing of Vital Bus 2 | |||
2328 hours on the 16th. | ( | ||
1 1 | i caused a reactor trip at 1026 hours. | ||
The Station returned to service at 2328 hours on the 16th. | |||
4 1 | |||
1 1 | |||
2 3 | |||
4 F F.uted Reas m: | |||
Method: | |||
Exhibil G - Insinut siims S-Schedu8cd A Equipment Failure (Explain) t-Manual fin Pseparais.m of Data B-Maintenance e*i Test 2-Manual seraan l~rier) Shetislo'I*en5cc C RefuelinE 3-Automatic Scram Fseni Rep.wo Il l'RII de q NtIRI G l, | |||
D Regidanoi> Restslctiim 4-Continued From Previous Month (llfil l l' Openalis Tsaining A liciise l'xaniinati"'' | |||
5-Reduction I Adminisssative 9-Other 5 | |||
G Operatiusial I isne il aplain t I sluhis 1 - Sanw,Sunse l'8/77) ll Oshes flitplaini i | |||
e}} | e}} | ||
Latest revision as of 20:14, 11 December 2024
| ML20138A817 | |
| Person / Time | |
|---|---|
| Site: | Beaver Valley |
| Issue date: | 09/30/1985 |
| From: | Smith P DUQUESNE LIGHT CO. |
| To: | |
| Shared Package | |
| ML20138A815 | List: |
| References | |
| NUDOCS 8512120118 | |
| Download: ML20138A817 (7) | |
Text
.
NARRATIVE
SUMMARY
OF MONTHLY OPERATING EXPERIENCE September 1985 i
September 1 The Unit entered the mcnth in Mode 5 as a result of a reactor trip / safety injection due to a
loss of instrument air which occurred on August 29, 1985. Plant heat up began on the 1st with the Unit entering Mode 4 at 1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br />.
September 2 Plant heat-up continued with the Unit entering Mode 3 at 0108 hours0.00125 days <br />0.03 hours <br />1.785714e-4 weeks <br />4.1094e-5 months <br />.
September 3 Plant heat-up continued wi th reactor criticali ty achieved at 1247 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.744835e-4 months <br /> and the Unit being synched to the grid at 1411 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.368855e-4 months <br />.
September 4 The Station operated at a reduced power level of approximately 57 percent as a result of maintenance being performed on feedwater pump [ FW-P-1A).
September 5 Repai rs to feedwater pump [ FW-P-1A] were completed at 1153 hours0.0133 days <br />0.32 hours <br />0.00191 weeks <br />4.387165e-4 months <br /> and power level was subsequently increased to a nominal 100 percent.
September 6 The Station was in Operational Mode 1 with reactor power through at a nominal 100 percent.
Reactor Coolant System was September 15 at a normal operating pressure and temperature.
September 16 Inadve rtant grounding of Vital Bus #2 caused the Loop B OTAT and OPAT bistables to trip producing a reactor trip at 1026 hours0.0119 days <br />0.285 hours <br />0.0017 weeks <br />3.90393e-4 months <br />.
The reactor achieved criticality at 2203 hours0.0255 days <br />0.612 hours <br />0.00364 weeks <br />8.382415e-4 months <br /> and the Unit was synched to the grid at 2328 hours0.0269 days <br />0.647 hours <br />0.00385 weeks <br />8.85804e-4 months <br />.
September 17 The Station was in Operational Mode 1 with reactor through power at a nominal 100 percent.
Reactor Coolant September 25 4 System was at normal operating pressure and temperature.
8512120118 851003 DR ADOCK 05000334 PDR 1
September 1985 Summary of Monthly Operating Experience September 26 At 1023 hours0.0118 days <br />0.284 hours <br />0.00169 weeks <br />3.892515e-4 months <br /> the plant P250 computer began reading N42 and N43 approximately 20 percent low.
This resulted in two channels calculating an erroneous targeta 0.
At 1120 hours0.013 days <br />0.311 hours <br />0.00185 weeks <br />4.2616e-4 months <br /> operators noticed the rod position indicators (RPI's) for control banks C and D reading 200 steps with the rods actually at 228 and 225 steps. At 1125 hours0.013 days <br />0.313 hours <br />0.00186 weeks <br />4.280625e-4 months <br />, the interaction between the plant variable computer and the plant P250 com t deenergized and both the operations were no$pu er was RPIs and the a monitor returned to normal.
Plant t affected by this event.
September 27 The Station was in Operational Mode I with reactor through power at a nominal 100 percent.
Reactor Coolant System September 30 was at normal operating pressure and temperature.
^
1 2
OPERATI G DATA REPORT DOCKET NO. 50-334 DATE 10/3/63 COMPLETED BY P. A.
Smith TELEPHONE. 417-641-1825 OPERATING STATUS l
I. Unit Name: Beaver Valley Power Station, Unit il Notes September 1985
- 2. Reporting Period:
- 3. t l===d Thermal Power (MWt):
2W
- 4. Nameplate Rating (Gross MWe):
923 835
- 5. Design Electrial Rating (Net MWe):
- 6. Maximum Dependable Capacity (Gross MWe):
860
- 7. Maximum Dependable Capacity (Net MWe):
810
- 8. If Cheness Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
e
- 9. Power Level To Which Restricted.If Any (Net MWe):
None
- 10. Reasons For Restrictions,if Any:
N/A This MontJi Yr. tete
' Cumulative
- 11. Hours In Reporting Period 720.0 6',551.0 82,559.0
- 12. Number Of Hours Reactor Was Caitical 647.6 6,062.2 43,417.9
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 4.482.8
- 14. Hours Generator On-Line 644.8 5.915.0 41.997.9
- 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated (MWH) 1.627.823.0 14,513,009.9 97,911,523.9
- 17. Gross Electrical Energy Generated (MWH) 517,000.0 4,657,000.0 31,151,400.0
~
- 18. Net Electrical Energy Generated (MWH) 485.300.0 4.366.550.0 28,991,393.0
- 19. Unit Service Factor 89.6 90.3 53.3
- 20. Unit Availability Factor 89.6 90.3 53.3
- 21. Unit Capacity Factor (Using MDC Neti 83.2 82.3 46.9
- 22. Unit Capacity Factor iUsing DER Net) 80.7 79,8 45.5
- 23. Unit Forced Outage Rate 10.4 g,5 24.8
- 24. Shutdowns Scheduled Over Next 6 Months ! Type.Dete.snd Duration of Eacht:
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units in Test Status (Priur to Commercial Operationi:
Forecast Achieved INITIA L CRITICALITY N/A N/A INITIA L ELECTRICITY N/A_
N/A COMMERCIAL OPERATION N/A N/A 4
<,,77)
\\\\
1
t MAJOR MAINTENANCE 1.
Maintenance of Feedwater Pump [FW-P-1 A].
2.
Repaired Main Steam Trip Valves [TV-MS-101B] and [TV-MS-101C].
3.
Maintenance of Station Air Compressor [SA-C-1A] and [S A-C-1B].
4.
Inspected and repaired Steam Driven Auxiliary Feedwater Pump [FW-P-2].
4 a
t i
I r
I e
+ -
..m,,
-+y-v-w:.1 v-
=,
---w--
---er--
+
-v-
AVERAGE DAll UNIT POWER LEVEL.
t DOCKET NO.
50~334 UNIT 3V?S U::1: 41 10/3/85 DATE P.A. Smith COMPLETED BY TELEPHONE (412) 643-1825 SEPTEMBER Mom DAY AVERACE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 0 g
37 667 0
788 2
18 l
3 135 827 39 784 20 582 784 23 783 6
785 7
22 7
785 784 73 4
783 g
24 786 785 25 789 9
742 10 26 788 II 827 829 27 747 j
12 28 789 13 788 39 1
i-14 790 787 30 15 789 31 i
.339 t
16 INSTRUCTIONS On this format. fist the average d:ily unit power le.c!!n MWe. Net Or esch day in the reputtine month. Compute to t
the ne: rest whole mepwatt.
I 19/77 )
. _ _., _ - ~..
UNITSHUTDOWNS ANDPOWER REDUCTIONS DOCKET NO.
50-334 UNIT NAME BVPS Unit #1 DATE 10/3/85 REPORT MONIH SEPTEMBER COMPLETED BY P. A.
Smith TELEPilONE (412) 643-1825 "u
en
- o 0
- N C.0 t Licensee Cause, & Corrective g
,a e
No.
Date
%5 3UE Event
!e Action to
- e R
"5 l
5,E "
Report #
$3 eo Prevent Recurrence H
E M
y*y NU O
8 30 850901 F
62.2 A
4 85-015 PA AIRDRY The Station remained off line follow-ing a reactor trip / safety injection due to a loss of instrument air caused by a broken line on the instrument air dryer.
Repairs were made and the Station returned to service at 1411 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.368855e-4 months <br /> on the 3rd.
31 850903 F
0 B
5 N/A CH PUMPXX The Station was operating at s' reduced power level as a result of maintenance being performed on feedwater pump [FW-P-1A].
(CONTINUED) 1 2
3 4
F: F used Reasam:
Hethod:
1.mlubit G. Insisus siims S Schedueil A-Eiguipment Failure (Emplain) 1-Manual fin Psepasasi.m os Dana 8
B. Maintenance of Test 2-Manual scree I nis) Sheels l'w I kernce C Refuelint 3-Automatic Scram F$cn' Relant 81 l'RII de INllRI G D-Regulatoey Restricii.*
4-Continued From Frevious Month Ultill I Openalais Tsaining A license Examinati"
5-Ite<'uc tion I: Adnunistrative 9-Other 5
G Operatiimal I s eios 11 aplaml I sinhis I Same S. misc 08/77)
II OtherflN plaiul
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.
50-334 UNIT NAME BVPS Unit il DATE - 10/3/85 REPORT MONIH SEPTEMBER COMPLETED BY P.
A.
Smith TELErtlONE (412) 643-1825 S
cn
% MO oa 0." t Licensee
$#5 Cause, & Corrective a
No.
Date 0
'E t', E Event f4 Action to R
"5 5
5.E "
Report #
e o ao Prevent Recurrence H
S M
y*g NU O
e 31 (CONTINUED)
Repairs to feedwater pump [FW-P-1A]
completed at 1153 hours0.0133 days <br />0.32 hours <br />0.00191 weeks <br />4.387165e-4 months <br /> on the 5th and power level was subsequently increased.
32 850916 F
13.0 A
3 85-016 EG ZZZZZZ Inadvertant ground ing of Vital Bus 2
(
i caused a reactor trip at 1026 hours0.0119 days <br />0.285 hours <br />0.0017 weeks <br />3.90393e-4 months <br />.
The Station returned to service at 2328 hours0.0269 days <br />0.647 hours <br />0.00385 weeks <br />8.85804e-4 months <br /> on the 16th.
4 1
1 1
2 3
4 F F.uted Reas m:
Method:
Exhibil G - Insinut siims S-Schedu8cd A Equipment Failure (Explain) t-Manual fin Pseparais.m of Data B-Maintenance e*i Test 2-Manual seraan l~rier) Shetislo'I*en5cc C RefuelinE 3-Automatic Scram Fseni Rep.wo Il l'RII de q NtIRI G l,
D Regidanoi> Restslctiim 4-Continued From Previous Month (llfil l l' Openalis Tsaining A liciise l'xaniinati"
5-Reduction I Adminisssative 9-Other 5
G Operatiusial I isne il aplain t I sluhis 1 - Sanw,Sunse l'8/77) ll Oshes flitplaini i
e