TXX-5033, Interim Deficiency Rept CP-86-36 Re Pipe Support Mods. Initially Reported on 860609.No Addl Instances Reportable Per 10CFR50.55(e) Identified During Continuing Engineering Evaluation.Next Rept Will Be Submitted on or About 861029: Difference between revisions

From kanterella
Jump to navigation Jump to search
StriderTol Bot insert
 
StriderTol Bot change
 
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:.-      .                                                                                      Log # TXX-5033-File # 10010 903.9 TEXAS UTILITIES GENERATING COMPANY
{{#Wiki_filter:Log # TXX-5033-File # 10010 903.9 TEXAS UTILITIES GENERATING COMPANY MKYWAY TOWER. 400 NORTH OEJVE STREET. L.B. 81. IBAILAS. TEXAS 78201 September 26, 1986 UNTEiNY.7.*.h b $ h & {h y I Mr. Eric H. Johnson, Director 6@ 2 9 $
            ,          MKYWAY TOWER . 400 NORTH OEJVE STREET. L.B. 81. IBAILAS. TEXAS 78201 September 26, 1986 UNTEiNY.7.*.h                                                                               b $ h & {h y       I Mr. Eric H. Johnson, Director Division of Reactor Safety and Projects 6@ 2 9 $
Division of Reactor Safety and Projects i
i g U. S. Nuclear Regulatory Commission                                                                   'S 611 Ryan Plaza Drive, Suite 1000                                             L Arlington, TX 76012
g U. S. Nuclear Regulatory Commission
'S 611 Ryan Plaza Drive, Suite 1000 L
Arlington, TX 76012


==SUBJECT:==
==SUBJECT:==
COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)
COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)
DOCKET NOS. 50-445 AND 50-446 PIPE SUPPORTS SDAR:   CP-86-36 (INTERIM REPORT)
DOCKET NOS. 50-445 AND 50-446 PIPE SUPPORTS SDAR:
CP-86-36 (INTERIM REPORT)


==Dear Mr. Johnson:==
==Dear Mr. Johnson:==
 
On June 9,1986, we notified you of a reportable item involving the scope of plant modifications resulting from the project's pipe support reverification program (see TXX-4844).
On June 9,1986, we notified you of a reportable item involving the scope of plant modifications resulting from the project's pipe support reverification program (see TXX-4844). This is a follow-up interim report on a reportable item under the provision of 10CFR50.55(e). We have submitted an interim report logged TXX-4958, dated August 13, 1986.
This is a follow-up interim report on a reportable item under the provision of 10CFR50.55(e). We have submitted an interim report logged TXX-4958, dated August 13, 1986.
The continuing engineering evaluation has not identified any additional instances which are considered reportable pursuant to 10CFR50.55(e). The attached list shows the support modifications initiated to date. The evaluation of this issue is continuing and we anticipate submitting our next report by October 29, 1986.
The continuing engineering evaluation has not identified any additional instances which are considered reportable pursuant to 10CFR50.55(e). The attached list shows the support modifications initiated to date. The evaluation of this issue is continuing and we anticipate submitting our next report by October 29, 1986.
Very truly yours, V/VJ W. G. Counsil JCH/amb Attachment c - NRC Region IV (0 + 1 copy)
Very truly yours, V/VJ W. G. Counsil JCH/amb Attachment c - NRC Region IV (0 + 1 copy)
Director, Inspection and Enforcement (15 copies)
Director, Inspection and Enforcement (15 copies)
U. S. Nuclear Regulatory Commission Washington, D. C. 20555 8610090139 860926 PDR   ADOCK 05000445 S                     PDR A snvsnum or ruxas vtut.orsen vs.scime cemesur
U. S. Nuclear Regulatory Commission Washington, D. C.
                                                                                                      }
20555 8610090139 860926 PDR ADOCK 05000445 S
 
PDR
.. e. s >
}
ATTACHMENT PIPE SUPPORT MODIFICATIONS Number of Unit         Cateaory                         Modifications I       Prudent                               762*
A snvsnum or ruxas vtut.orsen vs.scime cemesur
Recent Industry Practice             921 Adjustment                             56 Cumulative Effects                   237 II       Prudent                             1265 Recent Industry Practice             209 Adjustment                             63 Cumulative Effects                   319 o
: e. s >
ATTACHMENT PIPE SUPPORT MODIFICATIONS Number of Unit Cateaory Modifications I
Prudent 762*
Recent Industry Practice 921 Adjustment 56 Cumulative Effects 237 II Prudent 1265 Recent Industry Practice 209 Adjustment 63 Cumulative Effects 319 o
The reduction in this category from the previous report represents Trapeze supports that were previously identified for modification, and were subsequently deleted; thus were recategorized in "Recent Industry Practice".}}
The reduction in this category from the previous report represents Trapeze supports that were previously identified for modification, and were subsequently deleted; thus were recategorized in "Recent Industry Practice".}}

Latest revision as of 02:03, 6 December 2024

Interim Deficiency Rept CP-86-36 Re Pipe Support Mods. Initially Reported on 860609.No Addl Instances Reportable Per 10CFR50.55(e) Identified During Continuing Engineering Evaluation.Next Rept Will Be Submitted on or About 861029
ML20210T697
Person / Time
Site: Comanche Peak  
Issue date: 09/26/1986
From: Counsil W
TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC)
To: Johnson E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
References
CP-86-36, TXX-5033, NUDOCS 8610090139
Download: ML20210T697 (2)


Text

Log # TXX-5033-File # 10010 903.9 TEXAS UTILITIES GENERATING COMPANY MKYWAY TOWER. 400 NORTH OEJVE STREET. L.B. 81. IBAILAS. TEXAS 78201 September 26, 1986 UNTEiNY.7.*.h b $ h & {h y I Mr. Eric H. Johnson, Director 6@ 2 9 $

Division of Reactor Safety and Projects i

g U. S. Nuclear Regulatory Commission

'S 611 Ryan Plaza Drive, Suite 1000 L

Arlington, TX 76012

SUBJECT:

COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)

DOCKET NOS. 50-445 AND 50-446 PIPE SUPPORTS SDAR:

CP-86-36 (INTERIM REPORT)

Dear Mr. Johnson:

On June 9,1986, we notified you of a reportable item involving the scope of plant modifications resulting from the project's pipe support reverification program (see TXX-4844).

This is a follow-up interim report on a reportable item under the provision of 10CFR50.55(e). We have submitted an interim report logged TXX-4958, dated August 13, 1986.

The continuing engineering evaluation has not identified any additional instances which are considered reportable pursuant to 10CFR50.55(e). The attached list shows the support modifications initiated to date. The evaluation of this issue is continuing and we anticipate submitting our next report by October 29, 1986.

Very truly yours, V/VJ W. G. Counsil JCH/amb Attachment c - NRC Region IV (0 + 1 copy)

Director, Inspection and Enforcement (15 copies)

U. S. Nuclear Regulatory Commission Washington, D. C.

20555 8610090139 860926 PDR ADOCK 05000445 S

PDR

}

A snvsnum or ruxas vtut.orsen vs.scime cemesur

e. s >

ATTACHMENT PIPE SUPPORT MODIFICATIONS Number of Unit Cateaory Modifications I

Prudent 762*

Recent Industry Practice 921 Adjustment 56 Cumulative Effects 237 II Prudent 1265 Recent Industry Practice 209 Adjustment 63 Cumulative Effects 319 o

The reduction in this category from the previous report represents Trapeze supports that were previously identified for modification, and were subsequently deleted; thus were recategorized in "Recent Industry Practice".