TXX-6511, Interim Deficiency Rept CP-86-41 Re small-break LOCA Evaluations of Effects of Operational Status of Equipment During Mode 4.Initially Reported on 860528.Westinghouse Owners Group Evaluating Issue.Next Rept Expected by 880229: Difference between revisions

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{{#Wiki_filter:1 1
{{#Wiki_filter:1 1
Log # TXX-6511 File # 10110 Ref #     FR50.55(e)     !
Log # TXX-6511 File # 10110 Ref #
                                                      ~
FR50.55(e)
TUELECTRIC                       June 12,1987               I William G. Counsli Executive Vice President U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 J
~ --
TUELECTRIC June 12,1987 I
William G. Counsli Executive Vice President U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 J


==SUBJECT:==
==SUBJECT:==
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DOCKETS NOS. 50-445 AND 50-446 SMALL BREAK LOCA MODE 4 OPERATION SDAR: CP-86-41 (INTERIM REPORT)
DOCKETS NOS. 50-445 AND 50-446 SMALL BREAK LOCA MODE 4 OPERATION SDAR: CP-86-41 (INTERIM REPORT)
Gentlemen:
Gentlemen:
On May 28, 1986, we verbally notified your Mr. Ian Barnes of a deficiency involving small break LOCA evaluations regarding the effects of the                                       j operational status of plant equipment during Mode 4 operation. This is an                                 !
On May 28, 1986, we verbally notified your Mr. Ian Barnes of a deficiency involving small break LOCA evaluations regarding the effects of the j
interim report of a potentially reportable item under the provisions of                                   j 10CFR50.55(e).           Our most recent interim report was logged TXX-6062, dated                       ;
operational status of plant equipment during Mode 4 operation. This is an interim report of a potentially reportable item under the provisions of j
October 29, 1986.
10CFR50.55(e).
J!
Our most recent interim report was logged TXX-6062, dated October 29, 1986.
At this time, the issue of Small Break LOCA in Mode 4 has not been resolved by                             i the Westinghouse Owners Group (WOG).                   The WOG met with the NRC staff on                 l November 6,1986, in Bethesda to discuss the W0G's plans for resolving the                                 !
J At this time, the issue of Small Break LOCA in Mode 4 has not been resolved by i
issue. As a result of questions arising from that meeting, the WOG sent a                                 i letter to the NRC dated January 8, 1987, (0G-209) which discussed the                                     !
the Westinghouse Owners Group (WOG).
feasibility of applying Leak-Before-Break Technology in the resolution of this                           !
The WOG met with the NRC staff on l
issue.                                                                                                   1 All WOG activities have been on hold pending word from the NRC, with the                                   !
November 6,1986, in Bethesda to discuss the W0G's plans for resolving the issue. As a result of questions arising from that meeting, the WOG sent a i
exception of the Operations Subcommittee's effort to prepare procedural                                   I guidance which will help operators deal with a LOCA in the shutdown modes.                                 !
letter to the NRC dated January 8, 1987, (0G-209) which discussed the feasibility of applying Leak-Before-Break Technology in the resolution of this issue.
This interim guidance was sent to WOG representatives in W0G-87-102 dated                                 J May 12, 1987, and it is being evaluated by TV Electric.
1 All WOG activities have been on hold pending word from the NRC, with the exception of the Operations Subcommittee's effort to prepare procedural I
guidance which will help operators deal with a LOCA in the shutdown modes.
This interim guidance was sent to WOG representatives in W0G-87-102 dated J
May 12, 1987, and it is being evaluated by TV Electric.
We anticipate submitting our next report on this issue by February 29, 1988, i
We anticipate submitting our next report on this issue by February 29, 1988, i
Very truly yours,         ,
Very truly yours, M
M W. G. Counsil             1 JCH/gj                                                                                                     I l
W. G. Counsil 1
c - R. D. Martin, Region IV                                                                               ;
JCH/gj I
Resident Inspectors, CPSES (3)                                                                     l 8706170385 070612 PDR       ADOCK 05000445                                                                         Th O S                             PDR                                                                 h       t 0
l c - R. D. Martin, Region IV Resident Inspectors, CPSES (3) l 8706170385 070612 O
400 North Olive Street LB 81 Dallas, Texas 75201
PDR ADOCK 05000445 Th t
                                                                                                                !}}
S PDR h
0 400 North Olive Street LB 81 Dallas, Texas 75201
!}}

Latest revision as of 23:14, 3 December 2024

Interim Deficiency Rept CP-86-41 Re small-break LOCA Evaluations of Effects of Operational Status of Equipment During Mode 4.Initially Reported on 860528.Westinghouse Owners Group Evaluating Issue.Next Rept Expected by 880229
ML20215B620
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 06/12/1987
From: Counsil W
TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC)
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
CP-86-41, TXX-6511, NUDOCS 8706170385
Download: ML20215B620 (1)


Text

1 1

Log # TXX-6511 File # 10110 Ref #

FR50.55(e)

~ --

TUELECTRIC June 12,1987 I

William G. Counsli Executive Vice President U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 J

SUBJECT:

COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)

DOCKETS NOS. 50-445 AND 50-446 SMALL BREAK LOCA MODE 4 OPERATION SDAR: CP-86-41 (INTERIM REPORT)

Gentlemen:

On May 28, 1986, we verbally notified your Mr. Ian Barnes of a deficiency involving small break LOCA evaluations regarding the effects of the j

operational status of plant equipment during Mode 4 operation. This is an interim report of a potentially reportable item under the provisions of j

10CFR50.55(e).

Our most recent interim report was logged TXX-6062, dated October 29, 1986.

J At this time, the issue of Small Break LOCA in Mode 4 has not been resolved by i

the Westinghouse Owners Group (WOG).

The WOG met with the NRC staff on l

November 6,1986, in Bethesda to discuss the W0G's plans for resolving the issue. As a result of questions arising from that meeting, the WOG sent a i

letter to the NRC dated January 8, 1987, (0G-209) which discussed the feasibility of applying Leak-Before-Break Technology in the resolution of this issue.

1 All WOG activities have been on hold pending word from the NRC, with the exception of the Operations Subcommittee's effort to prepare procedural I

guidance which will help operators deal with a LOCA in the shutdown modes.

This interim guidance was sent to WOG representatives in W0G-87-102 dated J

May 12, 1987, and it is being evaluated by TV Electric.

We anticipate submitting our next report on this issue by February 29, 1988, i

Very truly yours, M

W. G. Counsil 1

JCH/gj I

l c - R. D. Martin, Region IV Resident Inspectors, CPSES (3) l 8706170385 070612 O

PDR ADOCK 05000445 Th t

S PDR h

0 400 North Olive Street LB 81 Dallas, Texas 75201

!